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PAGE (3 Catawba Nuclear Station, Unit 1 0151010 l 014l 113 1 l0Fl014
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NAME TELEPHONE NUMSER AREA COOE Roger W. Ouellette, Assistant Engineer - Licensing 710 14 31 7131-17151310 COedPLETE 08st LINE FOR EACH CORAPONENT FAILURE DESCRISED IN THIS REPORT (13)
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, oe On January 4, 1985, at 1352:56 hours, Motor-Driven Auxiliary Feedwater (CA) Purcps lA and 1B auto-started during testing of the Turbine Impulse Chamber Pressure. The testing initiated an inadvertent reactor trip signal, which in turn, automatically tripped Main Feedwater (CF) pump 1A (CF pump 1B was not running), and started CA Pumps lA and 1B.
At the time of the incident, Unit I was in Mode 3 (Hot Standby), with an average Reactor Coolant terperature (Tave) of 559"F and Pressurizer pressure of approximately 1830 psig. To recover from the incident, the switch was returned to normal, the react'or trip breakers were closed, CA Pumps lA and IB were tripped. CF pumps lA and IB were reset, and CF pump 1B was started.
This incident is classified as a Personnel Error. The Instrument and Electrical (I&E) Supervisor of the test crew N/A'd a step in the Turbine Impulse Pressure Chamber test section of the procedure without thoroughly analyzing the impact on plant operation. If that step would have been performed, this incident would not have occurred.
This incident is reportable pursuant to 10 CFR 50.73, Section (a) (2)
(iv), and 10 CFR 50.72, Section (b)(2)(ii).
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LER NUMBER (6)
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Catawba Nuclear Station. Unit 1 015101010 l411 13 8l5 0l0l1 0l0 nl ? OF 0l 4 TEXT t# snore spere a segured, use e#conar NAC form JSSA'sJ 1171 Instrument Procedure IP/1/A/3222/00B (Analog Channel Operational Test Channel II 7300) is performed by the Instrun.ent and Electrical (ISE) group monthly per Work Request 3634 SWR to satisfy Technical Specification Surveillance Requirements 4.3.1.1 and 4.3.2.1 for Channel II of the Process Control System.
Section 10.8 of the procedure is the test of the Turbine Impulse Chamber Pressure. During that section, the Turbine Impulse Pressure test switch is placed in the test position, which in turn simulates greater than 10% turbine or reactor power. The actuation of one of two impulse pressure channels serves as an input that gives a P-7 Signal, a signal that unblocks "at power" reactor trips it the Reactor Trip Breakers are closed and P-13 status light (Turbine not at power) is lit. A combination of the P-7 signal and any of the following will initiate a Reactor Trip;
- 1) High Pressurizer Level, 2) Iow Pressurizer pressure, 3) Reactor Coolant Pump Bus Underfrequency,
- 4) Reactor Coolant Pump Bus Undervoltage, 5) Two Reactor Coolant Loops Loss of Flow.
During the performance of procedure IP/1/A/3222/00B, two significant plant conditions existed.
First, the Unit was in Mode 3 with the pressurizer pressure being maintained at approximately 1830 psig. This was because the Upper Head Injection (UHI) System was out of service due to Nuclear Station Modification (NSM) #CN-10337 and because of a high concentration of entrained gases in the UHI accumulator.
Second, rod drop testing was being performed per IP/0/A/3220/01 (Full length Rod Cluster Control Assembly Drop Timing-IRE System).
On January 4, 1985, at approximately 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, Section 10.8 of IP/1/A/3222/00B was started when the I&E Technician notified the Senior Reactor Operator that one Channel of Turbine Impulse Pressure would be tested.
Step 10.8.1 of the procedure gave the following conditions:
If Rx trip breakers are closed and ISI18.14.01 (P-13 Turbine not at power) is on, verify the following annunciators are not in alarm state:
1AD06.01.09 PZR Hi Level Alert IAD06.04.08 PZR Lo Press Alert 1AD06.06.05 UV NC Pump Bus Alert 1AD06.04.05 Under freq. NC Pump Bus Alert Verify that not more than one of the following annunciators are in the alarm state:
1AD06.01.01 Loop A Lo Flow Alert 1AD06.01.02 Loop B Lo Flow Alert 1AD06.01.03 Loop C Lo Flow Alert l
1AD06.01.04 Loop D Lo Flow Alert If any of these conditions exist, DO NOT PROCEED, l
notify I&E Supervisor.
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N NRC Feren 386A U.S. NUCLEla [EGULf. TORY COMMIS$10N LICENSEE EVENT REPORT (LER) TEXT CHNTINUATION uPaovfo Ous No. siso-osa EXPIRE 3. 8/3t /85 FAcaLITY NAME (H DOCKET NUMBER D!
