LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 4091981013R00 - NRC Website |
|
text
-
D DA/RYLAND k
COOPERA T/VE. e o so< ec w5 e AsT Av south. LA CROSSE W15 CON 5iN S4601 (608) 788 4 000 Decenber 10, 1981 In reply, please refer to LAC-7974 DOCKET NO. 50-409 Mr. James G. Keppler, Regional Director U. S. Nuclear Regulatory Commission Directorate of Regulatory Operations g p, n ;
2 @f Region III 799 Roosevelt Road W
M Glen Ellyn, Illinois60-137 J
3 j
OEC,gy blN [
I2' SUBJECT: DAIRYLAND POWER COOPERATIVE LA CROSSE BOILTNG WATER REACTOR (LACBWR)
, -i PROVISIONAL OPERATING LICENSE NO. DPR-45
%a
^# M
~
ca REPORTABLE OCCURJENCE NO. 81-13
,?/\\
1; O
REFERENCES:
(1) LAC 3WR Technical Speci fications M TT&T~\\ "
Section 6.9.1.9.b (2) LALRWR Technical Specifications, Section 4.2.3.2.1
Dear Mr. Keppler:
In accordance with Reference 1, this report is notification of operation in a degraded mode permitted by a limiting condition for operation.
Reference 2 requires that specified AC electrical buses be operable and energized from sources of power other than the diesel generators during Operating Conditions I and 2 and when the control power key switch is not off or shen all control rods are not fully inserted.
At 0831 on November 12, 1981, following a reactor scram, the 1A 2400 V Bus transferred automatically to the reserve transfonner properly, but the 2400 V Bus IB Reserve Feed Breaker 252 R1B did not automatically closu and connect the IB 2400 V Bus to the reserve transformer (see attached drawing). The IB Emergency Diesel Generator (EDG) started and suppliea power to the 18 480 V Essential Bus. The turbine operator flagged the control switch for Breaker 252 R1B to " trip" position and released it which resulted in the control switch contacts aligning in the "after trip" position. This latter position is necessary for automatic breaker closure. Breasc: 252 R1B then closed automatical ly.
The IB 480 V Bus Main Feed Breaker was closed at 0833, re-energizing the non-essential loads on the IB 480 V Bus. At 0855 the IB Essential Bus was returned to its normal feed The IB EDG was then secured.
Breaker 252 R1B was tested both locally and tron the Control Roon approximately ten times. The breaker operated properly every time. The control switch in the Control Room was inspected and no physical problems were observed.
It is thought the contacts may not have made up properly when the hbk
$0 0 00 s O(G 16 G81 h., y
/
d
O Mr. James G. Keppler, Regional Dire' 1r December 10, 1981 U. S. Nuclear Regulatory Commissia LAC-79 74 operator turned tha control
.h to trip af ter the 2400 V 1B Bus had been transferred to the unit auxi. iary transformer during the last plant startup on October 19, 1981. The operators are being reminded to operate all switches in a firm manner aN to maintain the switch in the tripped or closed position for 1 to 2 seconds before regasing it to the neutral position.
A Licensee Event Report (Reference: Appendix A, Regulatory Guide 1.16, Revision 4) is enclosed.
If you have any questions, please contact us.
Very truly yours, DAIRYLAND POWER COOPERATIVE
/
a
./ l 41ilhL.),
@(? rt Frank Linder, Jeaeral i'anager
)
FL :LSG:eme Enclosures cc: Director, Office of Inspectice and Enforcement (30)
U. S. Nuclear Regulatory Commission Washington, D. C.
20555 l
Director, Office of Management Information (3) and Program Control U. S. Nuclear Regulatory Commission Washington, D. C.
20555 NRC Resident Inspector J
7,;
r P-t
- i t
f rbli 1
[
I?
I
!i ' i
- i 8.
!g
?T:
1 go, 1 p' ijiit ;!,
il.
i ;
Ni a
O j '-'!
idilill-t I'3 li h
8 10 I
ifIdn,j i a l-E=-
[
rill--
5 i ll 11!;
4 n!p!
m 4-- 1g,:
i
- +
4 Ii i H..
sqt;.
u
- - we.--
i I
ja ;il 1*
a +-, =
1 p;t j!! I y;.as x_i
~ = = t n =,
4 1
+ :=
N,.
g y,
0 I;
i ii i !
