05000454/FIN-2013007-02
From kanterella
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Failure to Properly Assess Operability of the 2A EDG Following Post-Modification Testing |
Description | The inspectors identified a finding of very low safety significance and an associated NCV of Technical Specification (TS) 3.8.1 when licensee personnel failed to properly assess the operability of the 2A emergency diesel generator (EDG) following a post-maintenance test that rendered the 2A EDG ventilation fan, a credited support system, incapable of performing its auto-start support system function for a period of two days. As part of the licensees immediate corrective actions, a trip signal that prevented the 2A EDG fan from starting was reset. The licensee entered this issue into their CAP as IR 1252529, 2A DG [EDG] Vent Fan Trip Signal Not Reset. The performance deficiency was determined to be more than minor because it was associated with the Configuration Control and Human Performance attributes of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, following an August 15, 2011, post-maintenance test of the 2A EDG room ventilation system high differential pressure (D/P) trip time delay, the licensee failed to implement the necessary procedural steps that ensured the high D/P trip signal was reset. This resulted in the 2A EDG room ventilation fan from auto-starting, resulting in the inoperability of the 2A EDG from August 15-17, 2011. The inspectors determined that this finding screened as having very low safety significance (Green) in accordance with IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings at Power, Exhibit 2, Mitigating Systems Screening Questions, as it did not represent an actual loss of function of at least a single train of safety-related equipment for greater than its Technical Specification (TS) allowed outage time and did not represent an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. This issue had a cross-cutting aspect in the Work Practices component of the Human Performance cross-cutting area (H.4(a)), because licensee personnel failed to use appropriate human performance techniques to ensure that work tasks were performed safely and individuals do not proceed in the face of uncertainty. |
Site: | Byron |
---|---|
Report | IR 05000454/2013007 Section 4OA2 |
Date counted | Sep 30, 2013 (2013Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | A Dahbur B Bartlett C Thompson E Duncan M Jones N Shah |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | H.12, Avoid Complacency |
INPO aspect | QA.4 |
' | |
Finding - Byron - IR 05000454/2013007 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Byron) @ 2013Q3
Self-Identified List (Byron)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||