05000352/FIN-2011004-03
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Finding | |
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Title | Test Equipment Interference Resulting in Reactor Scram |
Description | A Green, self-revealing NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, occurred when Exelon did not adequately assess the potential impacts of test equipment on turbine trip circuitry. This resulted in an automatic reactor scram of Unit 1 when the main turbine high reactor water level trip relay inadvertently energized during a surveillance test on June 3, 2011. This test is a quarterly surveillance, designed to verify proper operation of the Digital Feed Water Level Control System (DFWLCS) which initiates a turbine trip on high reactor level. The DFWLCS has a 1 out of 2 twice logic to energize the trip relay, so each channel is tested separately to eliminate the possibility of inadvertent actuation. As an additional precaution, the surveillance procedure contains steps for the technician to verify the other channels are free of closed trip contacts prior to beginning the test. Exelon used a Simpson 260 Volt/Ohm Meter (VOM) to perform this verification by demonstrating a nominal voltage difference between each side of the contact and station ground. During this verification step, Exelon inadvertently established a direct current loop from station ground, to the floating battery ground from the 125V power supply, to the trip circuit. This completed the circuit, energized the main turbine high reactor water level trip relay, which tripped the main turbine and caused the reactor to scram. Exelon revised the test procedure to change the requirements for test instrumentation to prevent this from recurring and entered the issue into the corrective action program as IR 1224283. The inspectors determined that the performance deficiency was more than minor in accordance with IMC 0612, Appendix B, Issue Screening, because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and affected the objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during power operation. Specifically, by not considering the impact of maintenance and test equipment (M&TE) during multiple revisions of the surveillance procedure, Exelon failed to recognize a vulnerability which could lead to a plant transient. In accordance with IMC 0609, Attachment 4, Phase 1 - Initial Screen and Characterization of Findings, the finding was determined to be of very low safety significance (Green) because the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. The inspectors determined that this performance deficiency did not reflect current performance, as the last revision to the surveillance procedure that affected M&TE requirements was greater than three years ago. As a result, the inspectors did not assign a cross-cutting aspect to this finding. |
Site: | Limerick ![]() |
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Report | IR 05000352/2011004 Section 4OA3 |
Date counted | Sep 30, 2011 (2011Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | K Mangan N Sieller S Hammann T Moslak A Rosebrook A Ziedonis D Roberts E Dipaolo E Miller J Ambrosini J Kulp J Lilliendahl J Nicholson |
INPO aspect | |
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Finding - Limerick - IR 05000352/2011004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Limerick) @ 2011Q3
Self-Identified List (Limerick)
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