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| 05000409/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-001/01T-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-001-01, /01T-0:on 820108,during Annual Test,Reactor Bldg Spray Valve Could Not Be Opened Using Manual Handwheel in Control Room.Caused by Separation of Coupling Between Valve & Shaft.Coupling Reconnected | /01T-0:on 820108,during Annual Test,Reactor Bldg Spray Valve Could Not Be Opened Using Manual Handwheel in Control Room.Caused by Separation of Coupling Between Valve & Shaft.Coupling Reconnected | |
| 05000409/LER-1982-002-03, /03L-0:on 820121,containment Bldg Fire Detection Zone 19 Placed in Bypass.Caused by Spurious Alarm Annunciation Due to Faulty Detector Head Over Msiv.Head Cleaned | /03L-0:on 820121,containment Bldg Fire Detection Zone 19 Placed in Bypass.Caused by Spurious Alarm Annunciation Due to Faulty Detector Head Over Msiv.Head Cleaned | |
| 05000409/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-003-03, /03L-0:on 820313,during Type B Leakage Test on Personnel Airlock,Manometer Read Incorrectly.Caused by Inadequate Tightening of Strongbacks on Inner Door.Need for Tight Installation Emphasized & Procedure Revised | /03L-0:on 820313,during Type B Leakage Test on Personnel Airlock,Manometer Read Incorrectly.Caused by Inadequate Tightening of Strongbacks on Inner Door.Need for Tight Installation Emphasized & Procedure Revised | |
| 05000409/LER-1982-004-03, /03L-0:on 820329,emergency Svc Water Supply Sys Suction Hoses Leaked During First Positive Pressure Hydrostatic Surveillance Test.Caused by Flat Spot in Hose Fitting Castings.Spot Filed & Hose Reclamped | /03L-0:on 820329,emergency Svc Water Supply Sys Suction Hoses Leaked During First Positive Pressure Hydrostatic Surveillance Test.Caused by Flat Spot in Hose Fitting Castings.Spot Filed & Hose Reclamped | |
| 05000409/LER-1982-004, Forwards LER 82-004/03L-0 & Updated LER 81-015/01X-1. Detailed Event Analysis Submitted | Forwards LER 82-004/03L-0 & Updated LER 81-015/01X-1. Detailed Event Analysis Submitted | |
| 05000409/LER-1982-005, Forwards LER 82-005/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-005/01T-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-005-01, /01T-0:on 820413,discrepancy Discovered in Seismic & Stress Analysis of HPCS Discharge Piping.Caused by Analytical Models Being Based on Piping Matls & Configuration for Const Under Allis-Chalmers Contract | /01T-0:on 820413,discrepancy Discovered in Seismic & Stress Analysis of HPCS Discharge Piping.Caused by Analytical Models Being Based on Piping Matls & Configuration for Const Under Allis-Chalmers Contract | |
| 05000409/LER-1982-006, Forwards LER 82-006/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-006/01T-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-006-01, /01T-0:on 820420,during Reactor Refueling,Insp Revealed Degraded Segment on Fuel Assembly 1-8.Caused by Pellet/Clad Interaction W/Oxygen Resulting in Cracking. Allis-Chalmers Assembly Replaced W/Exxon Assembly | /01T-0:on 820420,during Reactor Refueling,Insp Revealed Degraded Segment on Fuel Assembly 1-8.Caused by Pellet/Clad Interaction W/Oxygen Resulting in Cracking. Allis-Chalmers Assembly Replaced W/Exxon Assembly | |
| 05000409/LER-1982-007-03, /03L-0:on 820515,during Refueling Outage,Buses 1A & 1B Were Supplied by 1A & 1B Emergency Diesel Generators for 12 Minutes.Caused by Undervoltage Relay Breaker Opened During Troubleshooting of Dc Ground | /03L-0:on 820515,during Refueling Outage,Buses 1A & 1B Were Supplied by 1A & 1B Emergency Diesel Generators for 12 Minutes.Caused by Undervoltage Relay Breaker Opened During Troubleshooting of Dc Ground | |
| 05000409/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-008-03, /03L-0:on 820517,high Pressure Svc Water Diesel Pump 1A Failed to Start.Caused by Chewed Gear in Starter Motor.Gear & Starter Motor Replaced | /03L-0:on 820517,high Pressure Svc Water Diesel Pump 1A Failed to Start.Caused by Chewed Gear in Starter Motor.Gear & Starter Motor Replaced | |
| 05000409/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-009-01, /01T-0:on 820520,while Performing Type C Leak Tests on Retention Tank Pump Discharge Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated. Valve Relapped & Restroked | /01T-0:on 820520,while Performing Type C Leak Tests on Retention Tank Pump Discharge Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated. Valve Relapped & Restroked | |
