05000483/FIN-2017003-01
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Finding | |
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Title | Spurious Containment Spray Pump Start |
Description | The inspectors reviewed a self -revealed, non- cited violation of Technical Specification 5.4.1.a, Procedures, for the licensees failure to implement Preventative Maintenance Basis document IC-LSELS, Load Shed and Emergency Load Sequencer (LSELS), Revision 0. Specifically, the licensee failed to replace load shed and emergency load sequencer relay driver Card NF039AR06SL23, a Consolidated Controls 6N232 relay driver card, within the scheduled periodicity. On June 28, 2017, containment spray train A pump , PEN01A, spuriously started due to the cards failure. As a result, one train of the containment spray system was rendered inoperable for a total of 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br />, of which all 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> w ere unplanned. As immediate corrective actions, the licensee replaced the circuit card under Job 17002747, completed post -maintenance testing, and restored the system to operable status on June 30, 2017. The licensee entered this issue into the corrective action program under Condition Report 20170 3433. The failure to replace load shed and emergency load sequencer relay driver Card NF039AR06SL23 within the scheduled periodicity was a performance deficiency. This performance deficiency was more than minor , and therefore a finding, because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone and its objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, o n June 28, 2017, containment spray train A pump , PEN01A, spuriously started due to the cards failure. As a result, one train of the containment spray system was rendered inoperable for a total of 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> . Using Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings At - Power, Exhibit 2, Mitigating Systems Screening Questions, dated June 19, 2012, the inspectors determined the finding was of very low safety significance (Green) because (1) the finding was not a deficiency affecting the design or qualification of a mitigating system; (2) the finding did not represent a loss of system and/or function; ( 3) the finding did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) the finding does not represent an actual loss of function of one or more non- technical specification trains of equipment designated as high safety -significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Specifically, the total duration of inoperability was 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> which is less 3 than the technical specification allowed completion time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for this system. The finding had a cross -cutting aspect in the area of problem identification and resolution associated with resolution because the licensee failed to take effective corrective actions to address issues in a timely manner commensurate with their safety significance. Specifically, the licensee did not replace load shed and emergency load sequencer relay driver Card NF039AR06SL23 prior to failure although this issue was documented in corrective actions ranging from April 2008 to January 2017 [P.3]. |
Site: | Callaway |
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Report | IR 05000483/2017003 Section 1R12 |
Date counted | Sep 30, 2017 (2017Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.12 |
Inspectors (proximate) | D Bradley S Janicki B Bartlett K Clayton C Cowdrey M Hayes C Stott N Taylor |
Violation of: | Technical Specification - Procedures |
CCA | P.3, Resolution |
INPO aspect | PI.3 |
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Finding - Callaway - IR 05000483/2017003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Callaway) @ 2017Q3
Self-Identified List (Callaway)
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