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s U S. NUCLEt460 kELULATOAV COamstessoas seRC Form 3RB APPROvt0 0e80 peO 3190-4104 LICENSEE EVENT REPORT (LER)
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PAGE G FACILITY asanat til SAN ON0FRE NUCLEAR GENERATING STATION, UNIT 3 o 151 o Io I o 131612 1loFl0l3 TITLE 14e JANUARY 1,1984, RADIOLOGICAL EVACUATION EVENT EVENT DATE (El LER NuesgER tel REPORT DATE (71 OTHER F ACILITIES INVOLVED tel MONTH DAY YEAR YEAR
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NJ.ME TELEPHONE NUMBER J. G. HAYNES, STATION MANAGER 7 11 14 4 19 1217 17 10101 COMPLETE ONE LINE FOR E ACM COMPONENT F AILURE DESCRIBED IN TMla REPORT (131
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On 1/1/84, at approximately 1100, with Unit 3 in Mode 1 at 100% power, precautionary Penetration and Radwaste Buildings' evacuation was initiated when Units 2 and 3 area radiation monitors and plant vent stack monitors alarmed.
Tech Spec required fire watches in areas containing safety related equipment were suspended for approximately two hours as a result of the precautionary evacuation.
This event was reported pursuant to 10 CFR 50.72(b)(2)(vi) and is reported herein pursuant to 10 CFR 50.73(a)(2)(x).
Area radiation monitors and plant vent stack' monitors were alarmed when, during routine draining of the Waste Gas Header line, approximately 110 cubic feet of gas were released from the header. Approximately 84 curies of noble gas (Xe-132) were released.
This did not exceed regulatory or technical specification limits, or the threshold for re-porting pursuant to 10 CFR 50.72(b)(2)(iv).
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NRC Form 3663 U S NUCLEOR REGULOTORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION eaaoveo oMe No 3+oto4 E M PIP ES 8!31 M "I
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- ) vee we San Onofre Nuclear Generating Station Unit 3 o 15 lo lo lo 13 l612 814 0l0 l1 0 10 012 OF 0l3 TEXT (# me spece e reevneg use ear,noner Nec ro,= J66Wsi1171 On January 1,1984, at approximately 1015, with Unit 3 in Mode 1 at 100% power and plant conditions stable, an Operator was dispatched to perform a routine draining operation at three Waste Gas Header drain valve points in the Penetration Building and Radwaste Building.
Periodic draining of the Waste Gas Header (WGH) is necessary to remove excess moisture condensation and carryover liquid from the various inputs to the WGH.
The Radiation Exposure Permit (REP) which covers this activity requires Health Physics to be notified prior to initiation of draining and for an HP Technician to be present.
The Operator did not conduct the activity in accordance with these REP conditions because he did not recognize the potential for release of radioactivity represented by the draining.
The Operator performed the first draining at a drain point at the 9 foot elevation in the Penetration Building and removed approximately 1/2 gallon of water from the WGH.
The liquid was drained into a floor drain.
However, he allowed the draining to continue into the gas-liquid phase for three to five minutes in an attempt to ensure all liquid was drained from this portion of the WGH. Approximately 110 cebic feet of gas were released from the WGH into the Penetration Building.
The plant HVAC system is designed to remove this type of airborne release and to provide a pressure differential such that air will flow from the adjacent buildings, such as the Penetration Building, to the Radwaste Building.
At the conclusion of the first draining, the Operator went to the second drain point at the 27 foot elevation in the Radwaste Building.
He completed the second draining and, having obtained an insignificant 1iquid volume, promptly terminated the draining upon gas-liquid flow. At this time, he was called by the Control Room and directed to stop activities as several area radiation monitors and the plant vent stack monitors were in alarm.
The plant vent stack monitor simultaneously alarms in the Control Room and the State The alarm was activated from 1045 until of California, Of fice of Emergency Services.
