05000445/LER-1993-001, :on 930118,trip Blocks Were Not in Place for Switch Manipulation & Reactor Trip Occurred While Restoring Ssps to Normal Lineup.Caused by Personnel Error.Event Reviewed & Training & Procedure Revised
| ML20128M733 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 02/16/1993 |
| From: | William Cahill, Reimer D TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| LER-93-001, LER-93-1, TXX-93100, NUDOCS 9302220258 | |
| Download: ML20128M733 (8) | |
| Event date: | |
|---|---|
| Report date: | |
| 4451993001R00 - NRC Website | |
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TUELECTRIC y4 February 16, 1993 WUllam J. Cahllt, Jr.
Gmur Ywe President U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STA110N (CPSES)
DOCKET NO. 50-445 REACTOR PROTECTION SYSTEM ACTUATION LICENSEE EVENT REPORT 93-001-00 Gentlemen:
Enclosed is Licensee Event Report 93-001-00 for Comanche Peak Steam Electric Station Unit 1, " Reactor Trip Caused by Personnel Error during Solid State Protection System Testing."
Sincerely, William J. Cahill, Jr.
By:
o', J. Kelley, Jr.
Vice President of Nuclear Operations OB/tg Enclosure c-Mr. J. L. Milhoan, Region IV Mr. L. A. Yandell, Region IV Resident Inspectors, CPSES (2) 9302220258 930216 PDR ADOCK 05000445 S
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%.mee m.i pe At 1144 on January 18,1993, while restoring the Solid State Protection System (SSPS) from a test lineup, the Reactor Operator used an incorrect instruction. As a result, trip blocks were not in p' ace for switch manipulation and a reactor trip occurred while restoring SSPS to a normallineup.
Root cause of the event was personnel error. Contributing factors were that a test procedure reference was not specific which led the RO to an incorrect instruction and that senior supervision moni oring during the restoration was less than adequate. Corrective t
actions included event review, training and procedure revision.
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1.
DESCRIPTION OF THE REPORTABLE EVENT
A.
REPORTABLE EVENT CL ASSIFICATION l
Any event or condition that resulted in manual or automatic actuation of any-Engineered Safety Feature (ESF), including the Reactor Protection System =
(RPS)(Ells:(JC)).
B.
PLANT OPERATING CONDITIONS PRIOR TO THE EVENT On January 18,1993, Comanche Peak Steam Electric Station (CPSES) Unit 1 was in Mode 1, Power Operation, with reactor power at 100 percent.
C.
STATUS OF STRUCTURES. SYSTEMS. OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT There were no inoperable structures, systems or components that contributed to the event.
D.
NARRATIVE
SUMMARY OF THE EVENT. INCLUDING DATES AND l
APPROXIMATE TIMES At 1130 on January 18,1993, a Train A Solid State Protection System (SSPS) logic test had just been completed and the Reactor Operator (RO)(utility, licensed) was proceeding to return SSPS to a Normallineuo. The Shift Technical Advisor / Unit Supervisor (STA/US)(utility, licensed), a Senior Reactor Operator, was supervising the RO during testing as required by plant management for activities identified as "high risk".
The test procedure referenced the Standard Operating Procedure (SOP) for SSPS for instructions on how to restore SSPS to a Normal lineup. The test procedure did not reference a specific section of the SOP and the Reactor Operator went to an attachment titled, " Control Switch Lineup Sheet - Normal Lineup", which he had correctly used earlier in the test procedure to verify the initial SSPS switch lineup prior to starting the actual test in this case, however, the RO should have gone to the body of the procedure to the section titled," Disabled Lineup to Normal Lineup OR
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Disabled Lineup to Mode 5/6 Lineup." The attachments of the SOP are verification sheets only and were not to be used for switch manipulation. As a result of using the verification sheet, the required trip block was not in place when the RO took the INPUT ERROR INHIBIT switch to NORMAL. Both the RO and STA/US had incorrectly assumed that since the Mode Selector switch on the SSPS Output Relay Test Panel was in TEST that the required blocks were in place. The STA/US had also started -
reviewing test data at the conclusion of the test and was not paying as close attention to the RO during restoration as he did during the actual test. The STA/US believed that his responsibilities were primarily 16 monitor the actual test and that the RO would not require monitoring to restore SSPS to the Normallineup. At 1144, the RO j
took the INPUT ERROR INHIBIT switch to NORMAL and a reactor trip occurred.
Following the trip, Control Room personnel responded in accordance with emergency operating procedures. Plant systems responded as expected. The plant was stabilized in Mode 3, Hot Standby. An event or condition that results in an automatic actuation of any ESF, including the RPS,is reportable within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> under 10CFR50.72(b)(2)(ii). At 1250 on January 18,1993, the Nuclear Regulatory Commission Operations Center was notified of the event via the Emergency Notification System.
The investigation following the trip revealed that the previous revision of the test procedure had referenced the specific section in the SOP for restoring SSPS to a Normallineup. The procedure was revised and the reference removed because of problems encountered when procedure sections changed numbers. When a procedure section number was changed, it required that all other procedures referencing that section would also have to change. By removing the specific section number from the referencing procedures this problem was solved; however, the alternative was inadequate in that it led to confusion in this instance.
E.
THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE. OR PROCEDURAL OR PERSONNEL ERROR The reactor trip was annunciated by numerous alarms in the Control Room. The cause of the trip was immediately known.