LER NUMSER (6)
PAGE(3)
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'. M YEAR Catawba Nuclear Station, Unit 1 015 l 0 l 0 l 01411 l 3 81 5 0 l0l1 0l0 0 13 OF 0l4 TEXT (# swre space a naquesd, ese menonal NAC Forsn J66A'al(ID The I&E Technician found that the Reactor trip breakers were closed for rod drop testing and ISI18.14.01 was lit.
Then he checked the other alarms. He found annunciator 1AD06.04.08 lit.
This was because pressurizer pressure was less than 1945 psig.
The I&E Technician then asked the Shift Technical Advisor (STA) and Nuclear Control Operator (NCO) about the effects on plant operation by continuing with the procedure.
The SIA and NCO related to him the effects on safety injection by continuing with the procedure. The STA told the I&E Technician that safety injection would not be affected.
After this conversation, the I&E Technician discussed the step with I&E Supervisor A.
After further discussing the step with I&E Supervisor B and an I&E Staff Engineer, I&E Supervisor A decided to continue with the procedure and N/A'd step 10.8.1.
This decision was made because low power reactor trips were believed to be blocked due to the indication of status light 1SI18.11.02 (P-7 low power Reactor Trips blocked). Also, the decision was based on the conversations with the STA and NCO.
At 1351:52:872 hours, the Turbine Impulse Pressure test switch was placed in the test position per step 10.8.3 of IP/1/A/3222/00B by the I&E Technician.
Simultaneously, low power reactor trips were unblocked and a pressurizer low pressure reactor trip signal was initiated. The reactor trip breakers opened. Since Tave was low at the time, a combination of low Tave and a Reactor Trip signal gave a Feedwater Isolation signal. This tripped Main Feedwater (CF) pump A (CF pump B was not running but also received a trip signal). Loss of both CF pumps caused the auto-start of both motor-driven Auxiliary Feedwater (CA) pumps.
Immediately after the incident, the I&E Technician placed the Turbine Impulse Pressure test switch in the normal position.
The Reactor Trip breakers were closed, CF pump 1A was reset, and both CA pumps were shutdown by the NCO. When the NCO attempted to return CF pump 1A to service, its discharge valve would not reopen. The NCO then reset and placed CF pump 1B in service to feed the steam generators. A work request was issued to repair CF pump 1A's discharge valve.
This incident is classified as a Personnel Error.
Since I&E Supervisor A N/A'd and initialed step 10.8.1 in IP/1/A/3222/00B, he is responsible for analyzing the impact on plant operation of not performing the step.
However, I&E Supervisor A did not review logic diagrams or drawings
~
before making his decision. He was under the assumption that P-7 Reactor Trips were blocked, and was unaware that moving the Turbine Impulse Pressure test switch to the test position would unblock those trips. There was also miscommunication. The I&E Supervisor relied on conversation with the STA and NCO instead of discussing the issue with the appropriate individual, the Shift Supervisor.
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.U S. NUCLEJJ kEIULATORY COMMIS510N UCEN!EE EVENT REPORT (LER) TEXT CONTINUATION ueRovEO oMe No siso-cio4 E XPIR ES. $/31/85 FACILITY NAME (Il DOCKEY NUMBER GI LER NUMBER (61 PAGE131 II Ab I] h YEAR Catawba Nuclear Station, Unit 1 0 l5 l0 l0 l01411 l 3 81 5 0 l0 l1
-- 0l0 0 13 OF gl4 rur a mee wa s mens. m aeww nc ram nwmm The I&E Technician found that the Reactor trip breakers were closed for rod drop testing and ISI18.14.01 was lit.
Then he checked the other alarms, He found annunciator 1AD06.04.08 lit.
This was because pressurizer pressure was less than 1945 psig.
The I&E Technician then asked the Shift Technical Advisor (STA) and Nuclear Control Operator (NCO) about the effects on plant operation by continuing with the procedure.
The STA and NCO related to him the effects on safety injection by continuing with the procedure. The STA told the I&E Technician that safety injection would not be affected. After this conversation, the I&E Technician discussed the step with I&E Supervisor A.
After further discussing the step with I&E Supervisor B and an I&E Staff Engineer, I&E Supervisor A decided to continue with the procedure and N/A'd step 10.8.1.
This decision was made because low power reactor trips were believed to be blocked due to the indication of status light ISI18.11.02 (P-7 low power Reactor Trips blocked). Also, the decision was based on the conversations with the STA and NCO.
