| | | Reporting criterion |
|---|
| 05000387/LER-1986-001, :on 860110,two Divs of Control Room Emergency Outside Air Supply Sys Declared Inoperable Resulting in Four Dampers Not Being Tested.Caused by Procedure Deficiency. Dampers Tested.Procedures Will Be Reviewed |
- on 860110,two Divs of Control Room Emergency Outside Air Supply Sys Declared Inoperable Resulting in Four Dampers Not Being Tested.Caused by Procedure Deficiency. Dampers Tested.Procedures Will Be Reviewed
| 10 CFR 50.73(a)(2)(1) |
| 05000388/LER-1986-001-01, :on 860121,during Startup,Reactor Scrammed When Vessel Water Level Dropped to Plus 13 Inches.Caused by Operator Failing to Notice Turbine Bypass Valves Opened. Procedures Revised.Alarms Will Be Installed |
- on 860121,during Startup,Reactor Scrammed When Vessel Water Level Dropped to Plus 13 Inches.Caused by Operator Failing to Notice Turbine Bypass Valves Opened. Procedures Revised.Alarms Will Be Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-002-01, :on 860206,during Performance of 31-day Chemistry Surveillance,Available Weight of Sodium Pentaborate Less than Tech Spec Limit of 5,500 Lb.Caused by Improper Valve Closure.Valve Closed Tightly |
- on 860206,during Performance of 31-day Chemistry Surveillance,Available Weight of Sodium Pentaborate Less than Tech Spec Limit of 5,500 Lb.Caused by Improper Valve Closure.Valve Closed Tightly
| 10 CFR 50.73(a)(2)(i) |
| 05000388/LER-1986-002, :on 860122,HPCI Sys Shut Down During Quarterly Flow Surveillance Test.Caused by Leak of Approx 5 Gpm in Pressure Control Valve 2F035 Due to Tear in Main Diaphragm. Diaphragm Replaced.Test Completed |
- on 860122,HPCI Sys Shut Down During Quarterly Flow Surveillance Test.Caused by Leak of Approx 5 Gpm in Pressure Control Valve 2F035 Due to Tear in Main Diaphragm. Diaphragm Replaced.Test Completed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000387/LER-1986-003-01, :on 860216,partial Loss of Power Occurred to Div I Nuclear Steam Supply Shutoff Sys.Caused by Mislabeling of Four of Eight Breakers.Breakers Relabeled |
- on 860216,partial Loss of Power Occurred to Div I Nuclear Steam Supply Shutoff Sys.Caused by Mislabeling of Four of Eight Breakers.Breakers Relabeled
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-003, :on 860124,Tech Spec Motherhood Clause Entered Due to Malfunctioning Which Provides ECCS Initiation Signals.Caused by Broken Adjustment Locking Screw Replaced |
- on 860124,Tech Spec Motherhood Clause Entered Due to Malfunctioning Which Provides ECCS Initiation Signals.Caused by Broken Adjustment Locking Screw Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000387/LER-1986-004, :on 860129,standby Gas Treatment Sys Train a Manually Initiated to Maintain 0.25 Inch Wg Vacuum in Secondary Containment.Caused by Unanticipated Actuation of Esf.Actuator Air Regulator Adjusted |
- on 860129,standby Gas Treatment Sys Train a Manually Initiated to Maintain 0.25 Inch Wg Vacuum in Secondary Containment.Caused by Unanticipated Actuation of Esf.Actuator Air Regulator Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-004-01, :on 860115,reactor Manually Scrammed Due to Overheating of Phase Main Transformer B.Caused by Improper Alignment of Knife Switches to Transformer Cooling Loops. Knife Switches Corrected |
- on 860115,reactor Manually Scrammed Due to Overheating of Phase Main Transformer B.Caused by Improper Alignment of Knife Switches to Transformer Cooling Loops. Knife Switches Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-005-01, :on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & Lubricated |
- on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & Lubricated
| |
| 05000387/LER-1986-005, :on 860228,Zone III of Reactor Bldg Ventilation Isolated on High Railroad Access Shaft Radiation.Caused by Increase in Background Radiation Due to Shine from CRD Mechanisms.Lead Shields Installed |
- on 860228,Zone III of Reactor Bldg Ventilation Isolated on High Railroad Access Shaft Radiation.Caused by Increase in Background Radiation Due to Shine from CRD Mechanisms.Lead Shields Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-006-01, :on 860413,inboard Containment Isolation Valve Closed & RWCU Pumps Tripped.Caused by Isolation of RWCU During High Differential Flow as RWCU Filter/Demineralizer Being Returned to Svc.No Action Planned |
