LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 4091982003R00 - NRC Website |
|
text
I
~
9 D
DA/RYLAND
~
h [k
COOPERAT/VE e.O box 8i7 2615 EAST AV SOUTH
- LA CROSSE. WISCONSIN 54601 (608) 788-4000 March 23, 1982 In reply, please refer to LAC-8167 DOCKET N0. 50-409 Mr. James G. Keppler, Regional Director U. S. Nuclear Regulatory Commission Directorate of Regulatory Operations Region III 799 Roosevelt Road Glen Ellyn, Illinois 60137
SUBJECT:
DAIRYLAND POWER COOPERATIVE LA CROSSE BOILING WATER REACTOR (LACBWR)
PROVISIONAL OPERATING LICENSE NO. DPR-45
?J '. c'!,g
~'
REPORTABLE OCCURRENCE NO. 82-03
,. *2
'g
.y
REFERENCES:
(1) LACBWR Technical Specifications,
!Y
'P l Jg Sections 6.9.1.9.b and c (2) LACBWR Technical Specifications, ng Section 5.2.1.2
" Q oma 77 (3) LACBWR Technical Specifications, yq Section 3.0.3 N' Q, / -
p
Dear Mr. Keppler:
In accordance with Reference 1, this report is notification of observed inadequacies in the implementation of a procedure which led to commencement of a plant shutdown required by a limiting condition for operation.
On March 12-13, 1982, a Type B leakage test of the personnel air lock was conducted. The test method used involves placing an airtight reference chamber inside the airlock. Both the reference chamber and the air space between the inner and outer personnel air lock doors are pressurized to at least 52 psig. The difference in pressure between the reference chamber and the airlock is measured with a manometer. Any change in dif ferential pressure is assumed to be due to leakage from the airlock. The acceptance criteria is 3.75 SCFH.*
On March 13, the leakage rate was calculated to be 3.23 SCFH, which is within the acceptance. criteria. A small amount of leakage was found using the soap bubble techniqu'e on the inner door gasket. No leakage was detected through the outer door. The test was detennined satisfactory.
- Shall not exceed 10% of leakage rate Lpo, where Lpo is 37.5 SCFH (Reference 2).
WP-6 -
0204020472 820323
@R 2 9 g82
[
PDR ADDCK 05000409
/
,S PDR
i i
3 Mr. James G. Keppler, Regional Director March 23, 1982 U. S. Nuclear Regulatory Commission LAC-8167 At 0750 on March 14, it was determined that the auxiliary operator hoc not l
read the manameter correctly when conducting the Type B test on the personnel ai rl ock. Also, the operators who removed the strongbacks, which are installed
{
on the inner airlock door for the test, found them to be not as secure as noma 1 The strongbacks are needed because the force on the inner door during the Type B test is from the opposite direction than would be the case in a containment pressurization accident. A reactor shutdown commenced in l
accordance with Reference 3.
f The Mechanical Maintenance Supervisor and the Operations Supervisor were I
called in to supervise their departments in conducting a retest.
A successful retest was concluded at 2000 on March 14. The calculated leakage rate was i
1.503 SCFH, which is within the acceptance criteria of Reference 2.
The l
lowest reactor power reached was 40% Rated Thermal Power (18 MWe-Net).
[
The Type B test procedure for the personnel airlock will be modified to include instructions for reading the manometer.
The importance of secure instrllation of the strongbacks has been emphasized to the Maintenance Department.
The Nuclear Regulatory Commission Resident Inspector for LACBWR, M. Branch, was notified of the event at approximately 0830 on March 14, 1982. The NRC Operations Center was notified at 0850 on March 14, 1982.
A Licensee Event Report (Reference: Appendix A, Regulatory Guide 1.16, Revision 4) is enclosed.
If there are questions concerning this report, please contact us.
Very truly yours, l
DAIRYLAND POWER COOPERATIVE WENS AVFrank Linder, General Manager P
FL:LSG:eme Enclosures cc:
Director, Office of Inspection and Enforcement (30)
U. S. Nuclear Regulatory Commission Washington, D. C.
20555 Director, Office of Management Infomation (3) and Program Control U. S. Nuclear Regulatory Commission Washington, D. C.
