05000390/FIN-2016002-02
From kanterella
Jump to navigation
Jump to search
Finding | |
|---|---|
| Title | Failure to Translate Design Requirements into a Maintenance Procedure for the 1B-B Charging Pump Room Cooler |
| Description | The NRC identified a Green NCV of 10 Code of Federal Regulations (CFR) 50, Appendix B, Criterion III, Design Control for the licensees failure to specify nominal shaft size along with specific acceptance criteria for shaft tolerance measurements for the 1B-B centrifugal charging pump (CCP) room cooler fan shaft. The licensee repaired the room cooler by replacing the fan shaft and the finding was entered into the licensees corrective action program as CR 1146474. The performance deficiency was more than minor because it affected the equipment performance attribute of the mitigating system cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors determined that this finding required a detailed risk analysis since it represented an actual loss of function of a single train for greater than its TS-allowed outage time. The finding does not present an immediate safety concern because the licensee has verified current operability. A Senior Reactor Analyst evaluated the increase in core damage frequency due to the pump being non-functional over the exposure period and determined it was 3.6E-7/year (Green). The dominant scenario was a loss of component cooling water, which combined with a loss of RCP seal injection causes a loss of coolant accident and leads to core damage. The risk increase was very low because of the limited exposure time, the availability of the opposite train pump, and the time dependent nature of the pump failing due to lack of room cooling. The inspectors determined that the finding had a cross-cutting aspect of design margin in the area of Human Performance because the licensee failed to carefully guard margins through a systematic and rigorous process. Specifically, the translation of shaft diameter from design documents into 0-MI-0.16 lacked rigor and allowed an undersized shaft to go undetected, leading to cooler failure. |
| Site: | Watts Bar |
|---|---|
| Report | IR 05000390/2016002 Section 1R15 |
| Date counted | Jun 30, 2016 (2016Q2) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.15 |
| Inspectors (proximate) | A Blamey A Lerch C Young D Dumbacher D Jones G Callaway J Eargle J Hamman J Jandovitz J Nadel L Micewski N. Pitoniak R Fanner S Sanchez |
| Violation of: | 10 CFR 50 Appendix B 10 CFR 50 Appendix B Criterion III, Design Control |
| CCA | H.6, Design Margins |
| INPO aspect | WP.2 |
| ' | |
Finding - Watts Bar - IR 05000390/2016002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Watts Bar) @ 2016Q2
Self-Identified List (Watts Bar)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||