1345. Health Physics, upon receipt of the alarms, at approximately 1100 initiated a Also at precautionary evacuation of the Penetration and Radwaste Buildings.
approximately 1100, discussion of the release took place between SCE and the State, which resulted in a 10 CFR 50.72(b)(2)(vi) notification to the NRC at 1532.
As a result of the evacuation, during the period of 1115 to 1250, two continuous fire watches in these areas were suspended.
Since the fire watches were required by Technical Specification 3.3.3.7 for inoperable fire detectors associated with safety related equipment, their evacuation is reported pursuant to 10 CFR 50.73(a)(2)(x).
Subsequent review has determined the evacuation was not necessary to prevent personnel exposures froia exceeding administrative limits.
The post evacuation surveys of personnel from the area identified several individuals who had minor surface contamination of Rb-88, as a result of the noble gas in the bu ilding. The individuals were placed in a holdup area, and within 30 minutes the activity decayed suf ficiently to permit their release without further decontamination.
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INRC Fera 304A U $ NUCLEAft AECULATO3V Commission LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
E kerRES 8'3195
,ACILITY MAME m DOCKET NUMGER 121 LER NUMcER 166
. AGE {31 San Onofre Nuclear Generating Station Unit 3 o ls jo lo jo j3 [ 6;2 8l4 0 ; 0l1 0l0 0l3 oF 0l3 rww ~.
e wcr w.m No individuals other than the Operator received any apparent exposure from the material.
The Operator received an exposure of 34 millirad which is significantly below regulatory limits. Whole body counting of the Operator was negative.
The airborne material is calculated to have been approximately 84 Curies of Xe-133.
The plant HVAC system removed the gas, which was released via the plant vent stack system. The release was sufficient to exceed the plant vent stack alarm setpoint but did not exceed Technical Specification limits (10% of dose limit, 33% of dose rate limit) nor other regulatory limits. This conclusion is based upon calculations using the Offsite Dose Calculation Manual (0DCM), which is the methodology required by the Tech-nical Specifications for evaluating this type of release. The greatest quantity of material was released during the first hour. Based on this amount the ODCM calculation indicates the concentration in unrestricted areas, when averaged over an hour, was 5.7 E-7 microcuries per cubic centimeter (1.9 times the applicable concentration of the limit specified in Appendix B, Table II of 10 CFR 20 in unrestricted areas, when averaged over one hcur ).
The ODCM uses an average meteorology rather than actual meteorological conditions at the time of release.
Calculations using the actual meteorological conditions during the release indicates a concentration of 7.82 E-6 microcuries per cubic centimeter (26 times the applicable concentration of the limit specified in Appendix B, Table II of 10 CFR 20 in unrestricted areas, when The unrestricted area concentration calculated using averaged over one hour).
actual meteorologocal conditions is provided for information only, and any future reports pursuant to 10 CFR 50.72(b)(2)(iv) and 10 CFR 50.73(a)(2)(viii)(A) will be based on calculations using ODCM average meteorology.
The investigation of this incident indicates that there are no reasonable or credible circumstances which could have increased the severity of the incident. No plant systems or components failed as a result of this event.
The cause of this event was that the Operator violated the requirements of the REP.
The Operator did not recognize the potential for a release of material and did not If the HP Technician had been present, the HP believe HP coverage was mandatory.
instruments would have identified the radiological implications of the three to five Corrective actions include:
the Operatc< received disciplinary minutes of venting.
action for violating the REP; and an llP Technician will be stationed in the Radwaste Building when determined by the Health Physics or Operations Manager to be necessary or desirable to facilitate interaction between HP and Operations.
A Secondary contributor to this event was the fact that draining of condensate from the WGH was not proceduralized since it was considered to be within the skill level of an Revisions to existing procedures will be made to incorporate this activity.
Operator.
The sources of the water in the WGH are under investigation.
A test program is being Based on the results, conducted to identify which systems have carryover into the WGH.
Design Change Packages (DCP's) may be prepared to accomplish automatic draining of the WGH.
A review of the plant vent stack alarm operation has resulted in an increase in the ODCM-based alarm setpoint to a more appropriate value, and a noise suppression circuit has been added to eliminate spurious spikes.
