05000387/LER-2006-005, Regarding HPCI Safety Function Compromised

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Regarding HPCI Safety Function Compromised
ML063120117
Person / Time
Site: Susquehanna Talen Energy icon.png
Issue date: 10/25/2006
From: Saccone R
Susquehanna
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
PLA-6122 LER 06-005-00
Download: ML063120117 (4)


LER-2006-005, Regarding HPCI Safety Function Compromised
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3872006005R00 - NRC Website

text

R. A. Saccone Vice President - Nuclear Operations PPL Susquehanna, LLC 769 Salem Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542-1504 rasaccone @ pplweb.com t lI p p 00 >"

0m, T M OCT ?5 2006 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop OP1-17 Washington, DC 20555 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-387/2006-005-00 PLA-6122 Docket 50-387 Attached is Licensee Event Report 50-387/2006-005-00. This event was determined to be reportable per 10 CFR 50.73(a)(2)(v)(D) when surveillance testing revealed a condition that could have compromised the Unit 1 High Pressure Coolant Injection System's ability to respond within Technical Specification time limitations.

There were no actual consequences to the health and safety of the public as a result of this event.

No new regulatory commitments have been created through issuance of this report.

'Ro.

t. S accne Vice President - Nuclear Operations Attachment cc':

Mr. A:J 'Blamey, NRC Sr. Resident Inspector Mr. S. J. Collins, NRC Regional Administrator, Region I Mr. R. R. Janati, DEP/BRP Mr. R. Osborne, Allegheny Electric

K' H

NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME Susquehanna Steam Electric Station - Unit 1
2. DOCKET NUMBER
3. PAGE 05000387 1 OF3
4. TITLE HPCI Safety Function Compromised
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED SEQUENTIAL REV MONTH DAY YEAR FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR MONTHRDAY.YEAR00 NUMBER NO.

___I05000 FACILITY NAME DOCKET NUMBER 08 31 2006 2006 005 00 10 25 2006 05000

9. OPERATING MODE
11. THIS REPORT IS SUBMRrIED PURSUANTTO THE REQUIREMENTS OF 10CFR §: (Checkall that apply) 1 E] 20.2201 (b)

El 20.2203(a)(3)(i)

El 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii)

10. POWER LEVEL

[] 20.2201 (d)

[] 20.2203(a)(3)(ii)

[I 50.73(a)(2)(ii)(A)

El 50.73(a)(2)(viii)(A)

El 20.2203(a)(1)

El 20.2203(a)(4)

[I 50.73(a)(2)(ii)(B)

[] 50.73(a)(2)(viii)(B) 100%

El 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

[I 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

El 20.2203(a)(2)(ii)

E] 50.36(c)(1)(ii)(A)

[I 50.73(a)(2)(iv)(A)

El 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

El 50.36(c)(2)

[I 50.73(a)(2)(v)(A)

El 73.71 (a)(4)

El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

El 50.73(a)(2)(v)(B)

El 73.71 (a)(5)

El 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

[E 50.73(a)(2)(v)(C)

El OTHER Voluntary Report El 20.2203(a)(2)(vi)

[E 50.73(a)(2)(i)(B)

[D 50.73(a)(2)(v)(D)

Specify in Abstract below or in (If more space is required, use additonal copies of (if more space is required, use additional copies of NRC Form 366A)

CORRECTIVE ACTIONS

The following corrective actions have been completed:

The rod bushing has been replaced.

The preventive maintenance schedule has been recalculated to ensure the next rod bushing replacement conforms to the intended replacement frequency.

ADDITIONAL INFORMATION

Failed Components Information:

Component:

Manufacturer:

HPCI Turbine Stop Valve, FV-15612 Schutte & Koerting Past Similar Events:

None