LER-1980-003, Forwards LER 80-003/01T-0 |
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"'rRIOA PO'VJER d LIGHTCOMPAIIY February 6, 1981 PRN-LI 64 Mr, James P. O'Reilly, Director, Rea'ion II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 101 Marietta Street, Suite 3100 Atlanta; Georgia 30303
Dear Mr. O'Rei lly:
REPORTABLE OCCURRENCE 336-81-03 ST.
LUCIE UNIT 1
DATE OF OCCURRENCE:
JANUARY 23, 1981 TECHNICAL.SPECIFICATION 6.9.1.8 MASONRY WALLS The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide prompt notification of the subject occurrences Very truly yours, D. Schmidt Vice President Power Resources PLP/mrs Attachment-cc:
Director, Office of Inspection and Enforcement (40)
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REPORTABLE OCCURRENCE 335-81-03 LICENSEE EVENT REPORT PAGE TWO ADDITIONAL EVENT DESCRIPTION During the early stages of the Bulletin 80-11 evaluation (September 1980) plant walls were inspected to verify that they were built as designed; 14 walls were found missing clip angles which tie them to surrounding structural members.
Although the seismic evaluation had not been started, it was considered prudent to install the missing angles.
13 of the walls were completed by 12/28/80.
The 14th wall, forming one side of a cubicle, has sufficient restraint outside the cubicle to preclude its falling outward.
There is no safety related equipment inside this cubicle.
Since the inner side of this wall is in an inaccessible high radiation area during operation, repair will be completed during the 1981 refueling outage.
These walls could not be shown to meet the Bulletin 80-11 reevaluation criteria without the angles so this is considered reportable.
On 1/23/81 our engineering department xeported 3 walls which required strengthening.
These 3 walls had no safety related equipment mounted on or supported by them but there is safety related equipment adjacent.
Due to the nature and inherent strength of this equipment (metal enclosed seismic Class 1
cable trays and metal seismic Class 1 vent ducting), its location relative to.
the walls (passing through near the top of the walls or running vertically adjacent to the wall) and the fact that the probable failure mode (if any) was cracking or distortion rather than collapse, it was believed in our best engineering judgement that these 3 walls would not render any safety related equipment inoperable if there were to be a seismic event during the interim period required for reinforcement of the walls.
Oux schedule called for all 3 walls to be completed by midnight Friday 1/30/81.
Due to various unforeseen difficulties the last wall was actually completed at about 5
PuM Saturday l/31 /81.
On Friday, 1/30/81, it was reported that an additional 19 walls required strengthened clip angles.
It was also reported that other walls were in the last stages of analysis with final results in doubt.
The engineering department worked to apply new detailed analysis techniques and to evaluate the safety significance of any walls found not to meet the re-evaluation criteria.
Of the 19 identified'n 1/30/81 Three were confirmed to need strengthened clip angles on 1/31/81 and 2/1/81.
Two were reinforced by 6 P.H.
Sunday (2/1/81) which was before the safety significance evaluation was completed.
The third wall whose (potential) collapse was found not to have any adverse safety effects was completed Tuesday (2/3/81).
The other 16 of the 19 did not require any modifications.
Of the remaining plant walls, some were found which would withstand design seismic events, but which required corrective action to restore the safety margin of Bulletin 79-02 for anchor bolts.
Since these walls have been shown not to fail and since some are inaccessible high radiation areas at power we have scheduled to complete corrective action by the end of our Fall; 1981 refueling outage.
REPORTABLE OCCURRENCE 335-81 "03 LICENSEE EVENT REPORT PAGE 3
Finally during review of the entire wall program three wall sections over doorways were identified (2/4/81) which required strengthened clip angles.
One wall had adjacent safety related metal seismic class 1 cable trays and conduit.
Oux best engineering
)udgment was that collaspe of this three foot wide section would not render any safety related equipment inoperable.
This wall was modified by 4
PM 2/5/81.
The other two had been conservatively designated safety related in error as there is no mounted or adjacent safety related equipment.
These walls will be modified,
- however, by the end of the 1981 refueling outage.
The following is a summary of walls corrected to date.
Details of the re-evaluation and corrective actions taken will be reported in our final response to IE Bulletin 80-11.
1.
Walls with missing clip angles 13 have been modified see previous discussion (identified Sept.
1980) 14 2.
Walls requiring reinforcement completed by 5'/31/81 (identified 1/23/81) 3.
Walls requiring clip angle reinforcement completed by 2/3/81 (3 of the 19 discussed on 1/30/81) 4.
Walls requiring adding clip angles (angles not required per original design) 1 done by 2/3/81, 2 not safety related (identified 2/5/81) 2 of these conservatively designated safety related in error.