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.e Southern California Edison Company gE SAN ONOFRE NUCLE AR CZNER A TING ST ATION P.O. Box 128 S AN C L EMEN T E. C ALIFORNI A 92672 J. G. H AY N E S January 31, 1984 O '. S. Nuclear Regulatory Commission Document Control Desk-Washington, D.
C.
20555
Subject:
Docket No. 50-362 30-Day Report Licensee Event Report No.84-001 San Onofre Nuclear Generating Station, Unit 3 Pursuant to 10 CFR 50.73.a.2(x), this submittal provides the required 30-day writtea Licensee Event Report (LER) for an occurrence involving the precautionary evacuation of personnel due to an inadvertent release of radioactive material.
The material released did not exceed regulatory or Technical Specification limite.
The health and safety of plant personnel or the public were not affected by this event.
If you require any additional information, please so advise.
Sincerely, y+
Enclosure:
LER No.84-001 cc:
A. E. Chaffee (USNRC Resident Inspector, Units 1, 2 and 3)
J. P. Stewart (USNRC Resident Inspector, Units 2 and 3)
J.
B. Martin (Regional Administrator, NRC Region V)
U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Institute of Nuclear Power Operations (INPO) l E E 2 3-
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| 05000362/LER-1984-001, :on 840101,precautionary Penetration & Radwaste Bldgs Evacuation Initiated When Units 2 & 3 Area Radiation Monitors & Plant Vent Stack Monitors Alarmed.Caused by Routine Draining of Waste Gas Header Line |
- on 840101,precautionary Penetration & Radwaste Bldgs Evacuation Initiated When Units 2 & 3 Area Radiation Monitors & Plant Vent Stack Monitors Alarmed.Caused by Routine Draining of Waste Gas Header Line
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii)(A) | | 05000361/LER-1984-001, :on 840111,preparation of Fire Hazard Analysis & Review of Fire Protection Surveillance Results Identified Deficiencies in Fire Protection Program.Review in Progress. Complete Rept Will Be Submitted by 840228 |
- on 840111,preparation of Fire Hazard Analysis & Review of Fire Protection Surveillance Results Identified Deficiencies in Fire Protection Program.Review in Progress. Complete Rept Will Be Submitted by 840228
| | | 05000361/LER-1984-001-01, :on 840111,preparation of Updated Fire Hazards Analysis Resulted in 91 Nonconformance Repts (NCR) Re Fire Protection Program Deficiencies.Compensatory Measures Established.Ncr Dispositions Planned |
- on 840111,preparation of Updated Fire Hazards Analysis Resulted in 91 Nonconformance Repts (NCR) Re Fire Protection Program Deficiencies.Compensatory Measures Established.Ncr Dispositions Planned
| | | 05000362/LER-1984-002, :on 840107,penetration Bldg Airborne Iodine of Noble Gas Concentrations Increased Above Precautionary Level.Cause Under Investigation.Engineering Evaluation Will Determine Corrective Actions |
- on 840107,penetration Bldg Airborne Iodine of Noble Gas Concentrations Increased Above Precautionary Level.Cause Under Investigation.Engineering Evaluation Will Determine Corrective Actions
| 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-003, :on 840107,while in Mode 3 at Zero Power,During Planned Reactor Shutdown,Control Element Assembly (CEA) 64 Slipped 30 Inches.Caused by Sluggish Operation of CEA Drive Mechanism.Vendor Requested to Review Event |
- on 840107,while in Mode 3 at Zero Power,During Planned Reactor Shutdown,Control Element Assembly (CEA) 64 Slipped 30 Inches.Caused by Sluggish Operation of CEA Drive Mechanism.Vendor Requested to Review Event
| | | 05000361/LER-1984-003-01, :on 840122,containment Purge Isolation Sys Actuated When Gaseous Activity Alarm Setpoint Reached Train a Containment Airborne Monitor 2RT7804.Caused by Increase in Containment Background Radiation |