20555 NRC Resident Inspector INPO 4
WP-6
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000409/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-001/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-001-01, /01T-0:on 820108,during Annual Test,Reactor Bldg Spray Valve Could Not Be Opened Using Manual Handwheel in Control Room.Caused by Separation of Coupling Between Valve & Shaft.Coupling Reconnected | /01T-0:on 820108,during Annual Test,Reactor Bldg Spray Valve Could Not Be Opened Using Manual Handwheel in Control Room.Caused by Separation of Coupling Between Valve & Shaft.Coupling Reconnected | | | 05000409/LER-1982-002-03, /03L-0:on 820121,containment Bldg Fire Detection Zone 19 Placed in Bypass.Caused by Spurious Alarm Annunciation Due to Faulty Detector Head Over Msiv.Head Cleaned | /03L-0:on 820121,containment Bldg Fire Detection Zone 19 Placed in Bypass.Caused by Spurious Alarm Annunciation Due to Faulty Detector Head Over Msiv.Head Cleaned | | | 05000409/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-003-03, /03L-0:on 820313,during Type B Leakage Test on Personnel Airlock,Manometer Read Incorrectly.Caused by Inadequate Tightening of Strongbacks on Inner Door.Need for Tight Installation Emphasized & Procedure Revised | /03L-0:on 820313,during Type B Leakage Test on Personnel Airlock,Manometer Read Incorrectly.Caused by Inadequate Tightening of Strongbacks on Inner Door.Need for Tight Installation Emphasized & Procedure Revised | | | 05000409/LER-1982-004-03, /03L-0:on 820329,emergency Svc Water Supply Sys Suction Hoses Leaked During First Positive Pressure Hydrostatic Surveillance Test.Caused by Flat Spot in Hose Fitting Castings.Spot Filed & Hose Reclamped | /03L-0:on 820329,emergency Svc Water Supply Sys Suction Hoses Leaked During First Positive Pressure Hydrostatic Surveillance Test.Caused by Flat Spot in Hose Fitting Castings.Spot Filed & Hose Reclamped | | | 05000409/LER-1982-004, Forwards LER 82-004/03L-0 & Updated LER 81-015/01X-1. Detailed Event Analysis Submitted | Forwards LER 82-004/03L-0 & Updated LER 81-015/01X-1. Detailed Event Analysis Submitted | | | 05000409/LER-1982-005, Forwards LER 82-005/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-005/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-005-01, /01T-0:on 820413,discrepancy Discovered in Seismic & Stress Analysis of HPCS Discharge Piping.Caused by Analytical Models Being Based on Piping Matls & Configuration for Const Under Allis-Chalmers Contract | /01T-0:on 820413,discrepancy Discovered in Seismic & Stress Analysis of HPCS Discharge Piping.Caused by Analytical Models Being Based on Piping Matls & Configuration for Const Under Allis-Chalmers Contract | | | 05000409/LER-1982-006, Forwards LER 82-006/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-006/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-006-01, /01T-0:on 820420,during Reactor Refueling,Insp Revealed Degraded Segment on Fuel Assembly 1-8.Caused by Pellet/Clad Interaction W/Oxygen Resulting in Cracking. Allis-Chalmers Assembly Replaced W/Exxon Assembly | /01T-0:on 820420,during Reactor Refueling,Insp Revealed Degraded Segment on Fuel Assembly 1-8.Caused by Pellet/Clad Interaction W/Oxygen Resulting in Cracking. Allis-Chalmers Assembly Replaced W/Exxon Assembly | | | 05000409/LER-1982-007-03, /03L-0:on 820515,during Refueling Outage,Buses 1A & 1B Were Supplied by 1A & 1B Emergency Diesel Generators for 12 Minutes.Caused by Undervoltage Relay Breaker Opened During Troubleshooting of Dc Ground | /03L-0:on 820515,during Refueling Outage,Buses 1A & 1B Were Supplied by 1A & 1B Emergency Diesel Generators for 12 Minutes.Caused by Undervoltage Relay Breaker Opened During Troubleshooting of Dc Ground | | | 05000409/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-008-03, /03L-0:on 820517,high Pressure Svc Water Diesel Pump 1A Failed to Start.Caused by Chewed Gear in Starter Motor.Gear & Starter Motor Replaced | /03L-0:on 820517,high Pressure Svc Water Diesel Pump 1A Failed to Start.Caused by Chewed Gear in Starter Motor.Gear & Starter Motor Replaced | | | 05000409/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-009-01, /01T-0:on 820520,while Performing Type C Leak Tests on Retention Tank Pump Discharge Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated. Valve Relapped & Restroked | /01T-0:on 820520,while Performing Type C Leak Tests on Retention Tank Pump Discharge Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated. Valve Relapped & Restroked | | | 