| 05000409/LER-1982-010-01, /01T-0:on 820521,while Performing Type C Leak Tests on Containment Bldg Heating Steam Condensate Return Isolation Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated.Valve Internals Replaced | /01T-0:on 820521,while Performing Type C Leak Tests on Containment Bldg Heating Steam Condensate Return Isolation Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated.Valve Internals Replaced | |
| 05000409/LER-1982-011-01, /01T-0:on 820523,while Performing Leak Tests on High Pressure Svc Water Containment Isolation Valve & Electrical Penetration Unit 5,leak Flow Rate Found Exceeding Tech Spec Limit.Caused by Hardening of Epoxy Sealant | /01T-0:on 820523,while Performing Leak Tests on High Pressure Svc Water Containment Isolation Valve & Electrical Penetration Unit 5,leak Flow Rate Found Exceeding Tech Spec Limit.Caused by Hardening of Epoxy Sealant | |
| 05000409/LER-1982-012-03, /03L-0:on 820526,during Refueling Outage, Containment Bldg Fire Suppression Header Removed from Svc to Repair High Pressure Svc Water Containment Isolation Valve.Header Returned to Svc Upon Completion of Repairs | /03L-0:on 820526,during Refueling Outage, Containment Bldg Fire Suppression Header Removed from Svc to Repair High Pressure Svc Water Containment Isolation Valve.Header Returned to Svc Upon Completion of Repairs | |
| 05000409/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-013-03, /03L-0:on 820603,during Cold Shutdown,Reactor Coolant Conductivity & Chloride Concentration Exceeded Tech Specs.Caused by Stagnant River Water Entering Reactor Vessel During Surveillance Test.Test Will Be Eliminated | /03L-0:on 820603,during Cold Shutdown,Reactor Coolant Conductivity & Chloride Concentration Exceeded Tech Specs.Caused by Stagnant River Water Entering Reactor Vessel During Surveillance Test.Test Will Be Eliminated | |
| 05000409/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-014, Forwards LER 82-014/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-014/01T-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-014-01, /01T-0:on 820605,gross Alpha Activity Exceeded Tech Spec Limitation During Startup from Refueling Outage. Caused by Degraded Fuel Cladding Experience Contributing to Irradiated Fuel Particles in RCS | /01T-0:on 820605,gross Alpha Activity Exceeded Tech Spec Limitation During Startup from Refueling Outage. Caused by Degraded Fuel Cladding Experience Contributing to Irradiated Fuel Particles in RCS | |
| 05000409/LER-1982-015-01, /01T-0:on 820616,both HPCS Pumps Placed in Pullout & LPCS Valve Control Switch Turned to Close to Prevent Challenging of Eccs.Caused by Shift Supervisor Not Cognizant of Work Scope Involved W/Change | /01T-0:on 820616,both HPCS Pumps Placed in Pullout & LPCS Valve Control Switch Turned to Close to Prevent Challenging of Eccs.Caused by Shift Supervisor Not Cognizant of Work Scope Involved W/Change | |
| 05000409/LER-1982-015, Forwards LER 82-015/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-015/01T-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-016-03, /03L-0:on 820702,during Refueling Outage 1,200 Gallons of Water Leaked from Condensate Demineralizer Sys. Caused by Resin Addition Not Closing When Turned to Close. Valve Control Relay Replaced | /03L-0:on 820702,during Refueling Outage 1,200 Gallons of Water Leaked from Condensate Demineralizer Sys. Caused by Resin Addition Not Closing When Turned to Close. Valve Control Relay Replaced | |
| 05000409/LER-1982-016, Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | |
| 05000409/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | |
| 05000409/LER-1982-019-03, /03L-0:on 820927,during Power Escalation Following Refueling Outage,Water Level Safety Channel 3 Determined Nonconservative W/Respect to Possible Low Water Level Condition.Caused by Transmitter Drift.Channel Adjusted | /03L-0:on 820927,during Power Escalation Following Refueling Outage,Water Level Safety Channel 3 Determined Nonconservative W/Respect to Possible Low Water Level Condition.Caused by Transmitter Drift.Channel Adjusted | |
| 05000409/LER-1982-020, Updated LER 82-020/03X-1:on 821119-20,on Three Occasions Vacuum Pump Which Maintains Isokinetic Flow Rate to Stack Activity Monitors Tripped.Caused by Pump & Motor Overheating.Motor Thermal Overload Fuses Upgraded | Updated LER 82-020/03X-1:on 821119-20,on Three Occasions Vacuum Pump Which Maintains Isokinetic Flow Rate to Stack Activity Monitors Tripped.Caused by Pump & Motor Overheating.Motor Thermal Overload Fuses Upgraded | |