- on 840122,containment Purge Isolation Sys Actuated When Gaseous Activity Alarm Setpoint Reached Train a Containment Airborne Monitor 2RT7804.Caused by Increase in Containment Background Radiation
| | | 05000361/LER-1984-004, :on 840116,train a Containment Purge Isolation Sys Spuriously Actuated.Caused by Subgroup Relay Actuation Voltage Transient on ESF Bus.No Corrective Action Planned as Minor Transients Expected in Test |
- on 840116,train a Containment Purge Isolation Sys Spuriously Actuated.Caused by Subgroup Relay Actuation Voltage Transient on ESF Bus.No Corrective Action Planned as Minor Transients Expected in Test
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000362/LER-1984-004-01, :on 840222,three Safety Injection Pumps Started & Injected 150 Gallons of Water Into Rcs.Caused by Dirty Contacts on Relay Hold Pushbutton.Contacts Cleaned |
- on 840222,three Safety Injection Pumps Started & Injected 150 Gallons of Water Into Rcs.Caused by Dirty Contacts on Relay Hold Pushbutton.Contacts Cleaned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-005, :on 840106,following Reactor Trip for Testing, RCS Sample Analysis Indicated That RCS Specific Activity Exceeded 1.0 Uci/G Dose Equivalent.Cause Indicative of Iodine Spiking Following Power Change |
- on 840106,following Reactor Trip for Testing, RCS Sample Analysis Indicated That RCS Specific Activity Exceeded 1.0 Uci/G Dose Equivalent.Cause Indicative of Iodine Spiking Following Power Change
| | | 05000361/LER-1984-005-01, :on 840127,while in Mode 5,w/purge/vent Stack wide-range Monitor 3RT-7865 & Flow Rate Monitor Out of Svc for Installation of Noise Suppression Circuit,Flow Rate Estimates Not Performed as Required |
- on 840127,while in Mode 5,w/purge/vent Stack wide-range Monitor 3RT-7865 & Flow Rate Monitor Out of Svc for Installation of Noise Suppression Circuit,Flow Rate Estimates Not Performed as Required
| 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-006, :on 840103,spurious Toxic Gas Isolation Sys Actuations Occurred.Caused by Toxic Gas Isolation Sys Setpoint Set at Threshold Level of Detection.Tech Specs Revised to Raise Setpoint Requirements |
- on 840103,spurious Toxic Gas Isolation Sys Actuations Occurred.Caused by Toxic Gas Isolation Sys Setpoint Set at Threshold Level of Detection.Tech Specs Revised to Raise Setpoint Requirements
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000362/LER-1984-006-01, :on 840226,during Surveillance,Reactor Trip Breaker 8 Undervoltage Device Did Not Actuate.Caused by Metal Filings Between Two Terminals of Control Room Pushbutton.No Corrective Action Planned |
- on 840226,during Surveillance,Reactor Trip Breaker 8 Undervoltage Device Did Not Actuate.Caused by Metal Filings Between Two Terminals of Control Room Pushbutton.No Corrective Action Planned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-007, :on 840203 & 04,Train a & B Main Steam Isolation Sys Spuriously Actuated on Low Pressure Signal from E-088.Caused by Voltage Fluctuation Resulting from Electrical Realignments,Testing & Maint |
- on 840203 & 04,Train a & B Main Steam Isolation Sys Spuriously Actuated on Low Pressure Signal from E-088.Caused by Voltage Fluctuation Resulting from Electrical Realignments,Testing & Maint
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000362/LER-1984-007-01, :on 840305,spurious Reactor Protection Sys Trip Occurred.Cause Undetermined.No Restrictions Placed on Plant Operations as Result of Trip |
- on 840305,spurious Reactor Protection Sys Trip Occurred.Cause Undetermined.No Restrictions Placed on Plant Operations as Result of Trip
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-008, :on 840310,operators Received Indications of Possible Saltwater Leak in One Main Condenser Quadrant. Caused by Water in Air Removal Piping.Drain Lines Cleaned |
