05000335/FIN-2016003-02
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Finding | |
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Title | Licensee-Identified Violation |
Description | Licensee identified violation (LIV) - T.S.6.8.1 requires written procedures be established, implemented, and maintained covering applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Rev 2, 1978. Appendix A, Section 9, Procedures for Performing Maintenance, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to this, Unit 1 Pressure Isolation Valve (PIV) V3217 was rebuilt in October 2013, using Licensee procedure 0-GMM-80.22, Swing Check Valve Inspections. 0-GMM-80.22 did not provide specific detail to ensure consistency and first time work quality and directly resulted in V3217 being reassembled incorrectly. Specifically the disc arm bushings were installed backwards, as well as no spacers in the bushing bores. The period of concern was from the achievement of Mode 4 on August 5, 2016 at 09:43 hours, to declaration of entry into the TS action statement and entry into Mode 5 on August 4, 2016 at 20:03 hours, resulting in 82 hours9.490741e-4 days <br />0.0228 hours <br />1.35582e-4 weeks <br />3.1201e-5 months <br /> of operation with V3217 seat leakage outside of TS acceptance criteria. The inspectors characterized the safety significance of the issue utilizing Manual Chapter 0609.04, Significance Determination Process Initial Characterization of Findings, and determined the issue affected the barriers cornerstone due to leakage past an isolation valve. Manual Chapter 0609 Appendix A, The significance determination process (SDP) for Findings At-Power, Exhibit 3 was used to further evaluate this finding which screened as Green because the finding represented neither an actual open pathway in the physical integrity of the reactor containment and does not involve an actual reduction in the function of the hydrogen igniters in the reactor containment. This issue has been entered into the licensees CAP as AR 2148252. |
Site: | Saint Lucie ![]() |
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Report | IR 05000335/2016003 Section 4OA7 |
Date counted | Sep 30, 2016 (2016Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | J Rivera L Suggs R Carrion T Morrissey S Roberts |
Violation of: | Technical Specification - Procedures |
INPO aspect | |
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Finding - Saint Lucie - IR 05000335/2016003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Saint Lucie) @ 2016Q3
Self-Identified List (Saint Lucie)
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