__ At 1351:52:872 hours, the Turbine Impulse Pressure test switch was placed
~
in the test position-per_ step 10.8.3 of IP/1/A/3222/00B by the I&E Technician.. Simultaneously, low power reactor trips were unblocked and a pressurizer low pressure reactor trip signal was' initiated. The reactor trip breakers opened.
Since Tave was low at the time, a combination of low Tave and a Reactor Trip signal gave a Feedwater Isolation signal. This tripped Main Feedwater (CF) pump A (CF pump B was not running but also received a trip signal). Loss of both CF pumps
~
caused the auto-start of both motor-driven Auxiliary Feedwater (CA) pumps.
Immediately after the incident, the I&E Technician placed the Turbine Impulse Pressure test switch in the normal position.
The Reactor Trip breakers were closed, CF pump 1A was reset, and both CA pumps were shutdown by the NCO.
When the NCO attempted to return CF pump 1A to service, its discharge valve would not reopen. The NCO then reset and placed CF pump 1B in service to feed the steam generators. A work request was issued to repair CF pump 1A's discharge valve.
This incident is classified as a Personnel Error. Since I&E Supervisor A N/A'd and initialed step 10.8.1 in IP/1/A/3222/00B, he is responsible for analyzing the impact on plant operation of not performing the step.
However, I6E Supervisor A did not review logic diagrams or drawings before making his decision. He was under the assumption that P-7 Reactor Trips were blocked, and was unaware that moving the Turbine Impulse Pressure test switch to the test position would unblock those trips. There was also miscommunication. The I&E Supervisor relied on conversation with the STA and NCO instead of discussing the issue with the appropriate individual, the Shift Supervisor.
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NRC Perm 366A U.S. NUCLEMt F.EIULATORY COMMIS$10N I"
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION e.PrRovEo oms No. 3 iso-oio4 E XPIRES. 8/3145 FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMSER (6)
PAGE (3)
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==n Catawba Nuclear Station, Unit 1 0 l5 l0 l0 l0 l4 l 113 81 5 Ol0 l1 010 0l 4 OF 0l4 TEXT (X tmue space e requed, use annonal NRC Form 366A'sn1h It was felt that the procedure was adequate in that it instructed the person to not proceed if any of the conditions were met.
However, the effects of not performing the step were not clearly stated.
CORRECTIVE ACTION
1.
Turbine Impulse Pressure test switch placed in normal position.
2.
Reactor trip breakere closed.
3.
Main Feedwater pumps reset.
4.
CA Pumps shutdown.
5.
Main Feedwater Pump 1B started.
6.
Work Request originated to repair valve ICF10.
7.
I&E will research step 10.8.1 in IP/1/A/3222/00B to see if there are any circumstances that the step can be N/A'd.
If they exist, they will be listed in the procedure step.
If they do not exist, a statement will be added to the step to ensure the individual performing the procedure is aware of the consequences 6f not performing the step.
8.
Personnel will be made aware of the possible effects of N/Aing steps in a procedure through review of this incident.
SAFETY ANALYSIS
All systems functioned as designed upon receipt of a reactor trip signal. Recovery from the incident was achieved promptly.
The health and safety of the public were not affected by this incident.
NRC FOKu 3664
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- - DUKE POWER GOMPANY P.O. BOX 33180 CHARLOTTE. N.C. 28242 HALB. TUCKER Tr_LEPH N E vna r.msson.,
(704) 073-4531 February 1, 1985
.m Document Control Desk U. S. Nuclear. Regulatory Commission Washington, D. C.
20555 Subject: Catawba Nuclear Station, Unit 1 Docket No. 50-413 Gentlemen:
Pursuant to 10 CFR 50.73 Section (a) (1) and (d), attached is Licensee Event Report 413/85-01 concerning the auto-start of motor-driven Auxiliary Feedwater pumps during Turbine Impulse Chamber Pressure test. This event was considered to be of no significance with respect to the health and safety of the public.
Very truly yours, h8 Y
/&
Hal B. Tucker RWO: sib l
Attachment cc:
Mr. James P. O'Reilly, Regional Administrator American Nuclear Insurers U. S. Nuclear Regulatory Commission c/o Dottie Sherman, ANI Library Region II The Exchange, Suite 245 101 Marietta-Street, NW, Suite 2900 270 Farmington Avenue Atlanta, Georgia 30323 Farmington, CT 06032 INPO Records' Center Mr. Jesse L. Riley Suite 1500 Carolina Environmental Study Group 1100 Circle 75 Parkway 854 Henley Place Atlanta, Georgia 30339 Charlotte, North Carolina 28207 Palmetto Alliance M&M Nuclear Consultants 2135h Devine Street 1221 Avenue of the Americas Columbia, South Carolina 29205 New York, New York 10020 Robert Guild, Esq.
