05000409/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-003/03L-0.Detailed Event Analysis Encl
ML20008E908
Person / Time
Site: La Crosse File:Dairyland Power Cooperative icon.png
Issue date: 02/25/1981
From: Linder F
DAIRYLAND POWER COOPERATIVE
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20008E909 List:
References
LAC-7383, NUDOCS 8103100495
Download: ML20008E908 (6)


LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
4091981003R00 - NRC Website

text

.

,03a6' D DA/RYLAND [k

COOPERAT/VE PO BOX 817

  • 2615 EAST AV SOUTH. LA CROSSE WISCCNSIN 9601 1608) 788-4000 February 25, 1981 In reply, please refer to LAC-7383 DOCKET NO. 50-409 Mr. James G. Keppler Regional Director U. S. Nuclear Regulatory Commission C

g Directorate of Regulatory Operations

'/N Region III y

Il N

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799 Roosevelt Road

{

Glen Ellyn, Illinois 60137 MAR 0 91981== 5 i:

SUBJECT:

DAIRYLAND POWER COOPERATIVE u m m.

LA CROSSE BOILING WATER REACTOR (LACBWR)

A**

,;S/

PROVISIONAL OPERATING LICENSE NO. DPR-4 5

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REPORTABLE OCCURRENCE NO. 81-03 References:,(1)

LACBWR Technical Specifications, Section 3. 9. 2.b. (2).

(2)

LACBWR Technical Specifications, LCO 4.2.2.22.a.3.

(3)

LACBWR Technical Specifications, Section 4.2.2.22.f.

Dear Mr. Keppler:

s In accordance with Reference (1), this is to notify you of conditions leading to operation in a degraded mode permitted by a limiting condition for operation.

Reference (2) established the li

'tions for the gross alpha activity of the reactor coolant system.

Reference (3) established sampling

.alysis and reporting requirements in the event the gross alpha activity of the reactor coolant system exceeded specified limits.

An analysis of a reactor coolant system sample taken at the inlet to the primary purification system cation exchanger at 0138 hours0.0016 days <br />0.0383 hours <br />2.281746e-4 weeks <br />5.2509e-5 months <br /> on February 2, 1981, while the plant was at 22% Reactor Rated Thermal Power, indicated that the coolant gross alpha activity exceeded the limiting condition for operation (1 5.0 x 10-8 pCi/ gram).

The as-found gross alpha activity value was 5.46 x 10-6 u Ci/gm. The sample was also analyzed for gross S y activity and iodine activity.

See for these results and the Additional Information required by Reference 3.

h'4% 8,1081009'6 2

219m 5

Mr. James G.

Keppler LAC-7383 Regional Director February 25, 1981 A second sample was taken approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> (4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 17 minutes) after the first, which was approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> after the first sample had been analyzed.

The alpha activity was 1.79 x 10 7 pCi/ml, well within the Technical Specification limit.

There-fore, the additional sampling for gross B y and iodine activities was no longer required and the reactor did not have to be shut down.

A third sample was taken at 0709 as a precaution.

The alpha activity was 1.27 x 10-7 pCi/ml.

This sample was also analyzed for iodine activities as a confirmatory measure.

These results are also reported in Attachment 1.

The observed increase in alpha activity was not considered attrib-utable to fuel failures.

This is supported by the relatively low Sy and iodine activities measured.

The increase in iodine activities between the 0138 and 0709 samples reflects the power increase.

The samples were taken during the power escalation for the commence-ment of Cycle 7.

The contribution to the temporary indicated in-crease in~ gross alpha activity of the reactor coolant system came from residual irradiated fuel material which entered the system as a result of degraded fuel pin cladding primarily experienced during Cycle 4 and to a much lesser degree during Cycle 5 and subsequent handling of the irradiated fuel assemblies during refueling.

Hand-ling of core components during refueling and later operation of the forced circulation pumps resulted in the more general distribution of suspended alpha bearing material in the coolant.

The reactor scram and tripping and restart of the forced circulation pumps on February 1, 1981, caused resuspension of alpha emitting material previously deposited at various points in the primary system.