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| 05000335/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000335/LER-1980-001-03, /03L-0:on 800102,during Surveillance Testing of IA Diesel Generator,Fuel Transfer Pump Failed to Start. Failure Caused by Dirty Starter Contactor.Pump Cleaned & Returned to Svc | /03L-0:on 800102,during Surveillance Testing of IA Diesel Generator,Fuel Transfer Pump Failed to Start. Failure Caused by Dirty Starter Contactor.Pump Cleaned & Returned to Svc | | | 05000335/LER-1980-002-03, /03L-0:on 800104,during Normal Operations,Control Element Assembly Dropped to Full Insertion,Causing Tq to Exceed Core Limits.Caused by Failure of 15-volt Power Supply in Coil Power Programmer.Power Supply Replaced | /03L-0:on 800104,during Normal Operations,Control Element Assembly Dropped to Full Insertion,Causing Tq to Exceed Core Limits.Caused by Failure of 15-volt Power Supply in Coil Power Programmer.Power Supply Replaced | | | 05000335/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000335/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000335/LER-1980-003-03, During Normal Operations, Control Element Assembly 30 Reed Switch Position Indication Channel Failed.Cause Is Unknown.Channel Repaired & Returned to Svc | During Normal Operations, Control Element Assembly 30 Reed Switch Position Indication Channel Failed.Cause Is Unknown.Channel Repaired & Returned to Svc | | | 05000335/LER-1980-004-01, /01T-0:on 800124,operating at 100% Power,Feeder Breaker from Startup Transformer 1B to 4160-volt Essential Bus B Found Open.Caused by Improper Label on Switch.Label Changed & Personnel Informed of Event | /01T-0:on 800124,operating at 100% Power,Feeder Breaker from Startup Transformer 1B to 4160-volt Essential Bus B Found Open.Caused by Improper Label on Switch.Label Changed & Personnel Informed of Event | | | 05000335/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000335/LER-1980-005-03, /03L-0:on 800130 & Again on 800131,while Operating at 100% Power,Control Element Assembly Dropped to Bottom of Core.Caused by Loose Lead in 15-volt Power Supply.Control Element Assembly Returned to Normal Position | /03L-0:on 800130 & Again on 800131,while Operating at 100% Power,Control Element Assembly Dropped to Bottom of Core.Caused by Loose Lead in 15-volt Power Supply.Control Element Assembly Returned to Normal Position | | | 05000335/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000335/LER-1980-006-03, /03L-0:on 800202,during Periodic Exercise of Containment Isolation Valves,Normally Closed Valves V-5201 & V-5204 Could Not Be Shut.Caused by Crystalline Boric Acid Deposits Caked on Valves.Valves Freed & Exercised | /03L-0:on 800202,during Periodic Exercise of Containment Isolation Valves,Normally Closed Valves V-5201 & V-5204 Could Not Be Shut.Caused by Crystalline Boric Acid Deposits Caked on Valves.Valves Freed & Exercised | | | 05000335/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000335/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000335/LER-1980-007-03, /03L-0:on 800204,during Periodic Control Element Assembly (CEA) Surveillance Testing,Cea 19 Dropped to Full Insertion While Being Withdrawn.Caused by Failed Timer Module in Coil Power Programmer.Timer Module Replaced | /03L-0:on 800204,during Periodic Control Element Assembly (CEA) Surveillance Testing,Cea 19 Dropped to Full Insertion While Being Withdrawn.Caused by Failed Timer Module in Coil Power Programmer.Timer Module Replaced | | | 05000335/LER-1980-008, Forwards Revised LER 80-008/03L-1 | Forwards Revised LER 80-008/03L-1 | | | 05000335/LER-1980-008-03, Sample Valves for Tanks 1A1,1A2,1B1 & 1B2 Had Been Mislabeled.Caused by Drawing Error.Working Diagrams Revised & Piping & Labeling Corrected | Sample Valves for Tanks 1A1,1A2,1B1 & 1B2 Had Been Mislabeled.Caused by Drawing Error.Working Diagrams Revised & Piping & Labeling Corrected | | | 05000335/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000335/LER-1980-009-03, /03L-0:on 800208,during Normal Operation,Rcs Leakage Was Determined to Be 4.38 Gpm Unidentified Leakage. Caused by Relief Valve Rv 2115 on Vol Control Tank Oscillating Open & Closed W/Charging Pump Pulsations | /03L-0:on 800208,during Normal Operation,Rcs Leakage Was Determined to Be 4.38 