NRC. Resident Inspector P. O. Box 12097 Catawba Nuclear Station Charleston, So' '~a Carolina 29412
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| 05000413/LER-1985-001, :on 850104,during Testing of Turbine Impulse Chamber Pressure,Motor Driven Auxiliary Feedwater Pumps 1A & 1B auto-started,initiating Reactor Trip Signal.Caused by Personnel Error.Procedure Reviewed |
- on 850104,during Testing of Turbine Impulse Chamber Pressure,Motor Driven Auxiliary Feedwater Pumps 1A & 1B auto-started,initiating Reactor Trip Signal.Caused by Personnel Error.Procedure Reviewed
| | | 05000413/LER-1985-002, :on 841231,unit Entered Hot Shutdown W/Ice Condenser Lower Inlet Doors Blocked Closed.Incident Discovered on 850109.Caused by Personnel Error.Blocking Devices Removed & Training Sessions Held |
- on 841231,unit Entered Hot Shutdown W/Ice Condenser Lower Inlet Doors Blocked Closed.Incident Discovered on 850109.Caused by Personnel Error.Blocking Devices Removed & Training Sessions Held
| | | 05000413/LER-1985-003, :on 850109,during Monthly Testing of Solid State Protection Sys,Reactor Trip Breaker Opened on High Flux Source Range Reactor Trip Signal.Caused by Procedural Deficiency.Procedure Revised |
- on 850109,during Monthly Testing of Solid State Protection Sys,Reactor Trip Breaker Opened on High Flux Source Range Reactor Trip Signal.Caused by Procedural Deficiency.Procedure Revised
| | | 05000413/LER-1985-004, :on 850114,due to Loss of Reactor Coolant Pump Motor Cooling Water,Reactor Manually Tripped.Caused by Malfunction of Valve 1RN-A83.Valve Opened Manually |
- on 850114,due to Loss of Reactor Coolant Pump Motor Cooling Water,Reactor Manually Tripped.Caused by Malfunction of Valve 1RN-A83.Valve Opened Manually
| | | 05000413/LER-1985-005, :on 850117,during Review of Tech Spec Action Item Log,Discovered Five Occurences When Unit Entered Mode 2 W/Power Range Neutron Monitor Inoperable.Caused by Personnel Error |
- on 850117,during Review of Tech Spec Action Item Log,Discovered Five Occurences When Unit Entered Mode 2 W/Power Range Neutron Monitor Inoperable.Caused by Personnel Error
| | | 05000413/LER-1985-006, :on 850120,hot Standby Initiated After Reactor Coolant Average Temp Could Not Be Increased to Greater than 541 F 15 Minutes After Temp Decrease During Performance of Natural Circulation Verification Test |
- on 850120,hot Standby Initiated After Reactor Coolant Average Temp Could Not Be Increased to Greater than 541 F 15 Minutes After Temp Decrease During Performance of Natural Circulation Verification Test
| 10 CFR 50.73(a)(2)(1) | | 05000413/LER-1985-007, :on 850122,diesel Generators 1A & 1B Started on Blackout Signal.During Troubleshooting on Circuit Breaker 1B,Zone B Lockout Initiated,Causing Trip of 6,900-volt Switchgear.Caused by Design Deficiency |
- on 850122,diesel Generators 1A & 1B Started on Blackout Signal.During Troubleshooting on Circuit Breaker 1B,Zone B Lockout Initiated,Causing Trip of 6,900-volt Switchgear.Caused by Design Deficiency
| | | 05000413/LER-1985-008, :on 850123,reactor Automatically Tripped Due to Steam Generator D lo-lo Level.Caused by Decrease in Auxiliary Steam Flow.Investigation to Be Conducted Re Transmitter Output Tubing Blockage |
- on 850123,reactor Automatically Tripped Due to Steam Generator D lo-lo Level.Caused by Decrease in Auxiliary Steam Flow.Investigation to Be Conducted Re Transmitter Output Tubing Blockage
| | | 05000413/LER-1985-009, :on 850131,during Loss of Control Room Functional Test,Safety Injection Occurred.Caused by Component Malfunction.Safety Injection Reset,Closing Cold Leg Safety Injection Valve |
- on 850131,during Loss of Control Room Functional Test,Safety Injection Occurred.Caused by Component Malfunction.Safety Injection Reset,Closing Cold Leg Safety Injection Valve
| | | 05000413/LER-1985-010, :on 850201,negative Flux Rate Setpoint Outside Design Analyses Assumptions.Caused by Inconsistent Interpretations of Setpoint.Bistable Setpoint Reduced to 2.5% Rated Thermal Power |