- on 840310,operators Received Indications of Possible Saltwater Leak in One Main Condenser Quadrant. Caused by Water in Air Removal Piping.Drain Lines Cleaned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-008-02, :on 840211,inadvertent Entry Into Mode 3 Occurred.Caused by Failure of Plant Monitoring Sys (PMS) Due to Incorrect RCS Temp Display.Pms Display Repaired & Returned to Svc |
- on 840211,inadvertent Entry Into Mode 3 Occurred.Caused by Failure of Plant Monitoring Sys (PMS) Due to Incorrect RCS Temp Display.Pms Display Repaired & Returned to Svc
| 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-009, :on 840214,analysis of Startup Test Data Established Calculated Thermal Power Calculated by Core Protection Calculators May Become Decalibr Relative to Secondary Calorimetric Power.Procedure Changed |
- on 840214,analysis of Startup Test Data Established Calculated Thermal Power Calculated by Core Protection Calculators May Become Decalibr Relative to Secondary Calorimetric Power.Procedure Changed
| | | 05000362/LER-1984-009, :on 840317,during Surveillance of Sys Alignment Status,Manual Isolation Valves Found Closed,Rendering Both Trains of Containment Spray Sys Inoperable.Procedure Modified to Clarify Valve Lineup Requirements |
- on 840317,during Surveillance of Sys Alignment Status,Manual Isolation Valves Found Closed,Rendering Both Trains of Containment Spray Sys Inoperable.Procedure Modified to Clarify Valve Lineup Requirements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-009-01, Revised LER 84-009-01:on 840214,analysis of Startup Test Data for Units 2 & 3 Established That Calculated Thermal Power May Become Decalibr Relative to Secondary Calometric Power.Procedure S023-5-1 Revised | Revised LER 84-009-01:on 840214,analysis of Startup Test Data for Units 2 & 3 Established That Calculated Thermal Power May Become Decalibr Relative to Secondary Calometric Power.Procedure S023-5-1 Revised | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(1) | | 05000206/LER-1984-009-02, :on 841205,load Sequencer 31-day Surveillance Delinquent.Caused by Personnel Oversight.Personnel Counseled & Performance of Tech Spec Required Surveillances in Specified Manner Reemphasized |
- on 841205,load Sequencer 31-day Surveillance Delinquent.Caused by Personnel Oversight.Personnel Counseled & Performance of Tech Spec Required Surveillances in Specified Manner Reemphasized
| 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-009-01, Forwards LER 84-009-01 | Forwards LER 84-009-01 | | | 05000206/LER-1984-010, :on 840930,during Mode 5 Outage,Two of Three Boric Acid Flow Paths Inoperable.Caused by Accumulated Gas from Vol Control Tank Due to Leak in Valve CV406B.Valve Diaphragms Replaced.Procedures Revised |
- on 840930,during Mode 5 Outage,Two of Three Boric Acid Flow Paths Inoperable.Caused by Accumulated Gas from Vol Control Tank Due to Leak in Valve CV406B.Valve Diaphragms Replaced.Procedures Revised
| | | 05000361/LER-1984-010-02, :on 840223,reactor Power Surge Occurred Due to Partial Loss of Extraction Steam Feedwater Heating.Caused by Spurious Cycle of First Point Level Controller Resulting in High Levels in Point Heaters |
- on 840223,reactor Power Surge Occurred Due to Partial Loss of Extraction Steam Feedwater Heating.Caused by Spurious Cycle of First Point Level Controller Resulting in High Levels in Point Heaters
| | | 05000362/LER-1984-010, :on 840424,train a Containment Purge Isolation Sys Spuriously Actuated by Electrical Noise Spikes from Containment Area Radiation Monitor 3RT-7804.Cause Under Investigation |
- on 840424,train a Containment Purge Isolation Sys Spuriously Actuated by Electrical Noise Spikes from Containment Area Radiation Monitor 3RT-7804.Cause Under Investigation
| | | 05000361/LER-1984-011, :on 840225,containment Purge Isolation Sys Actuated When Containment Airborne Monitor 2RE-7804 Gaseous Channel C Failed.Caused by Water in Gaseous Detector Cell, Short Circuiting pre-amp.Water Removed |