- on 860413,inboard Containment Isolation Valve Closed & RWCU Pumps Tripped.Caused by Isolation of RWCU During High Differential Flow as RWCU Filter/Demineralizer Being Returned to Svc.No Action Planned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-006, :on 860304,Div II LOCA Isolation Signal Generated.Caused by Power Interruption to LOCA Logic While Loose States Link Being Tightened.No Corrective Actions Planned |
- on 860304,Div II LOCA Isolation Signal Generated.Caused by Power Interruption to LOCA Logic While Loose States Link Being Tightened.No Corrective Actions Planned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-007, :on 860315,unplanned Div I LOCA Isolation Occurred When Fuse Blew in Nuclear Steam Supply Shutoff Sys Logic.No Specific Cause Determined.Fuse Replaced & Isolation Logic Reset |
- on 860315,unplanned Div I LOCA Isolation Occurred When Fuse Blew in Nuclear Steam Supply Shutoff Sys Logic.No Specific Cause Determined.Fuse Replaced & Isolation Logic Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-007-01, :on 860609,as-found Leakage Exceeded Tech Spec 3.6.1.2 Criteria During Integrated Leak Rate Test.Cause Unstated.Isolation Valves Reworked |
- on 860609,as-found Leakage Exceeded Tech Spec 3.6.1.2 Criteria During Integrated Leak Rate Test.Cause Unstated.Isolation Valves Reworked
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000388/LER-1986-008-01, :on 860619,HPCI Sys Failed to Attain Required Flow Rate & Declared Inoperable.Caused by Broken Control Valve.Valve Repaired & Procedure SO-252-002 Reperformed.W/ |
- on 860619,HPCI Sys Failed to Attain Required Flow Rate & Declared Inoperable.Caused by Broken Control Valve.Valve Repaired & Procedure SO-252-002 Reperformed.W/
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 05000387/LER-1986-008, :on 860314,six Inadvertent Actuations of Reactor Protection Sys Channel a Occurred.Probably Caused by CRD Changeout Activities in under-vessel Area.Changeout Effort Will Be Reviewed W/Foremen |
- on 860314,six Inadvertent Actuations of Reactor Protection Sys Channel a Occurred.Probably Caused by CRD Changeout Activities in under-vessel Area.Changeout Effort Will Be Reviewed W/Foremen
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-009-01, :on 860708,Limiting Condition for Operation 3.0.3 Entered Twice.Caused by Surveillance Procedure SI-280-305 Being Performed While RCIC Sys Inoperable.W/ |
- on 860708,Limiting Condition for Operation 3.0.3 Entered Twice.Caused by Surveillance Procedure SI-280-305 Being Performed While RCIC Sys Inoperable.W/
| 10 CFR 50.73(a)(2)(1) |
| 05000387/LER-1986-009, :on 860315,half Scram Signal Generated on Div I of Reactor Protection Sys Due to Noise Induced Upscale Trip of intermediate-range Monitors C & G.Caused by Relay Cycling.Actuation Cleared |
- on 860315,half Scram Signal Generated on Div I of Reactor Protection Sys Due to Noise Induced Upscale Trip of intermediate-range Monitors C & G.Caused by Relay Cycling.Actuation Cleared
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-010-01, :on 860717,reactor Manually Shut Down Due to Excessive Unidentified Drywell Leakage.Caused by Leaking RHR Loop B Injection Testable Check Valve HV-251-F050B.Valve Repacked & Returned to Svc |
- on 860717,reactor Manually Shut Down Due to Excessive Unidentified Drywell Leakage.Caused by Leaking RHR Loop B Injection Testable Check Valve HV-251-F050B.Valve Repacked & Returned to Svc
| 10 CFR 50.73(a)(2)(1) |
| 05000387/LER-1986-010, :on 860327,both Access Hatches to Reactor Bldg Ventilation Sys Recirculation Plenum Found Open,Affecting Secondary Containment Integrity.Caused by Maint Personnel Error.Future Work Plans Modified |
- on 860327,both Access Hatches to Reactor Bldg Ventilation Sys Recirculation Plenum Found Open,Affecting Secondary Containment Integrity.Caused by Maint Personnel Error.Future Work Plans Modified
| 10 CFR 50.73(a)(2)(i) |
| 05000388/LER-1986-011-01, :on 860717,limiting Condition for Operation Not Entered When Primary Containment Isolation Valve Inoperable. Caused by Smoking Electrical Components from Transversing in-core Probe Machine C |