- on 850201,negative Flux Rate Setpoint Outside Design Analyses Assumptions.Caused by Inconsistent Interpretations of Setpoint.Bistable Setpoint Reduced to 2.5% Rated Thermal Power
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000413/LER-1985-011, :on 850207,safety Injection Trains a & B Inoperable.Caused by Personnel Error.Pump 1B Returned to Svc & Operator Update Issued Addressing Impact of Solid State Protection Sys Inoperability |
- on 850207,safety Injection Trains a & B Inoperable.Caused by Personnel Error.Pump 1B Returned to Svc & Operator Update Issued Addressing Impact of Solid State Protection Sys Inoperability
| | | 05000413/LER-1985-012, :on 850209,low Steam Line Pressure Signal Caused Safety Injection & Reactor Trip.Caused by Loss of Voltage on Power Panelboard of Vital Instrumentation & Control Power Sys.Emergency Procedures Used |
- on 850209,low Steam Line Pressure Signal Caused Safety Injection & Reactor Trip.Caused by Loss of Voltage on Power Panelboard of Vital Instrumentation & Control Power Sys.Emergency Procedures Used
| | | 05000413/LER-1985-013, :on 850220,discovered Conduits Penetrating Fire Barriers W/O Ends Sealed for Fire Protection.Caused by Personnel Error & Procedure Deficiency.Training Provided to Personnel & Procedures Revised |
- on 850220,discovered Conduits Penetrating Fire Barriers W/O Ends Sealed for Fire Protection.Caused by Personnel Error & Procedure Deficiency.Training Provided to Personnel & Procedures Revised
| | | 05000413/LER-1985-014, :on 850222,stainless Steel Valves Discovered Installed W/Carbon Steel Filler Matl.Caused by Const Isometrics Incorrectly Specifying Matls Which Led to Use of Incorrect Welding Procedure |
- on 850222,stainless Steel Valves Discovered Installed W/Carbon Steel Filler Matl.Caused by Const Isometrics Incorrectly Specifying Matls Which Led to Use of Incorrect Welding Procedure
| | | 05000413/LER-1985-015, :on 850302,breakers Not Locked in Off Position on Certain Safety Injection & Auxiliary Feedwater Pump Motors.Caused by Administrative Deficiency & Personnel Error.Procedure Revised |
- on 850302,breakers Not Locked in Off Position on Certain Safety Injection & Auxiliary Feedwater Pump Motors.Caused by Administrative Deficiency & Personnel Error.Procedure Revised
| | | 05000413/LER-1985-016, :on 850302,while in Mode 1 at 30% Power,Three Power Range High Overpower Trip Circuits Calibr to 109% Power.Caused by Personnel Error.Circuits Recalibr |
- on 850302,while in Mode 1 at 30% Power,Three Power Range High Overpower Trip Circuits Calibr to 109% Power.Caused by Personnel Error.Circuits Recalibr
| | | 05000413/LER-1985-017, :on 850306,turbine Driven Auxiliary Feedwater Pump Automatically Started Due to Wide Range Level Instrumentation Sensing lo-lo Levels in Steam Generators. Caused by Design Deficiency |
- on 850306,turbine Driven Auxiliary Feedwater Pump Automatically Started Due to Wide Range Level Instrumentation Sensing lo-lo Levels in Steam Generators. Caused by Design Deficiency
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000413/LER-1985-018, :on 850307,Train a Diesel Generator & Turbine Driven Auxiliary Feedwater Pump Concurrently Inoperable. Caused by Personnel Error Placing Batteries on Equalize Charge.Batteries Returned to Svc |
- on 850307,Train a Diesel Generator & Turbine Driven Auxiliary Feedwater Pump Concurrently Inoperable. Caused by Personnel Error Placing Batteries on Equalize Charge.Batteries Returned to Svc
| 10 CFR 50.73(a)(2)(1) | | 05000413/LER-1985-019, :on 850307,during Performance of Analog Channel Operational Test,Steam Generator C Level Channel 4 Found Inoperable.Caused by Personnel Error.Circuit Card Replaced |
- on 850307,during Performance of Analog Channel Operational Test,Steam Generator C Level Channel 4 Found Inoperable.Caused by Personnel Error.Circuit Card Replaced
| | | 05000413/LER-1985-020, :on 850314,reactor Trip Occurred Due to Power Range High Flux Rate Signal.Caused by Loose Detector Cable Inside Power Range Cabinets.Work Request Initiated to Repair Loose Cable |