- on 840225,containment Purge Isolation Sys Actuated When Containment Airborne Monitor 2RE-7804 Gaseous Channel C Failed.Caused by Water in Gaseous Detector Cell, Short Circuiting pre-amp.Water Removed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000362/LER-1984-011-01, :on 840227,during Investigation of Reactor Trip Breaker Pushbutton Event,One Set of Leads in Each of Four Plant Protection Sys Bays Found Disconnected.Caused by Leads Disconnected During Earlier Surveillance |
- on 840227,during Investigation of Reactor Trip Breaker Pushbutton Event,One Set of Leads in Each of Four Plant Protection Sys Bays Found Disconnected.Caused by Leads Disconnected During Earlier Surveillance
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-012, :on 840301,spurious Toxic Gas Isolation Sys (Tgis) Actuation Occurred.Caused by Unnecessary Conservatisms in Tgis Setpoint.Basis for Setpoint Will Be Reanalyzed & Tech Specs Amended |
- on 840301,spurious Toxic Gas Isolation Sys (Tgis) Actuation Occurred.Caused by Unnecessary Conservatisms in Tgis Setpoint.Basis for Setpoint Will Be Reanalyzed & Tech Specs Amended
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000362/LER-1984-012-01, :on 840330,MSIVs 3HV8204 & 5 Failed to Close within Required 5 S.Caused by Cylinder Nitrogen Pressure Above Min Specified Limit W/Valves Open.Tech Spec Change Will Be Submitted to Increase Closure Time |
- on 840330,MSIVs 3HV8204 & 5 Failed to Close within Required 5 S.Caused by Cylinder Nitrogen Pressure Above Min Specified Limit W/Valves Open.Tech Spec Change Will Be Submitted to Increase Closure Time
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-013, :on 840305,containment Pressure Exceeded Tech Spec Limits.Caused by Misinterpretation of Venting Procedure.Operators Interpreted Procedure to Require 2 H Venting.Operators Counseled Re Procedure |
- on 840305,containment Pressure Exceeded Tech Spec Limits.Caused by Misinterpretation of Venting Procedure.Operators Interpreted Procedure to Require 2 H Venting.Operators Counseled Re Procedure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-013-01, :on 840330 & 0401,following Reactor Shutdown for Maint,Rcs Exceeded 1.0 Uci/G Dose Equivalent I-131. Caused by Iodine Spiking Following Power Change.Purification Flow Increased & RCS Activity Reduced |
- on 840330 & 0401,following Reactor Shutdown for Maint,Rcs Exceeded 1.0 Uci/G Dose Equivalent I-131. Caused by Iodine Spiking Following Power Change.Purification Flow Increased & RCS Activity Reduced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000362/LER-1984-013, :on 840330 & 0401,following Reactor Shutdown for Maint,Rcs Sample Analysis Indicated That RCS Specific Activity Exceeded 1.0 Uci/G Dose Equivalent I-131.Cause Indicative of Iodine Spiking Following Power Change |
- on 840330 & 0401,following Reactor Shutdown for Maint,Rcs Sample Analysis Indicated That RCS Specific Activity Exceeded 1.0 Uci/G Dose Equivalent I-131.Cause Indicative of Iodine Spiking Following Power Change
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000361/LER-1984-015, :on 840306,fire Program Discrepancies Found During Preparation of Fire Hazard Analysis (FHA) & Review of IE Info Notice 84-09.Compensatory Measures & Rev to FHA Implemented |
- on 840306,fire Program Discrepancies Found During Preparation of Fire Hazard Analysis (FHA) & Review of IE Info Notice 84-09.Compensatory Measures & Rev to FHA Implemented
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-015-01, :on 840427,0505 & 07,analysis of RCS Sample Indicated That Specific Activity Exceeded 1.0 Uci/G Dose Equivalent I-131.Cause Not Stated.Personnel Instructed to Perform Sampling within Required 4 H Period |