- on 860717,limiting Condition for Operation Not Entered When Primary Containment Isolation Valve Inoperable. Caused by Smoking Electrical Components from Transversing in-core Probe Machine C
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-011, :on 860325,reactor Protection Sys Actuated. Caused by Maint Personnel Error,Resulting in Upscale Spike from Intermediate Range Monitor.Existing Procedures Adequate.No Further Action Planned |
- on 860325,reactor Protection Sys Actuated. Caused by Maint Personnel Error,Resulting in Upscale Spike from Intermediate Range Monitor.Existing Procedures Adequate.No Further Action Planned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-012, :on 860328,Train B of Standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Started W/Invalid Div II LOCA Signal.Caused by Blown Fuse by Electrician.Work Practices Emphasized |
- on 860328,Train B of Standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Started W/Invalid Div II LOCA Signal.Caused by Blown Fuse by Electrician.Work Practices Emphasized
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-013, :on 860402,procedure Deficiency Caused Div I of Reactor Bldg Zone III Ventilation Sys to Isolate & Standby Gas Treatment Sys to Initiate.Procedure Will Be Revised to Disable Isolation Logic |
- on 860402,procedure Deficiency Caused Div I of Reactor Bldg Zone III Ventilation Sys to Isolate & Standby Gas Treatment Sys to Initiate.Procedure Will Be Revised to Disable Isolation Logic
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-013-01, :on 860919,full Reactor Protection Sys Scram Occurred When Intermediate Range Monitors C & G Spiked Upscale.Caused by Noise Due to Faulty Primary Containment Penetration Connectors.Cables Rebuilt |
- on 860919,full Reactor Protection Sys Scram Occurred When Intermediate Range Monitors C & G Spiked Upscale.Caused by Noise Due to Faulty Primary Containment Penetration Connectors.Cables Rebuilt
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-014, :on 860927-30,sampling of RHR Svc Water Effluent Not Completed as Required by Tech Specs.Caused by Communication Problems.Administrative Controls Implemented to Correct Communication Deficiencies |
- on 860927-30,sampling of RHR Svc Water Effluent Not Completed as Required by Tech Specs.Caused by Communication Problems.Administrative Controls Implemented to Correct Communication Deficiencies
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-014, :on 860410,during Refueling Outage,Scram Discharge Vol (SDV) Level Transmitters Found Isolated from Sdv.Caused by Transmitters Being Locked Closed & Incorrect Checkoff List |
- on 860410,during Refueling Outage,Scram Discharge Vol (SDV) Level Transmitters Found Isolated from Sdv.Caused by Transmitters Being Locked Closed & Incorrect Checkoff List
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-015, :on 860415,Div II LOCA Isolation Occurred, Causing Isolation of Zones I & III HVAC Sys,Initiation of Standby Gas Treatment Sys B & Control Room Emergency Outside Air Supply Sys B.Caused by Blown Fuse |
- on 860415,Div II LOCA Isolation Occurred, Causing Isolation of Zones I & III HVAC Sys,Initiation of Standby Gas Treatment Sys B & Control Room Emergency Outside Air Supply Sys B.Caused by Blown Fuse
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-015, :on 861012,primary Containment Isolation Valve Closed Twice Due to Spurious High Flow Signal.Caused by Waterhammer Due to Opening of Valve F008.Operations Personnel Will Review Event |
- on 861012,primary Containment Isolation Valve Closed Twice Due to Spurious High Flow Signal.Caused by Waterhammer Due to Opening of Valve F008.Operations Personnel Will Review Event
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-015-01, :on 861012,valve F008 Isolated Twice,Due to Spurious High Flow Signal & Water Hammer,Respectively. Water Hammer Caused by Partial Draindown of Sys.Personnel Will Review Event |
- on 861012,valve F008 Isolated Twice,Due to Spurious High Flow Signal & Water Hammer,Respectively. Water Hammer Caused by Partial Draindown of Sys.Personnel Will Review Event
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-016-01, :on 861024,DX Unit Valve a Discovered Mispositioned.Caused by Procedure Incorrectly Stating That Valve a Be Placed at Zero Position.Procedure Revised to Reflect Correct Repositioning |