- on 850314,reactor Trip Occurred Due to Power Range High Flux Rate Signal.Caused by Loose Detector Cable Inside Power Range Cabinets.Work Request Initiated to Repair Loose Cable
| | | 05000413/LER-1985-021, :on 850313,during Performance of Turbine Driven Auxiliary Feedwater Pump Operability Test,Discovered CA Pump 1 Had Failed 850309 Operability Test.Caused by Personnel Error.Test Completed |
- on 850313,during Performance of Turbine Driven Auxiliary Feedwater Pump Operability Test,Discovered CA Pump 1 Had Failed 850309 Operability Test.Caused by Personnel Error.Test Completed
| | | 05000413/LER-1985-022, :on 850314,diesel Generator 1B Inoperable Due to Loss of Dc Control Power.Caused by Component Malfunction, Procedural Deficiency & Personnel Error.Control Power on Socket Repaired & Light Bulb Replaced |
- on 850314,diesel Generator 1B Inoperable Due to Loss of Dc Control Power.Caused by Component Malfunction, Procedural Deficiency & Personnel Error.Control Power on Socket Repaired & Light Bulb Replaced
| | | 05000413/LER-1985-023, :on 850329,reactor Power Exceeded 75% W/Only Two of Three Test Runs for Reactor Coolant Sys Performed. Caused by Software Problem.Thermal Output Calculations Program Modified,Reassembled & Reimplemented |
- on 850329,reactor Power Exceeded 75% W/Only Two of Three Test Runs for Reactor Coolant Sys Performed. Caused by Software Problem.Thermal Output Calculations Program Modified,Reassembled & Reimplemented
| 10 CFR 50.73(a)(2)(1) | | 05000413/LER-1985-024, :on 850409,Train B of Ventilation/Chilled Water Sys Became Inoperable Due to Failure of Filter Unit Preheater to Energize.On 850412,both Trains of Same Sys Inoperable for Several Hours |
- on 850409,Train B of Ventilation/Chilled Water Sys Became Inoperable Due to Failure of Filter Unit Preheater to Energize.On 850412,both Trains of Same Sys Inoperable for Several Hours
| | | 05000413/LER-1985-025, :on 850415,reactor Trip Occurred Due to lo-lo Level Signal from Steam Generator A.Caused by Administrative Error.Procedure Change Made to Require Notification of Flow Mismatches |
- on 850415,reactor Trip Occurred Due to lo-lo Level Signal from Steam Generator A.Caused by Administrative Error.Procedure Change Made to Require Notification of Flow Mismatches
| | | 05000413/LER-1985-026, :on 850422,during Testing of Nuclear Svc Water Flow Balance,Sys Aligned to Standby Nuclear Svc Water Pond on Pumphouse Pit B l0-l0 Level.Caused by Low Setting of Torque Switch for Valve 1RN4B |
- on 850422,during Testing of Nuclear Svc Water Flow Balance,Sys Aligned to Standby Nuclear Svc Water Pond on Pumphouse Pit B l0-l0 Level.Caused by Low Setting of Torque Switch for Valve 1RN4B
| | | 05000413/LER-1985-027, :on 850428,diesel Generator 1B Started on Blackout Signal.Caused by Short Circuit in Indicating Light Socket.Switchgears Closed |
- on 850428,diesel Generator 1B Started on Blackout Signal.Caused by Short Circuit in Indicating Light Socket.Switchgears Closed
| | | 05000413/LER-1985-028, :on 850422,both RHR Trains Inoperable & RCS Draining Began While Train a Inoperable Due to Maint.Caused by Personnel Error.Centrifugal Charging Pump a Started to Restore PCS Sys Level |
- on 850422,both RHR Trains Inoperable & RCS Draining Began While Train a Inoperable Due to Maint.Caused by Personnel Error.Centrifugal Charging Pump a Started to Restore PCS Sys Level
| | | 05000413/LER-1985-029, :on 850423,determined That End Stringer Clearance in Vital Instrumentation & Control Power Sys Exceeded Limits.Caused by Incorrect Mfg Installation Drawings.Styrofoam Spacers Installed |
- on 850423,determined That End Stringer Clearance in Vital Instrumentation & Control Power Sys Exceeded Limits.Caused by Incorrect Mfg Installation Drawings.Styrofoam Spacers Installed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000413/LER-1985-030, :on 850509,nuclear Svc Water Sys Automatically Aligned to Standby Nuclear Svc Water Pond & All Idle Sys Pumps Started Due to False lo-lo Level Signal in Sys Pumphouse Pit B.Caused by Loss of Voltage |