- on 840427,0505 & 07,analysis of RCS Sample Indicated That Specific Activity Exceeded 1.0 Uci/G Dose Equivalent I-131.Cause Not Stated.Personnel Instructed to Perform Sampling within Required 4 H Period
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000362/LER-1984-016-01, :on 840428,undervoltage (UV) Trip Device for Reactor Trip Breaker 256A4002-656-29 Exhibited Unacceptable Response Time.Following Maint,Breaker Yielded Acceptable UV Response Time.Breaker Returned to Svc |
- on 840428,undervoltage (UV) Trip Device for Reactor Trip Breaker 256A4002-656-29 Exhibited Unacceptable Response Time.Following Maint,Breaker Yielded Acceptable UV Response Time.Breaker Returned to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000361/LER-1984-016, :on 840309,technician Inadvertently Actuated Safety Injection,Containment Cooling & Containment Spray Activation Sys.Caused by Technician Error.Procedural Changes Implemented |
- on 840309,technician Inadvertently Actuated Safety Injection,Containment Cooling & Containment Spray Activation Sys.Caused by Technician Error.Procedural Changes Implemented
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-017-01, :on 840505 & 08,reactor Trip Occurred on High Steam Generator Water Level.Caused by Overfeeding Steam Generators W/Feedwater Control Sys in Manual Control.Design Changes Under Consideration |
- on 840505 & 08,reactor Trip Occurred on High Steam Generator Water Level.Caused by Overfeeding Steam Generators W/Feedwater Control Sys in Manual Control.Design Changes Under Consideration
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000361/LER-1984-017, :on 840321,shutdown Cooling HX Flow Control Valve 2HV9316 Discovered Locked Fully Open.Caused by Disengaged Handwheel Clutch.Surveillance Position Revised to Verify Handwheel Engaged |
- on 840321,shutdown Cooling HX Flow Control Valve 2HV9316 Discovered Locked Fully Open.Caused by Disengaged Handwheel Clutch.Surveillance Position Revised to Verify Handwheel Engaged
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-018-01, :on 840525,during Surveillance,Undervoltage Trip Device for Reactor Trip Breaker,Serial 256A4002-656-29, Exhibited Procedurally Unacceptable Response Time.Breaker Replaced W/Spare |
- on 840525,during Surveillance,Undervoltage Trip Device for Reactor Trip Breaker,Serial 256A4002-656-29, Exhibited Procedurally Unacceptable Response Time.Breaker Replaced W/Spare
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000361/LER-1984-018, :on 840324,remaining Control Room Isolation Sys Radiation Monitor 2/3RT-7825 Declared Inoperable.Caused by Low Flow Alarm Due to Dirty Filter.Filter Changed & Monitor Returned to Svc |
- on 840324,remaining Control Room Isolation Sys Radiation Monitor 2/3RT-7825 Declared Inoperable.Caused by Low Flow Alarm Due to Dirty Filter.Filter Changed & Monitor Returned to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | | 05000361/LER-1984-019, :on 840324,while at 100% Power,False Position Indication for Control Element Assembly (CEA) 20 on CEA Calculator (Ceac) 1 Resulted in Penalty Factors,Causing Reactor Trip.Specific Cause Undetermined |
- on 840324,while at 100% Power,False Position Indication for Control Element Assembly (CEA) 20 on CEA Calculator (Ceac) 1 Resulted in Penalty Factors,Causing Reactor Trip.Specific Cause Undetermined
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000362/LER-1984-019-01, :on 840505,post-maint Testing Not Performed Following Packing Adjustment to Reduce Leakage on Containment Isolation Valves 3HV9205 & 3HV9212.Caused by Personnel Error.Operations Personnel Briefed |
- on 840505,post-maint Testing Not Performed Following Packing Adjustment to Reduce Leakage on Containment Isolation Valves 3HV9205 & 3HV9212.Caused by Personnel Error.Operations Personnel Briefed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-020, :on 840326,w/unit in Mode 2 at 2% Power,Reactor Trip Occurred on High Steam Generator Level.Caused by Overfeeding Steam Generators During Manual Operation of Feedwater Control Sys |