05000409/LER-1982-010-01, /01T-0:on 820521,while Performing Type C Leak Tests on Containment Bldg Heating Steam Condensate Return Isolation Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated.Valve Internals Replaced | /01T-0:on 820521,while Performing Type C Leak Tests on Containment Bldg Heating Steam Condensate Return Isolation Valve,Leakage Flow Rate Found Exceeding Tech Spec Limit.Cause Not Stated.Valve Internals Replaced | | | 05000409/LER-1982-011-01, /01T-0:on 820523,while Performing Leak Tests on High Pressure Svc Water Containment Isolation Valve & Electrical Penetration Unit 5,leak Flow Rate Found Exceeding Tech Spec Limit.Caused by Hardening of Epoxy Sealant | /01T-0:on 820523,while Performing Leak Tests on High Pressure Svc Water Containment Isolation Valve & Electrical Penetration Unit 5,leak Flow Rate Found Exceeding Tech Spec Limit.Caused by Hardening of Epoxy Sealant | | | 05000409/LER-1982-012-03, /03L-0:on 820526,during Refueling Outage, Containment Bldg Fire Suppression Header Removed from Svc to Repair High Pressure Svc Water Containment Isolation Valve.Header Returned to Svc Upon Completion of Repairs | /03L-0:on 820526,during Refueling Outage, Containment Bldg Fire Suppression Header Removed from Svc to Repair High Pressure Svc Water Containment Isolation Valve.Header Returned to Svc Upon Completion of Repairs | | | 05000409/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-013-03, /03L-0:on 820603,during Cold Shutdown,Reactor Coolant Conductivity & Chloride Concentration Exceeded Tech Specs.Caused by Stagnant River Water Entering Reactor Vessel During Surveillance Test.Test Will Be Eliminated | /03L-0:on 820603,during Cold Shutdown,Reactor Coolant Conductivity & Chloride Concentration Exceeded Tech Specs.Caused by Stagnant River Water Entering Reactor Vessel During Surveillance Test.Test Will Be Eliminated | | | 05000409/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-014, Forwards LER 82-014/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-014/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-014-01, /01T-0:on 820605,gross Alpha Activity Exceeded Tech Spec Limitation During Startup from Refueling Outage. Caused by Degraded Fuel Cladding Experience Contributing to Irradiated Fuel Particles in RCS | /01T-0:on 820605,gross Alpha Activity Exceeded Tech Spec Limitation During Startup from Refueling Outage. Caused by Degraded Fuel Cladding Experience Contributing to Irradiated Fuel Particles in RCS | | | 05000409/LER-1982-015-01, /01T-0:on 820616,both HPCS Pumps Placed in Pullout & LPCS Valve Control Switch Turned to Close to Prevent Challenging of Eccs.Caused by Shift Supervisor Not Cognizant of Work Scope Involved W/Change | /01T-0:on 820616,both HPCS Pumps Placed in Pullout & LPCS Valve Control Switch Turned to Close to Prevent Challenging of Eccs.Caused by Shift Supervisor Not Cognizant of Work Scope Involved W/Change | | | 05000409/LER-1982-015, Forwards LER 82-015/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-015/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-016-03, /03L-0:on 820702,during Refueling Outage 1,200 Gallons of Water Leaked from Condensate Demineralizer Sys. Caused by Resin Addition Not Closing When Turned to Close. Valve Control Relay Replaced | /03L-0:on 820702,during Refueling Outage 1,200 Gallons of Water Leaked from Condensate Demineralizer Sys. Caused by Resin Addition Not Closing When Turned to Close. Valve Control Relay Replaced | | | 05000409/LER-1982-016, Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | | | 05000409/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1982-019-03, /03L-0:on 820927,during Power Escalation Following Refueling Outage,Water Level Safety Channel 3 Determined Nonconservative W/Respect to Possible Low Water Level Condition.Caused by Transmitter Drift.Channel Adjusted | /03L-0:on 820927,during Power Escalation Following Refueling Outage,Water Level Safety Channel 3 Determined Nonconservative W/Respect to Possible Low Water Level Condition.Caused by Transmitter Drift.Channel Adjusted | | | 05000409/LER-1982-020, Updated LER 82-020/03X-1:on 821119-20,on Three Occasions Vacuum Pump Which Maintains Isokinetic Flow Rate to Stack Activity Monitors Tripped.Caused by Pump & Motor Overheating.Motor Thermal Overload Fuses Upgraded | Updated LER 82-020/03X-1:on 821119-20,on Three Occasions Vacuum Pump Which Maintains Isokinetic Flow Rate to Stack Activity Monitors Tripped.Caused by Pump & Motor Overheating.Motor Thermal Overload Fuses Upgraded | |
|