LER-1981-006, Forwards LER 81-006/01T-0.Detailed Event Analysis Encl |
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D DA/RYLAND h
[k COOPERAT/VE eo soxsi7 esis EAST AV SOUTH LA CROSSE. WISCONSIN M601 y
(60a17es4000 May 29, 1981 In reply, please o
o refer to LAC-7571 DOCKET.NO. 50-409
~
Mr. James G. Keppler, Director U. S. Nuclear Regulatory Co:tmission o>
Directorate of Regulatory Operations
,G Region III 799 Roosevelt Road
/(f o[-
/h D Glen Ellyn, Illinois 60137 f~
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SUBJECT:
DAIRYLAND POWER COOPERATIVE L's JUN 0519816 32 LA CROSSE ECILING WATER REACTOR (LACBWR)
", ' ' T M '***
PROVISIONAL OPERATING LICENSE NO. DPR-45 C'
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p, REPORTABLE CCCURRENCE NO. 81-06 4l
(*
References:
(1)
DPC Letter, LAC-7555, Linder to Keppler, dated May 19, 1981.
(2; LACBWR Technical Specifications, Section G.8.1.
(3)
LACBWR Technical Specifications, Section 6.5.1.6.d.
(4) u.unr.wechnical Specifications, Section 4.2.2.18.
(5)
LAC 3WR Technical Specifications, Section 4.2.2.15.
(6)
LACBWR Technical Specifications, Section 4.2.1.1.
(7)
LACBWR Technical Specifications,,
Section 4.0.1.
(8)
LACBWR Technical Specifications, Section 5.2.1.1. (b).
Dear Mr. Keppler:
This letter constitutes the written follow-up to the event reported to you in Reference 1.
The subject occurrence involved the discovery on May 18, 1981 of an attachment which had been added to the Contain-ment Building pressure sensing line leading to Pressure Switch 37-35-702 which activates IB High Pressure Core Spray Pump (HPCS) and 1B High Pressure Service Water (HPSW)/ Alternate Core Spray (ACS) pump and sends one of two required opening signals to the AC Alternate Core Spray Valve on high Containment Building pressure of 5 psig.
The in-I stallation had been made without an approved Maintenance Request or Facility Change.
. 88106 080 49$
Mr. James G. Keppler, Director LAC-7571 U. S. Nuclear Regulatory Commission May 29, 1981 This is contrary to DPC procedures, Reference 2, which requires that written procedures be implemented and Reference 3, shi~ch requires that the Operations Review Committee review all proposed changes or modifications to unit systems or equipment that affect nuclear safety.
The attachment consisted of an additional pressure switch, and isolation and drain valve, and 1/4 in. copper tubing (see attached sketch).
The attachment had been assembled and leak tested at 60 psig without leakage prior to being installed.
Reference 4 requires that the low pressure coolant injection system (ACS) shall be available for automatic operation except at times when the reactor is shut down and the system depressurized to approximately atmospheric pressure.
Reference 5 allows one core spray pump to be removed from service for maintenance provided that all control rods are fully inserted, the reacter pressure is less than 85 psig, the " Control Power" key switch is in the "0FF" position, and the low pressure core spray subsystem is operable.
During the installation on April 1, 1981, while the reactor was at 85% Rated Thermal Pcwer, the valve between the conrainment wall and Pressure Switch 37-35-702 was closed for less than one minute, there-by deactivating the pressure switch.
Therefore, the installation process reduced the degree of redundancy of actuating signals for the 1B HPCS Pump, 1B HPSW/ACS Pump and AC ACS valve, but would not have prevented system actuation if required.
Since a leakage test had not been performed immediately following installation, verification that Containment Integrity, as rcquired by References 6 and 7, was not reduced, was not achieved.
In order to accomplish a leakage test of the installation, it was necessary
' to prevent r " anted operation of the IB EPCS pump.
This temporary deactivatior.
- guired advanced authorization frcm the NRC.
The de-activation wa. accomplished by placing the 1B HPCS pump in " PULLOUT",
thereby preventing pump start with consequential injection of cold water into the reactor.
A leakage test was performed on May 19, 1981.
The previously untested connections did not leak, however, an extremely small amount of leak-age was detected by the soap bubble method on the new isolation valve leading to the new pressure switch.
The amount of leakage observed, when comparing the size and rate of bubbles, appeared considerably less than'what has previously been observed during electrical pene-tration tests with acceptable leakage rates.
Therefore, the test was considered acceptable. i
Mr. James G. Keppler, Director LAC-7571 U. S. Nuclear Regulatory Commission May 29, 1981 Since the maximum leakage allowable through an electrical penetration ir. 0.375 SCFH, the leakage through the attachment can be assumed -
to be less than 0.375 SCFH'."
If this amount of leakage is added to the as-left Containment Building leakage after the Type A test in December, the leakage rate would be 29.95 SCFH + 0.375 SCFH =
30.33 SCFH, or 0.06% per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, still well within the Technical Specification limit (Reference 8) of 0.1% per day, on which the accident analyses have been based.
Therefore, the actual safety consequences of the pressure switch installation were minimal.
After the satisfactory leakage test on May 19, 1981, the installation was removed and the system returned to its initial configuration.
Another leakage test was then conducted with zero leakage observed.
This event has been discussed with the responsible departments and individuals involved.
The importance of following the procedural requirements for proper review of proposed modifications has been atrossed.
This action should prevent reoccurrence of similar events.
A Licensee Event Report (Reference:
Regulatory Guide 1.16, Revision 4) is enclosed.