- on 861024,DX Unit Valve a Discovered Mispositioned.Caused by Procedure Incorrectly Stating That Valve a Be Placed at Zero Position.Procedure Revised to Reflect Correct Repositioning
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000387/LER-1986-016, :on 860412,automatic Scram Signal Generated on Reactor Protection Sys When Reactor Vessel Water Level Dropped.Caused by Vessel Level Indication Error Resulting from Valve Pack Leak.Event Reviewed by Staff |
- on 860412,automatic Scram Signal Generated on Reactor Protection Sys When Reactor Vessel Water Level Dropped.Caused by Vessel Level Indication Error Resulting from Valve Pack Leak.Event Reviewed by Staff
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-017-01, :on 861101,unplanned ESF Actuation Occurred & RWCU Sys Isolated in High Sys Flow.Caused by Instantaneous Flow Spike Induced by Cracking Open Bypass Valve.Design Changes Initiated.Sys Returned to Svc |
- on 861101,unplanned ESF Actuation Occurred & RWCU Sys Isolated in High Sys Flow.Caused by Instantaneous Flow Spike Induced by Cracking Open Bypass Valve.Design Changes Initiated.Sys Returned to Svc
| |
| 05000387/LER-1986-017, :on 860414,isolations of Reactor Bldg Ventilation Zones I & II Occurred,Causing Standby Gas Treatment Sys & Emergency Outside Air Sys to Initiate.Caused by Improper Performance of Procedure |
- on 860414,isolations of Reactor Bldg Ventilation Zones I & II Occurred,Causing Standby Gas Treatment Sys & Emergency Outside Air Sys to Initiate.Caused by Improper Performance of Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-018, :on 860415,LOCA Isolation & Half Scram Caused Shutdown of Cooling,Isolation of HVAC Sys & Initiation of Standby Gas Treatment Sys.Caused by Arc When Test Lead Bumped Off.Review of Sys Underway |
- on 860415,LOCA Isolation & Half Scram Caused Shutdown of Cooling,Isolation of HVAC Sys & Initiation of Standby Gas Treatment Sys.Caused by Arc When Test Lead Bumped Off.Review of Sys Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000388/LER-1986-018-01, :on 861219,125-volt Dc Battery Charger 1D613 Inoperable.Unit 1 Supervisor Failed to Inform Unit 2 Supervisor of Equipment Failure,Resulting in Violation of Tech Spec.Battery Replaced |
- on 861219,125-volt Dc Battery Charger 1D613 Inoperable.Unit 1 Supervisor Failed to Inform Unit 2 Supervisor of Equipment Failure,Resulting in Violation of Tech Spec.Battery Replaced
| |
| 05000387/LER-1986-019, :on 860428,limiting Condition for Operation Action Statement 3.0.3 Entered Three Times to Perform Surveillance on 4.16 Kv Bus Undervoltage Relays.Caused by Absence of Action Statement |
- on 860428,limiting Condition for Operation Action Statement 3.0.3 Entered Three Times to Perform Surveillance on 4.16 Kv Bus Undervoltage Relays.Caused by Absence of Action Statement
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000388/LER-1986-019-01, :on 861218,22 & 25,facility Entered Limiting Condition for Operation 3.0.3 Three Times to Sample Wetwell. Caused by Off Normal Valve Lineup of Containment Radiation Monitoring Sys.Operating Strategy Reviewed |
- on 861218,22 & 25,facility Entered Limiting Condition for Operation 3.0.3 Three Times to Sample Wetwell. Caused by Off Normal Valve Lineup of Containment Radiation Monitoring Sys.Operating Strategy Reviewed
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-020, :on 860516,during Testing of Outside Air Intake Process Radiation Monitor B,Emergency Outside Air Supply Sys Train B Actuated.Caused by Jumper Not Making Contact W/ Terminals.Test Jacks Will Be Installed |
- on 860516,during Testing of Outside Air Intake Process Radiation Monitor B,Emergency Outside Air Supply Sys Train B Actuated.Caused by Jumper Not Making Contact W/ Terminals.Test Jacks Will Be Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-021, :on 860524,controlled Shutdown Initiated When All Emergency Svc Water (ESW) Sys Pumps Declared Inoperable. Caused by 860522 Failure of ESW Pump C Due to Severe Cavitation Damage.Pumps Repaired |
- on 860524,controlled Shutdown Initiated When All Emergency Svc Water (ESW) Sys Pumps Declared Inoperable. Caused by 860522 Failure of ESW Pump C Due to Severe Cavitation Damage.Pumps Repaired