- on 840326,w/unit in Mode 2 at 2% Power,Reactor Trip Occurred on High Steam Generator Level.Caused by Overfeeding Steam Generators During Manual Operation of Feedwater Control Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-020, :on 840527,8 H Grab Sample Due at 0800 Not Taken Until 0945.Low-range Flow at Sample Conditioning Skid Diverted from Filter a to Filter B,Causing Blown Fuse. Alternate Flow Path Established |
- on 840527,8 H Grab Sample Due at 0800 Not Taken Until 0945.Low-range Flow at Sample Conditioning Skid Diverted from Filter a to Filter B,Causing Blown Fuse. Alternate Flow Path Established
| 10 CFR 50.73(a)(2)(x) | | 05000362/LER-1984-020-01, :on 840527,grab Sample Not Taken Per 8 H Requirement.Caused by Sample Pump Isolation.Corrective Action Will Be Reported in LER Rev by 840801 |
- on 840527,grab Sample Not Taken Per 8 H Requirement.Caused by Sample Pump Isolation.Corrective Action Will Be Reported in LER Rev by 840801
| 10 CFR 50.73(a)(2)(1) | | 05000361/LER-1984-021, :on 840330,0405,07,10-12,15,19,22 & 23. Spurious Toxic Gas Isolation Sys Actuations Occurred.Caused by Conservative Setpoints Which Contained Unnecessary Conservatisms.Setpoints Will Be Reanalyzed |
- on 840330,0405,07,10-12,15,19,22 & 23. Spurious Toxic Gas Isolation Sys Actuations Occurred.Caused by Conservative Setpoints Which Contained Unnecessary Conservatisms.Setpoints Will Be Reanalyzed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000362/LER-1984-021-01, :on 840602,safety Relief Valve 3PSV-0245 on Nuclear Sample Sys Actuated.Caused by Setpoint on Valve Set Unnecessarily Low.Setpoint Raised & Valve Returned to Svc on 840606 |
- on 840602,safety Relief Valve 3PSV-0245 on Nuclear Sample Sys Actuated.Caused by Setpoint on Valve Set Unnecessarily Low.Setpoint Raised & Valve Returned to Svc on 840606
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000362/LER-1984-022-01, :on 840601,failure in Turbine Control Sys Caused High Pressure Turbine Stop Valves to Close,Resulting in Loss of Load Reactor Trip.Cause Undetermined.Module Replaced |
- on 840601,failure in Turbine Control Sys Caused High Pressure Turbine Stop Valves to Close,Resulting in Loss of Load Reactor Trip.Cause Undetermined.Module Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000361/LER-1984-022, :on 840330 & 0410,control Room Isolation Sys Train Spuriously Actuated from Spike on Control Room Airborne Radiation Monitor.Caused by Spurious Electrical Spikes.No Corrective Action Planned |
- on 840330 & 0410,control Room Isolation Sys Train Spuriously Actuated from Spike on Control Room Airborne Radiation Monitor.Caused by Spurious Electrical Spikes.No Corrective Action Planned
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000361/LER-1984-023, :on 840524,spurious Actuation of Control Room Isolation Sys Occurred Because of Noise Spike on Control Room Airborne Radiation Monitor.Monitor Detector Replaced & Preamplifier Properly Grounded |
- on 840524,spurious Actuation of Control Room Isolation Sys Occurred Because of Noise Spike on Control Room Airborne Radiation Monitor.Monitor Detector Replaced & Preamplifier Properly Grounded
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000362/LER-1984-023-01, :on 840601 & 11,during Turbine Overspeed Protection Test,Reactor Trip Occurred Involving RCS Specific Activity.Caused by Iodine Spiking.Primary Coolant Activity Will Be Monitored & Evaluated |
- on 840601 & 11,during Turbine Overspeed Protection Test,Reactor Trip Occurred Involving RCS Specific Activity.Caused by Iodine Spiking.Primary Coolant Activity Will Be Monitored & Evaluated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
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