Gpm Unidentified Leakage. Caused by Relief Valve Rv 2115 on Vol Control Tank Oscillating Open & Closed W/Charging Pump Pulsations | | | 05000335/LER-1980-010-03, /03L-0:on 800217,during 100% Power Operation, Control Element Assembly 65 Dropped to Full Insertion When Selected to Manual Insertion for A.S.I. Damping.Cause Undetermined.Assembly Operated Properly in Normal Position | /03L-0:on 800217,during 100% Power Operation, Control Element Assembly 65 Dropped to Full Insertion When Selected to Manual Insertion for A.S.I. Damping.Cause Undetermined.Assembly Operated Properly in Normal Position | | | 05000335/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000335/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000335/LER-1980-011-03, /03L-0:on 800219,during Normal Operation,Refueling Water Tank Engineered Safety Feature Actuation Sys Channel D Drifted Below Low Level Setpoint.Caused by Erroneous Level Signal in Level Transmitter | /03L-0:on 800219,during Normal Operation,Refueling Water Tank Engineered Safety Feature Actuation Sys Channel D Drifted Below Low Level Setpoint.Caused by Erroneous Level Signal in Level Transmitter | | | 05000335/LER-1980-012, Forwards Updated LER 80-012/03X-1 | Forwards Updated LER 80-012/03X-1 | | | 05000335/LER-1980-012-03, Diesel Generator B Failed to Reach Rated Speed During Operational Check.Caused by Sticking Injector Linkages.All Critical Linkage Bearings Received Adequate Lubrication | Diesel Generator B Failed to Reach Rated Speed During Operational Check.Caused by Sticking Injector Linkages.All Critical Linkage Bearings Received Adequate Lubrication | | | 05000335/LER-1980-013-09, /09T-0:on 800317,during Trouble Shooting Re Inability of a Diesel Generator to Accept Full Design Load, Hot Excitor Leads to Generator Field Found W/Burnt Insulation.Caused by Error in Ae Installation Drawings | /09T-0:on 800317,during Trouble Shooting Re Inability of a Diesel Generator to Accept Full Design Load, Hot Excitor Leads to Generator Field Found W/Burnt Insulation.Caused by Error in Ae Installation Drawings | | | 05000335/LER-1980-013, Forwards LER 80-013/09T-0 | Forwards LER 80-013/09T-0 | | | 05000335/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000335/LER-1980-014-03, /03L-0: on 800324,w/reactor Shutdown for refueling,6B2 Heater for Sbvs Discovered to Be Inoperable. Caused by Defective Thermocouple Amplifier (Fenwal Model 543) in 6B2 Heater Control Circuitry.Amplifier Replaced | /03L-0: on 800324,w/reactor Shutdown for refueling,6B2 Heater for Sbvs Discovered to Be Inoperable. Caused by Defective Thermocouple Amplifier (Fenwal Model 543) in 6B2 Heater Control Circuitry.Amplifier Replaced | | | 05000335/LER-1980-015-03, During Shutdown,Diesel Generator Loading Timers Found Out of Tolerance & Containment & Reactor Cavity Cooling Fans Failed to Start. Caused by Normal Setpoint Drift.Fans Retested | During Shutdown,Diesel Generator Loading Timers Found Out of Tolerance & Containment & Reactor Cavity Cooling Fans Failed to Start. Caused by Normal Setpoint Drift.Fans Retested | | | 05000335/LER-1980-015, Forwards Updated LER 80-015/03L-1 | Forwards Updated LER 80-015/03L-1 | | | 05000335/LER-1980-016, Forwards LER 80-016/09T-0 | Forwards LER 80-016/09T-0 | | | 05000335/LER-1980-016-09, /09T-0:on 800411,engineering Evaluation Determined That Application of Two Rosemount Model 1152 Pressure Transmitters Resulted in Reportable Situation.Caused by Design Problem.Transmitters to Be Replaced | /09T-0:on 800411,engineering Evaluation Determined That Application of Two Rosemount Model 1152 Pressure Transmitters Resulted in Reportable Situation.Caused by Design Problem.Transmitters to Be Replaced | | | 05000335/LER-1980-017-09, /09T-0:on 800428,penetrant Test of 45 Degree socket-welded Elbow Fittings in Nonclass Sys Showed Cracks at Same Location in Three Fittings.Caused by Generic Mfg Problem | /09T-0:on 800428,penetrant Test of 45 Degree socket-welded Elbow Fittings in Nonclass Sys Showed Cracks at Same Location in Three Fittings.Caused by Generic Mfg Problem | | | 05000335/LER-1980-017, Forwards LER 80-017/09T-0 | Forwards LER 80-017/09T-0 | | | 05000335/LER-1980-018-03, /03L-0:on 800419,liquid Waste Discharge Monitor Found to Be Isolated After Routine Controlled Release from 1B