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-022, :on 860601,start-up Bus 20 Deenergized,Causing Loss of Power.Caused by Cycling of Circuit Breaker 3T.Work Plans Reviewed & Sys Operating Instructions Revised |
- on 860601,start-up Bus 20 Deenergized,Causing Loss of Power.Caused by Cycling of Circuit Breaker 3T.Work Plans Reviewed & Sys Operating Instructions Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-023, :on 860612,ESF Actuation Occurred Due to EPA Breaker Trip.Caused by High Internal Temp as Result of Loose Breaker Contact Mounting Screw.Screw Tightened & Breaker Returned to Svc |
- on 860612,ESF Actuation Occurred Due to EPA Breaker Trip.Caused by High Internal Temp as Result of Loose Breaker Contact Mounting Screw.Screw Tightened & Breaker Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-024, :on 860703,discovered That Automatic Pump Start Relays Not Seismically Qualified.Cause Not Stated.Relays Replaced |
- on 860703,discovered That Automatic Pump Start Relays Not Seismically Qualified.Cause Not Stated.Relays Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000387/LER-1986-025, :on 860627,both Channels of Degraded Voltage Protection Inoperable While Limiting Condition for Operation 3.2.3 Entered & Cleared Eight Times to Perform Surveillance Testing.Tech Spec Change Requested |
- on 860627,both Channels of Degraded Voltage Protection Inoperable While Limiting Condition for Operation 3.2.3 Entered & Cleared Eight Times to Perform Surveillance Testing.Tech Spec Change Requested
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-026, :on 860623,determined That Available Weight of Sodium Pentaborate in Standby Liquid Control Sys Storage Tank Below 5,330 Lbs as Required by Tech Spec 3.1.5. Chemicals Added & Solution Retested |
- on 860623,determined That Available Weight of Sodium Pentaborate in Standby Liquid Control Sys Storage Tank Below 5,330 Lbs as Required by Tech Spec 3.1.5. Chemicals Added & Solution Retested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000387/LER-1986-027, :on 860725,w/Unit 1 Operating at 100% Power & Unit 2 Operating at 79% Power,Limiting Condition for Operation 3.0.3 Entered to Perform Surveillance Testing.Tech Spec Change Requested to Clarify Action |
- on 860725,w/Unit 1 Operating at 100% Power & Unit 2 Operating at 79% Power,Limiting Condition for Operation 3.0.3 Entered to Perform Surveillance Testing.Tech Spec Change Requested to Clarify Action
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-028, :on 860801 & 06,various Trips & Isolation Occurred.Caused by Transfer of Bus 10 Loads to Bus 20 Due to Lightning Strikes to 230 Kv Transmission Line.New Breaker Tested & Installed & Units Stabilized |
- on 860801 & 06,various Trips & Isolation Occurred.Caused by Transfer of Bus 10 Loads to Bus 20 Due to Lightning Strikes to 230 Kv Transmission Line.New Breaker Tested & Installed & Units Stabilized
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-029, :on 860816,initiations of Standby Gas Treatment & Control Room Emergency Outside Air Supply Sys B Occurred.Caused by Defective GE Electrical Protection Assembly Board (Epa).Board Replaced |
- on 860816,initiations of Standby Gas Treatment & Control Room Emergency Outside Air Supply Sys B Occurred.Caused by Defective GE Electrical Protection Assembly Board (Epa).Board Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000387/LER-1986-030, :on 860825,Limiting Condition for Operation 3.0.3 Entered & Cleared Four Times to Perform Surveillances on 4.16 Kv Engineered Safety Sys Buses.Caused by Tech Spec Discrepancy.Tech Spec Being Changed |
- on 860825,Limiting Condition for Operation 3.0.3 Entered & Cleared Four Times to Perform Surveillances on 4.16 Kv Engineered Safety Sys Buses.Caused by Tech Spec Discrepancy.Tech Spec Being Changed
| 10 CFR 50.73(a)(2)(i) |
| 05000387/LER-1986-031, :on 860829,reactor Protection Sys Distribution Panel Circuit Breaker Opened for Planned Maint Resulting in Unplanned ESF Actuations.Caused by Failure to Make Proper Correlation.Circuit Breaker Reclosed |
- on 860829,reactor Protection Sys Distribution Panel Circuit Breaker Opened for Planned Maint Resulting in Unplanned ESF Actuations.Caused by Failure to Make Proper Correlation.Circuit Breaker Reclosed
| 10 CFR 50.73(a)(2)(iv), System Actuation |