- on 850509,nuclear Svc Water Sys Automatically Aligned to Standby Nuclear Svc Water Pond & All Idle Sys Pumps Started Due to False lo-lo Level Signal in Sys Pumphouse Pit B.Caused by Loss of Voltage
| | | 05000413/LER-1985-031, :on 850511,nuclear Svc Water Sys Automatically Swapped to Standby Nuclear Svc Water Pond & All Idle Pumps Started.Caused by False lo-lo Level Signals in Pumphouse Pit B.Affected Valves Realigned |
- on 850511,nuclear Svc Water Sys Automatically Swapped to Standby Nuclear Svc Water Pond & All Idle Pumps Started.Caused by False lo-lo Level Signals in Pumphouse Pit B.Affected Valves Realigned
| | | 05000413/LER-1985-032, :on 850512,nuclear Svc Water Sys (Rn) Automatically Swapped to Standby Nuclear Svc Water Pond & Idle Rn Pumps Started Due to False lo-lo Level Signal in Rn Pumphouse Pit B.Caused by Personnel Error |
- on 850512,nuclear Svc Water Sys (Rn) Automatically Swapped to Standby Nuclear Svc Water Pond & Idle Rn Pumps Started Due to False lo-lo Level Signal in Rn Pumphouse Pit B.Caused by Personnel Error
| | | 05000413/LER-1985-033, :on 850513 & 14,steam Generator hi-hi & lo-lo Signals initiated,respectively.Hi-hi Signal Caused by Personnel Error.Cause of lo-lo Signal Unknown.Cf Isolation Signal Reset & lo-lo Signal Cleared |
- on 850513 & 14,steam Generator hi-hi & lo-lo Signals initiated,respectively.Hi-hi Signal Caused by Personnel Error.Cause of lo-lo Signal Unknown.Cf Isolation Signal Reset & lo-lo Signal Cleared
| | | 05000413/LER-1985-034, :on 850515,diesel Generators 1A & 1B Experienced Invalid Automatic Start Following Detection of Undervoltage Condition on Essential Switchgear.Caused by Transmission Sys Disturbance |
- on 850515,diesel Generators 1A & 1B Experienced Invalid Automatic Start Following Detection of Undervoltage Condition on Essential Switchgear.Caused by Transmission Sys Disturbance
| | | 05000413/LER-1985-035, :on 850528,motor Driven Auxiliary Feedwater CA Pumps Automatically Started Due to Low Suction Flow Trip of Both Main Feedwater CF Pumps.Caused by Personnel Error.Cf Pump Reset & Motor Driven CA Pumps Secured |
- on 850528,motor Driven Auxiliary Feedwater CA Pumps Automatically Started Due to Low Suction Flow Trip of Both Main Feedwater CF Pumps.Caused by Personnel Error.Cf Pump Reset & Motor Driven CA Pumps Secured
| | | 05000413/LER-1985-036, :on 850510,level Instrumentation for Upper Head Injection Sys Water Accumulator Tank Calibr Incorrectly. Caused by Procedural Deficiency.Instruments Recalibr to Correct Setpoint |
- on 850510,level Instrumentation for Upper Head Injection Sys Water Accumulator Tank Calibr Incorrectly. Caused by Procedural Deficiency.Instruments Recalibr to Correct Setpoint
| | | 05000413/LER-1985-037, :on 850529,auxiliary Feedwater (CA) Pump 1A Inadvertently Started During Periodic Test.Caused by Procedural Deficiency.Ca Pump 1A Secured.Procedure Changes Made |
- on 850529,auxiliary Feedwater (CA) Pump 1A Inadvertently Started During Periodic Test.Caused by Procedural Deficiency.Ca Pump 1A Secured.Procedure Changes Made
| | | 05000413/LER-1985-038, :on 850110,valve Stroke Time Test Not Performed After Steam Leak Repair.Caused by Personnel Error.Stroke Time Test Performed & Personnel Retrained |
- on 850110,valve Stroke Time Test Not Performed After Steam Leak Repair.Caused by Personnel Error.Stroke Time Test Performed & Personnel Retrained
| | | 05000413/LER-1985-039, :on 850523,spacers Required for Seismic Qualification of Channel 2 Vital Battery Bank 1EBB Not Reinstalled After Cells of Bank Replaced.Caused by Personnel Error.Spacers Replaced |
- on 850523,spacers Required for Seismic Qualification of Channel 2 Vital Battery Bank 1EBB Not Reinstalled After Cells of Bank Replaced.Caused by Personnel Error.Spacers Replaced
| | | 05000413/LER-1985-040, :on 850605,operability of Remaining Alternate Power Sources Not Demonstrated within 1 H of Declaring Diesel Generator 1A Inoperable.Caused by Personnel Error. Incident Discussed W/Personnel |
- on 850605,operability of Remaining Alternate Power Sources Not Demonstrated within 1 H of Declaring Diesel Generator 1A Inoperable.Caused by Personnel Error. Incident Discussed W/Personnel