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COMPONENT OR SYSTEM FAILURES A.
FAILURE MODE. MECHANISM. AND EFFECT OF EACH FAILED COMPONENT Not applicable - there were no component failures associated with this event.
B.
CAUSE OF EACH COMPONENT OR SYSTEM FAILURE Not applicable - there we_re no component failures associated with this event.-
C.
SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not applicable - there were no failed components with multiple functions that affected this event.
D.
FAILED COMPONENT INFORMATIOE Not applicable - there were no component failures associated with this event.
III. ANALYSIS OF THE EVENT
- - A.
SET 7 SYSTEM RESPONSES THAT OCCURRED-A Lo-Lo Steam Generator level signal was generated, resulting in an ESF actuation; actuating the Auxiliary Feedwater System (AFW)(Ells:(BA)). Associated components within these systems functioned as designed. Train B AFW actuated automatically, Train A did not autostart as a result of the configuration of Train A SSPS (the Mode
' Selector switch was still in TEST). This condition was immediately recognized and Train A AFW was manually started at 1147.
B.
DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY Train A SSPS was inoperable during the logic test. After the trip, Train A AFW did not autostart because Train A SSPS had not yet been restored. This _was quickly recognized and Train A AFW was manually started within 3 minutes following the trip and Steam Generator levels were restored.
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C.
SAFETY CONSEQUENCES AND IMPLICATIONS OF-THE EVENT' The reactor trip was the result of personnel error and was not required to mitigate an actual event. This event is best described in Section 15.2.3 of the CPSES Final-Safety Analysis Report (FSAR). The analysis uses conservative assumptions to-demonstrate the Departure from Nucleate Bolling Ratio will never decrease below the limiting value of 1.30 during the event. The event of January 18,1993, occurred at 100 percent reactor power, and all protective functions responded as required.
The event is completely bounded by the FSAR accident analysis. The event _of' January 18,1993, did not adversely affect the safe operation of CPSES Unit 1 or the health and safety of the public.
IV. CAUSE OF THE EVENT
ROOT CAUSE Root cause of the event was personnel error. The RO and STA/US were not sufficiently familiar with the SSPS circuitry in that they incorrectly assumed that sbtficient trip blocks were in place so that the INPUT ERROR INHIBIT switch could be taken to NORMAL without a reactor trip occurring.
CONTRIBUTING FACTORS
- 1. The test procedure did not make a specific enough' reference to' the SOP for SSPST l
restoration. This led the RO to an incorrect set of instructions which led to switch j
manipulation without the required trip blocks being established.
- 2. The STA/US did not monitor the restoration of the test lineup _as closely as he had-monitored the actual test.- The STA/US was reviewing the test results and did not pay i
close enough attention to catch the mistake.
faENERIC CONSIDERATIONS The familiarity with the specifics of the SSPS circuitry ls not consistent among operators.
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V.
CORRECTIVE ACTIONS TO PREVENT RECURRENCE-ROOT CAUSE The RO and STA/US were not sufficiently familiar with the SSPS circuitry.
CORRECTIVE ACTION
The RO and STA/US have received personal counseling. A "_ Lessons Learne' " was d
issued for shift personnel on the details of the event. Formal training is being revised -
to include aspects from this event and to include more detailed objectives and-lessons for operator understanding of the SSPS circuitry.
CONTRIBUTING FACTOR - 1 The test procedure did not make a specific enough reference to the SOP for SSPSi restoration.
CORRECTIVE ACTION
The test procedure was revised to include the applicable sections of the SOP in thei test procedure; therefore, the test procedure no longer references another procedure--
to perform certain steps.
A note was placed with all the verification attachments in the SOP stating th' t the--
a attachments are to be used for verification only and not for actual switch '
manipulation.
CONTRIBUTING FACTOR - 2 The STA/US did not monitor the restoration of the test lineup as closely as he had monitored the actual test.
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CORRECTIVE ACTION
Lessons Learned and formal training will stress that the requirements in place for "high risk activities" include active monitoring until the evolution is complete and equipment is restored to a normal steady-state lineup. The SOP for SSPS has been redefined as a "high risk activity" and will now require the same monitoring requirements as the testing SSPS.
GENERIC CONSIDER ATIONS The familiarity with the specifics of the SSPS circuitry is not consistent among operators.
CORRECTIVE ACTION
A " Lessons Learned" was issued for shift personnel on the details of the event.
Formal training is being revised to include aspects from this event and to include more detailed objectives and lessons for operator understanding of the SSPS circuitry.
VI. PREVIOUS SIMILAR EVENTS
In Licensee Event Report (LER)92-005 a RO was performing slave relay testing. The RO misinterpreted a procedure step and inadvertently unblocked the actuation signal which had been blocked in a previous procedure step. Upon performance of the next procedure step, all four feedwater split flow bypass valves closed. The root cause of this event was also personnel error; however, several of the lessons learned from LER 92-005 have -
been successfully incorporated. The extenuating circumstances in this event was the confusion with the recently revised test procedu e reference and that the SRO (STA/US) monitoring the evolution remained vigilant only L.1til the actual test was complete and did not monitor the restoration as closely.
Vll. ADDITIONAL INFORMATION The times listed in the report are approximate and Central Standard Time.