This effect has been witnessed in the past.

(Refer to RO 80-05, 80-06 and 79-10).

In addition, the primary purification system had been shut down for approximately five hcurs after the scram and had only been operating for several hours prior to the first sample being-taken.

The two subsequent samples provide evidence that the relatively high alpha activity was a temporary condition and that operation of the primary purification system reduces the alpha-emitting material suspended in the primary coolant.

Therefore, no further corrective action was considered necessary.

A Licensee Event Report (Ref. Appendix A, Regulatory Guide 1.16, Revision 4) is enclosed.

Mr. James G. Keppler LAC-7383 Regional Director February 25, 1981 If there are any questions concerning this report, please contact us.

Very truly yours, DAIRYLAND POWER COOPERATIVE t

.j t..,. L

,--w-Frank Linder, General Manager FL:LSG:af Enclosures cc:

Director, Office of Inspection and Enforcement (30)

U. S. Nuclear Regulatory Commission Washington, D.

C.

20555 Director, Office of Management Information and (3)

Program Control U. S. Nuclear Regulatory Commission Washington, D. C.

20555 NRC Resident Inspectors L '

LAC-7383 - 2/25/81 ATTACHMENT 1 ACTIVITY ANALYSES AND ADDITIONAL INFORMATION l

i Gross Beta and Gamma Activity:

0138, 2/2/81 6.92 x 10 2 pCi/ml 1110, 2/2/81

.324 pCi/ml Iodine Activity:

0138, 2/2/81 I-131 6.222.x 10-5 pCi/ml I-133 1.175 x 10-3 pCi/ml I-135

<7.958 x 10-4 pCi/ml 0709, 2/2/81 I-131 5.454 x 10-4 pCi/ml I-133 5.758 x 10-3 pCi/ml I-135 1.507 x 10-2 pCi/ml Alpha Activity:

0138, 2/2/81 5.46 x 10 8 p Ci/m1' 0555, 2/2/81 1.79 x 107 pCi/ml 0709, 2/2/81 1.27 x 107 pCi/ml

Additional Information

1)

Reactor power history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to sample in which limit was exceeded.

0200, 1/31/81.... 26%

0250, 1/31/81..... Commenced power reduction to S 0%.

0300,- 0700, 1/31/81.... s.2%

0800 - 2100, 1/31/81.... s.1%

2200 - 2400, 1/31/81....

.1 - 21%

0000 - 1100, 2/1/81.....

21% - 28%

1134, 2/1/81...... Reactor Scram 1543, 2/1/81...... Reactor Critical 2100 - 2200, 2/1/81.......3% - 20%

2200, 2/1/81 - 0138, 2/2/81.... 20%

22%

2)

Fuel burnup by core region:

See attached figure.

LAC-7383 - 2/25/81 ATTACHMENT 1 ' ACTIVITY ANALYSES AND ADDITIONAL INFORMATION - (Cont'd) 3)

Cleanup flow history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to sample in which limit was exceeded:

0100-2300, 1/31/81 45 gpm 2400, 1/31/81 44.5 gym 0100-0600, 2/1/81 44 gpm 0700-1100, 2/1/81 44.5 gpm 1200-1700, 2/1/81 Shutdown 1800-2100, 2/1/81 46 gpm 2200, 2/1/81 - 0200, 2/2/81 45.5 gpm 4)

Off gas level starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to sample in which limit was exceeded:

0000, 1/31/81 - 0000, 2/1/81 No Off-Gas Generated 0000-0800, 2/1/81 50 Ci/ day 0800-2400, 2/1/81 No Off-Gas Generated 5)

Gross alpha activity level starting with the last sample taken prior to sample in which limit was exceeded:

0036, 1/26/81 5.65 x 10-7 pCi/ml 0138, 2/2/81 5.46 x 10-6 pCi/ml 0555, 2/2/81 1.79 x 10-7 pCi/ml 0709, 2/2/81 1.27 x 10-7 uCi/mi _

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