A self-revealing finding was identified for the failure to properly repair condensate Demineralizer 1E tank liner prior to returning it to service. As a result, failure of the liner resulted in approximately 20,000 gallons of radiological contaminated condensate being spilled from the manway
flange. Operations lowered reactor power from 90 percent to 82 percent to conserve condensate system inventory. This issue was entered into the licensees corrective action program as Condition Report
RBS-2007-5440. The finding is greater than minor because it was associated with the equipment performance attribute of the
initiating events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown and power operations. Using the
NRC Manual Chapter 0609,
Significance Determination Process, Phase 1 worksheet, the finding was considered to be a
transient initiator contributor which contributed to both the likelihood of a
reactor trip and the likelihood that mitigation equipment or functions would not be available and, therefore, screened to Phase 2. Using the Phase 2 worksheets, the inspectors assumed that successful recovery of the condensate system from the leak was highly likely and determined the finding to be of very low safety significance. This finding has crosscutting aspects associated with human performance in the area of resources in that a complete, accurate, and up-to-date work package was not available to assure nuclear safety
H.2(c) (Section 1R19.2).