Equipment Drain Tank.Caused by Personnel Error.Procedure Change Issued | /03L-0:on 800419,liquid Waste Discharge Monitor Found to Be Isolated After Routine Controlled Release from 1B Equipment Drain Tank.Caused by Personnel Error.Procedure Change Issued | | | 05000335/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000335/LER-1980-019, Forwards LER 80-019/03L-0 | Forwards LER 80-019/03L-0 | | | 05000335/LER-1980-019-03, /03L-0:on 800501,during Normal Refueling Operations,Leak Check of Personnel Air Lock Indicated Leakage in Excess of Tech Specs.Caused by Defective Air Lock Handwheel Shaft Packing Gland.Packing Glands Adjusted | /03L-0:on 800501,during Normal Refueling Operations,Leak Check of Personnel Air Lock Indicated Leakage in Excess of Tech Specs.Caused by Defective Air Lock Handwheel Shaft Packing Gland.Packing Glands Adjusted | | | 05000335/LER-1980-020-03, /03L-0:on 800507,during Heatup Following Refueling,Auxiliary Feed Pump Governor Found Out of Adjustment.Caused by Drifting of Speed Setting Potentiometer.Potentiometer Readjusted | /03L-0:on 800507,during Heatup Following Refueling,Auxiliary Feed Pump Governor Found Out of Adjustment.Caused by Drifting of Speed Setting Potentiometer.Potentiometer Readjusted | | | 05000335/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000335/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000335/LER-1980-021-03, /03L-0:on 800507,during Normal Surveillance & post-maint testing,1A Diesel Generator Failed to Synchronize to Emergency Bus.Caused by Frequency Permissive Relay Being Set Incorrectly.Relay Setpoint Corrected | /03L-0:on 800507,during Normal Surveillance & post-maint testing,1A Diesel Generator Failed to Synchronize to Emergency Bus.Caused by Frequency Permissive Relay Being Set Incorrectly.Relay Setpoint Corrected | | | 05000335/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000335/LER-1980-022-03, /03L-0:on 800520,digital Data Processing Sys Malfunctioned During Power Operation.Caused by Computer Programing Error.Sys Repaired & Returned to Svc.Program Will Be Revised to Correct Software Problem | /03L-0:on 800520,digital Data Processing Sys Malfunctioned During Power Operation.Caused by Computer Programing Error.Sys Repaired & Returned to Svc.Program Will Be Revised to Correct Software Problem | | | 05000335/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000335/LER-1980-023-03, /03L-0:on 800511,during Power Ascension,Control Element Assemblies 19 & 58 Dropped to Full Insertion.Caused by Failure of 15-volt Power Supply Units.Both Control Element Assemblies Were Restored | /03L-0:on 800511,during Power Ascension,Control Element Assemblies 19 & 58 Dropped to Full Insertion.Caused by Failure of 15-volt Power Supply Units.Both Control Element Assemblies Were Restored | | | 05000335/LER-1980-024-03, /03L-0:on 800516,while Shut Down for Refueling, Periodic Test of Engineered Safety Features Showed 10 Diesel Generators Load Sequence Timers Were Out of Tolerance.Caused by Setpoint Drift.Maladjusted Relays Caused Other Prob | /03L-0:on 800516,while Shut Down for Refueling, Periodic Test of Engineered Safety Features Showed 10 Diesel Generators Load Sequence Timers Were Out of Tolerance.Caused by Setpoint Drift.Maladjusted Relays Caused Other Problems | | | 05000335/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000335/LER-1980-025-01, /01T-0:on 800512,during Planned Secondary Shutdown for Turbine Maint,Steam Header Would Not Depressurize Following Steam Stop Closure Due to Sheared Bypass Valve Stems.Cause Undetermined.Valve Stems Replaced | /01T-0:on 800512,during Planned Secondary Shutdown for Turbine Maint,Steam Header Would Not Depressurize Following Steam Stop Closure Due to Sheared Bypass Valve Stems.Cause Undetermined.Valve Stems Replaced | | | 05000335/LER-1980-025-09, /09X-1:on 800512,during Planned Secondary Plant Shutdown for Turbine Maint,Main Steam Header Would Not Depressurize Following Steam Stop Closure.Cause Unknown. Valve Stems Were Replaced & Verified Operable | /09X-1:on 800512,during Planned Secondary Plant Shutdown for Turbine Maint,Main Steam Header Would Not Depressurize Following Steam Stop Closure.Cause Unknown. Valve Stems Were Replaced & Verified Operable | |
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