| | | 05000413/LER-1985-041, :on 850613,main Feedwater Pump Trip Resulted in Manual Reactor Trip.Caused by Pump Recirculation Valve Not Capable of Modulating Quickly During Flow Reduction.Design Deficiency Corrected |
- on 850613,main Feedwater Pump Trip Resulted in Manual Reactor Trip.Caused by Pump Recirculation Valve Not Capable of Modulating Quickly During Flow Reduction.Design Deficiency Corrected
| | | 05000413/LER-1985-042, :on 850616,during Mode 1,nuclear Instrumentation High Flux Rate Power Range Reactor Trip Occurred.Cause Undetermined.Power Range Channels Reset. Equipment Realigned |
- on 850616,during Mode 1,nuclear Instrumentation High Flux Rate Power Range Reactor Trip Occurred.Cause Undetermined.Power Range Channels Reset. Equipment Realigned
| | | 05000413/LER-1985-043, :on 850622,manual Reactor Shutdown Initiated Following Automatic Trip of Main Feedwater Pump Turbine 1B Due to Loss of Condenser Vacuum.Caused by Personnel Error. Incident Discussed W/Personnel |
- on 850622,manual Reactor Shutdown Initiated Following Automatic Trip of Main Feedwater Pump Turbine 1B Due to Loss of Condenser Vacuum.Caused by Personnel Error. Incident Discussed W/Personnel
| | | 05000413/LER-1985-044, :on 850622,steam Generator lo-lo Level Reactor Trip Occurred.Caused by Main Feedwater Pump Turbine Speed Increasing W/O Proper Mode Due to Miscommunication.Sys Affected Returned to Normal Alignment |
- on 850622,steam Generator lo-lo Level Reactor Trip Occurred.Caused by Main Feedwater Pump Turbine Speed Increasing W/O Proper Mode Due to Miscommunication.Sys Affected Returned to Normal Alignment
| | | 05000413/LER-1985-045, :on 850710,reactor Trip Occurred on lo-lo Steam Generator Level.Incorrect Main Steam Pressure Transmitter Isolated During Surveillance Calibrs.Caused by Personnel Error |
- on 850710,reactor Trip Occurred on lo-lo Steam Generator Level.Incorrect Main Steam Pressure Transmitter Isolated During Surveillance Calibrs.Caused by Personnel Error
| | | 05000413/LER-1985-045-01, :on 850710,during 18-month Surveillance Calibrs,Reactor Trip Occurred on lo-lo Steam Generator. Caused by Personnel Error.Technician in Field Will Be Provided Documentation |
- on 850710,during 18-month Surveillance Calibrs,Reactor Trip Occurred on lo-lo Steam Generator. Caused by Personnel Error.Technician in Field Will Be Provided Documentation
| | | 05000413/LER-1985-046, :on 850723,fire Barrier Penetration C-AX-228-W-9 Determined Inoperable.Caused by Unsealed Installation of Two Temporary Cables Penetrating Fire Barriers.Cables Removed & Barrier Resealed |
- on 850723,fire Barrier Penetration C-AX-228-W-9 Determined Inoperable.Caused by Unsealed Installation of Two Temporary Cables Penetrating Fire Barriers.Cables Removed & Barrier Resealed
| | | 05000413/LER-1985-047, :on 850729,response Time Testing for Auxiliary Feedwater (CA) Transfer of Suction Source to Nuclear Svc Water Improperly Performed.Caused by Procedural Deficiency. Procedural Changes Effected |
- on 850729,response Time Testing for Auxiliary Feedwater (CA) Transfer of Suction Source to Nuclear Svc Water Improperly Performed.Caused by Procedural Deficiency. Procedural Changes Effected
| | | 05000413/LER-1985-048, :on 850729,actuation of Control Room Ventilation Sys Train B Occurred.Caused by Personnel Error. Control Room Filter Fan Shut Down & Pressure Stabilized. Undervoltage Relays & Sequencer Retested |
- on 850729,actuation of Control Room Ventilation Sys Train B Occurred.Caused by Personnel Error. Control Room Filter Fan Shut Down & Pressure Stabilized. Undervoltage Relays & Sequencer Retested
| | | 05000413/LER-1985-049-01, :on 850807,inadvertent Isolation of Both Discharge Headers of Fire Protection (Ry) Pumps Occurred. Caused by Personnel Error.Correct Ry Header Isolated. Procedure 2-18 Revised |
- on 850807,inadvertent Isolation of Both Discharge Headers of Fire Protection (Ry) Pumps Occurred. Caused by Personnel Error.Correct Ry Header Isolated. Procedure 2-18 Revised
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