+ r.a, t^-
- .r g
p g g y.
... !..i.. _.lil I li.ll.,_.z.-..
p..
r a
+ --. = =
hetaigj p--
yg ~, - (.
.w 4 w _i
%.o.I a-p
,.= l WWfSh w
~ _= ~ l ME.'2$.".!!l I
+ ~ = -
- c.
- . li p 11 lj jl ;
~ =! i ii=
m s
.w 3
+ =r1 (( i,Id
'" 3
^
I 11 lilli i !!I l i
i b 1Nb ' N E
.k
^
3 S
. -, d=4
.}.,}'} 4,',J', {
,A 4
i 1..
a J,. : - i'i, >i 3
o addsysM<eflyl es.w e >
w u~=
} --o-
,1 I(
'f g
il [I
.3 5,l.
l i
si 3 --o-g, I 8
E)
I 0,
t
,3 ll
~
.~ a:,
l.n M
.<0E i il3lIl i m
ro 3
3 e
o
'b M Ya l
- ,jiI
~
M e
I f. g cr n~,
i "+-O -.r::::
1.
ij 2
e
..e
(
Jh,, l!
N r
8 e
, ia 3
- e-.
=
jj, f, 3l N
1 e
~~-*-g' w w
^. > - -
+
s k-
.o.z.<!%:. I
- 1. )*
r r
g l.. Al-l E' " Mill 43.ll 45 I.
pc i
,i i
3
?w 3i t e
--*a *
- .ar l_JJ D '
i y i
d I e.~ eG4s D
{1, tr.
3 f516@'-d li
+ =s -
Ud+.b.a u
i
{
- - w ~~:
- - t
- - w.m!
u.
1,
. ; 10.,
ti s
g g]I
.2
! !}
i c+ -
l-IkM,ig ((!!d,i ~!!!, i
, ll[
Y t
y
,i s e a i
Ji 8k g-il
4c,,
. _d_ i l '; -}
l 5
i r
!.;+ -
i II A I
- i I.I
.t. _
8 e
4+ce:
t i
g"!glh i'
i 8
8 si l
"1s 8
1,
-.c+
~%s
I i
L 2
ode Og
~
'"~
I s i
- *4 2.'E
- - l',
!)
E
' ' 7. $
[
1 i
.. 3-I
'I.
i t;
6 :
'8 l 3' ll;=~
I a
g 2
e i
l!I lll l
8 3
.4, 57 O- - - I v F:
is!
l1 tf.d d: -
.[ >.J:.
a Ii
=
- f
.4
',e--
1
---<.c.
i
"; p-J
[
t ~,l-- J
]
3 zi ll 2
[
, g *5'i
+' w Ps s/I+' vel _
- # s e I49/9/ir pAos s 91 y "i
.O m.o m wa2 9 m,.s a m.o # it wy -w-r=
.oo i..a y p..!.
n m i I
i e
4
+
1 e
1 4
A
=
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000409/LER-1981-001, Forwards LER 81-001/02L-0 | Forwards LER 81-001/02L-0 | | | 05000409/LER-1981-001-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | | | 05000409/LER-1981-001-03, /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | | | 05000409/LER-1981-002, Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-002-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | | | 05000409/LER-1981-003-03, /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | | | 05000409/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | | | 05000409/LER-1981-004-03, /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | | | 05000409/LER-1981-006-01, /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followe | /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followed | | | 05000409/LER-1981-006, Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-007-01, /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | | | 05000409/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000409/LER-1981-008-01, /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | | | 05000409/LER-1981-008, Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-009-03, /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | | | 05000409/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010, Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010-01, /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | | | 05000409/LER-1981-011-03, /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | | | 05000409/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-012-03, /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | | | 05000409/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-013-03, Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | | | 05000409/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-014-03, /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | | | 05000409/LER-1981-014, Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | | | 05000409/LER-1981-015, Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-015-01, /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | |
|