Should you have any questions regarding this submittal, please contact us.
Very truly yours, DAIRYLAI!D PCWER CCOPEPATIVE Frank Linder, General Manager FL:LSG:af Enclosures
. 1
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. Mr. James G. Keppler, Director -
LAC-7571 U.. S. Nuclear Regulatory Comissicn May 29, 1981 a
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Director, Office of Inspection and Enforcement - (3 0 )
U. S. Nuclear Regulatory Comission Washington, D. C.
20555 Director, Office of Management Information and (3)
Program Control U. S. Nuclear Regulatory Comission Washington, D. C.
.20555 NRC Resident Inspectors 9
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| 05000409/LER-1981-001, Forwards LER 81-001/02L-0 | Forwards LER 81-001/02L-0 | | | 05000409/LER-1981-001-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Disconnect Switch Opened Due to Operator Error.Two Operators to Operate Switching Order | | | 05000409/LER-1981-001-03, /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | /03L-0:on 810116,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Disconnected.Caused by Maint on Main Transformer Airbreak Switch 25NA1 Due to Ice in Swivel Joint.Ice Melted | | | 05000409/LER-1981-002, Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | Forwards LER 81-002/02L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-002-02, /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | /02L-0:on 810201,independent Circuit Between Offsite Transmission Network & Onsite Power Distribution Sys Was Disconnected.Caused by Operator Opening Incorrect Disconnect Switch.Switch Reclosed.Operators Retrained | | | 05000409/LER-1981-003-03, /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | /03L-0:on 810202,gross Alpha Activity of Primary Coolant Sample Exceeded Tech Spec.Caused by Degraded Fuel Cladding During Previous Fuel Cycles.Primary Purification Sys Operation Reduced Concentration to Allowable Level | | | 05000409/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-004/03L-0.Detailed Event Analysis Also Submitted | | | 05000409/LER-1981-004-03, /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | /03L-0:on 810309,during Condition 3,480-volt Diesel Bldg Essential Switchgear Bus 1B Was Energized from 1B Emergency Diesel Generator for Approx 25 Minutes W/Control Power Key in on Position | | | 05000409/LER-1981-006-01, /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followe | /01T-0:on 810518,during Installation of Attachment on Containment Pressure Sensing Line,High Containment Bldg Pressure Starting Signal to HPCS Pump 1B,auxiliary Cooling Sys Pump & AC Valve Was Isolated.Procedures Not Followed | | | 05000409/LER-1981-006, Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | Forwards LER 81-006/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-007-01, /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | /01T-0:on 810601,during Initial Integrated Sys Test W/Plant Shut Down,Emergency Svc Water Supply Sys Did Not Produce 900 Gpm at 90 Psig,As required.Three-way Distributor Fabricated.Sys Retested Satisfactorily | | | 05000409/LER-1981-007, Forwards LER 81-007/01T-0 | Forwards LER 81-007/01T-0 | | | 05000409/LER-1981-008-01, /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | /01T-0:on 810729,main Steam Bypass Valve Did Not Open During Momentary Pressure Spikes Approx 20 Psi Above Nominal Reactor Pressure.Caused by Decrease in Pressure Prior to Valve Opening Due to Short Duration & Spikes | | | 05000409/LER-1981-008, Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-008/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-009-03, /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | /03L-0:on 810917,upscale Trip Setpoint on Nuclear Instrument Channel 7 Found in Excess of Tech Spec Limit. Cause Not Determined.Setpoint Reset | | | 05000409/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010, Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-010/01T-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-010-01, /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | /01T-0:on 810923,during Normal Operation Mechanical Interlock Preventing Simultaneous Opening of Both Doors of Containment Bldg Personnel Airlock Failed.Caused by Worn or Misadjusted Actuating Mechanism.Drawings Encl | | | 05000409/LER-1981-011-03, /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | /03L-0:on 811031,observed That Radiation Hose on High Pressure Svc Water Diesel Engine 1B Was Slightly Cracked.Cause Not Stated.Hose Replaced & Diesel 1B Tested Satisfactorily | | | 05000409/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-012-03, /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | /03L-0:on 811101,gasoline Levels in Three Emergency Svc Water Supply Sys Gasoline Engine Driven Pumps & Spare Pump Found to Be Less than 5 Gallons During Monthly Insp.Cause Unknown.Gasoline Added to Fill Tanks | | | 05000409/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-012/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-013-03, Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | Following scram,1B 2,400-volt Bus Reserve Feed Breaker Did Not Close Automatically.Cause Undetermined.Reserve Feed Breaker Control Switch Flagged to Trip Position | | | 05000409/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-013/03L-0.Detailed Event Analysis Submitted | | | 05000409/LER-1981-014-03, /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | /03L-0:on 811223,following Scram,Offsite Transmission Network Did Not Automatically Supply Onsite Power Distribution Sys.Cause Undetermined.Transformer Breaker Closed | | | 05000409/LER-1981-014, Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | Forwards LER 81-014/03L-0 & Updated LER 81-013/03X-1. Detailed Event Analysis Encl | | | 05000409/LER-1981-015, Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | Forwards LER 81-015/01T-0.Detailed Event Analysis Encl | | | 05000409/LER-1981-015-01, /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | /01T-0:on 811224,following Reactor Scram,Temp of 1B Forced Circulation Loop Piping Decreased Below Tech Specs Limit.Caused by Inoperation of Pump Due to Seal Problems & Lack of Monitoring.Personnel Reinstructed | |
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