05000440/FIN-2012005-03
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Finding | |
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Title | |
Description | The inspectors identified a finding of very low safety significance and associated non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure to establish appropriate procedures capable of restoring low-pressure coolant injection (LPCI) mode of residual heat removal (RHR), while in the shutdown cooling (SDC) mode, following a loss-of-coolant accident (LOCA) in Mode 3. Specifically, the licensee failed to prescribe procedures which ensured: (1) LPCI could be restored using only safety-related/seismic structures, systems and components; (2) no unanalyzed water hammer event occurred; (3) the equipment used for venting the system were appropriate; and (4) operator safety was maintained. This finding was entered into the licensees corrective action program and the licensee instituted compensatory actions to declare RHR trains INOPERABLE while aligned to SDC. Additionally, procedures affected are prohibited from use while the plant is in Mode 3. The performance deficiency was determined to be more than minor because, if left uncorrected it could have the potential to lead to a more significant safety concern. Specifically, the inspectors had concerns that procedures, as currently written, would have been unsuccessful in restoring LPCI. The finding screened as having a very low safety significance based on a Phase II Significance Determination Process evaluation. The result was a delta core damage frequency less than 1.0E-6/year. The inspectors determined this finding had a cross-cutting aspect in the area of Problem Identification and Resolution, Operating Experience, because the licensee did not implement operating experience through changes to the stations process, procedures, and equipment. Specifically, the licensees evaluation of Information Notice 2010-11 incorrectly concluded sufficient barriers were in place to prevent the occurrence of steam voiding in the RHR system. |
Site: | Perry ![]() |
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Report | IR 05000440/2012005 Section 4OA5 |
Date counted | Dec 31, 2012 (2012Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | |
Inspectors (proximate) | R Jickling M Marshfield C Moore M Bielby J Laughlin M Learn J Corujo-Sandin J Beavers R Edwards J Nance |
CCA | P.5, Operating Experience |
INPO aspect | CL.1 |
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Finding - Perry - IR 05000440/2012005 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Perry) @ 2012Q4
Self-Identified List (Perry)
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