LER-1981-015, Forwards LER 81-015/01T-0.Detailed Event Analysis Encl |
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D DA/RYLAND h
COOPERAT/VE eo sox 817 2615 EAST AV SOUTH LA CROSSE. WISCONSIN S4601 (608) 788-4000 January 6, 1982 In reply, please refer to LAC-8007 DOCKET e 50-409 Mr. James G. Keppler, Regional Director r, N A
U.
S. Nuclear Regulatory Commission V
Directorate of Regulatory Operations OECEjVgg B
Region III
- )
1 M 1319825 9 799 Roosevelt Road f %aa; mtrga Me Glen Ellyn, Illinois 60137 t
1 w
ppg
SUBJECT:
DAIRYLAND POWER COOPERATIVE 9r, b
LA CROSSE BOILING WATER REACTOR (LACBWR h
\\
~
dI PROVISIONAL OPERATING LICENSE NO. DPR-45 REPORTABLE OCCURRENCE NO. 81-15
References:
(1)
DPC Letter, LAC-7993, Lindar to Keppler, dated December 28, 1981.
(2)
LACBWR Technical Specifications, Section 4.2.2.4.a.
Dear Mr. Keppler:
This letter constitutes the written followup to the event reported to you in Reference 1.
Our letter discussed an occurrence on December 24, 1981, in which the temperature of the 1B Forced Circulation (FC) Loop decreased below 130 F, while primary pressure was greater than 280 psig.
Following a reactor scram, which occurred at 2115 December 23, 1981, the temperature of the piping in the 1B Forced Circulation (FC)
Loop decreased to a minimum of 86*F as measured by the 1B FC Pump Suction thermocouple.
The temperature of the 1B FC Loop was below 130 F from 0017 to 0433 on December 24, 1981.
Reactor pressure varied during this period between a maximum of 1145 psig and a minimum of 680 psig (Refer to attached table).
is Reference 2 states the Main Coolant System chrome piping RTN The 1B FC Loop temperature did not decrease b low fixed at 70 F.
the RT at anytime during this incident.
NDT An independent analysis of this incident was performed by Nuclear Energy Services.
The NES analysis also concluded the 1B FC Loop temperature did not decrease below the NDT.
A report covering this independent analysis will be docketed within the next few days. 9201150316 820106 gDRADOCKOSOOOg Y}d o22
O
. Mr. James G.;Keppler,. Regional-Director January 6, 1982 U. S. Nuclear Regulatory Commission LAC-8007 A Licensee Event Report (Reference:
Regulatory Guide 1.16, Revision 4).is enclosed.
~ If-there are any questions, please contact us.
Very truly yours, DAIRYLAND POWER COOPERATIVE Frank Linder, General Manager FL:LSG:af Attachment cc:
Director, Office of Inspection and En.forcement (30)
U.
S._ Nuclear Regulatory Commission Washington, D.
C.
20555 Director, Office of Management Information and (3)
Program Control U. S. Nuclear Regulatory Commission Washington, D. C.
20555 NRC Resident Inspector LAC-8007'- 1/6/82 1B FORCED CIRCULATION LOOP TEMPERATURE RATE OF TEMPERATURE
- TEMPERATURE PRESSURE CHANGE.BY. HOUR TIME
(*F)
(PSIG)
AFTER SCRAM 2115 551 1240 2215 384 1215
- - 167*/HR 2315 234 1140.
- - 150*/HR 0015 138 1080
- - 96*/HR 0017 132 0115' 101 1065
- - 37*/HR 0215 91 1145 (Max. Press. -
2 /HR below 130*F) 0223
'90 1100 3*/HR 0315 88 940 0341.
86 720
+
87 0345 86 0346 680
(-4*/HR 0315-0345)
+
'87 0354 86 735 0356 87 l
0415 90 820
+
2*/HR 0427 93 0430 109 820 j
0433 182 820 0435 212 i-0444 284 815 0515 263 780
+173*/HR
- 2*F was added to chart reading up until 0403 when chart paper returned to track.
The chart was off up to 4*F.
1 l-L
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| 05000409/LER-1981-001, Forwards LER 81-001/02L-0 | Forwards LER 81-001/02L-0 | | | 05000409/LER-1981-001-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | | | 05000409/LER-1981-001-03, /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | | | 05000409/LER-1981-002, Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-002-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | | | 05000409/LER-1981-003-03, /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | | | 05000409/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | | | 05000409/LER-1981-004-03, /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | | | 05000409/LER-1981-006-01, /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followe | /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followed | | | 05000409/LER-1981-006, Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-007-01, /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | | | 05000409/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000409/LER-1981-008-01, /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | | | 05000409/LER-1981-008, Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-009-03, /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | | | 05000409/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010, Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010-01, /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | | | 05000409/LER-1981-011-03, /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | | | 05000409/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-012-03, /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | | | 05000409/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-013-03, Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | | | 05000409/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-014-03, /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | | | 05000409/LER-1981-014, Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | | | 05000409/LER-1981-015, Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-015-01, /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | |
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