12-06-2016 | On October 18, 2016, with the unit shutdown for a planned refueling outage (Mode 5, Refueling, 0% power), an evaluation of data from the scheduled Main Steam Line Isolation Valve ( MSIV) (System Code SB) and Main Steam Line Drain valve penetration Local Leak Rate Testing ( LLRT) determined the 'as found' maximum pathway leakage for the 'B' Inboard MSIV, CV-4415, and the Outboard Main Steam Line Drain valve, MO-4424, was in excess of the Technical Specification (TS) 3.6.1.3 leakage limit of 100 scfh for a single MSIV and 5 200 scfh for combined pathway leakage. The cause was determined to be a failure to perform periodic internal inspections of the MSIVs and a non-optimal valve design for the steam line drain application. Corrective actions included reworking CV-4415 to restore its leakage limit to below TS limits. Corrective actions are planned to replace MO-4424 with an optimal valve design. This event was of low safety significance had no impact on public health or safety. This event is reportable pursuant to 10CFR50.73(a)(2)(i)(B). |
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Category:Letter
MONTHYEARIR 05000331/20240022024-10-25025 October 2024 NRC Inspection Report No. 07200032/2024001 and 05000331/2024002 ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24163A0012024-08-0505 August 2024 LTR-24-0119-1-1 Response to Nh Letter Regarding Review of NextEras Emergency Preparedness Amendment Review ML24193A2432024-07-12012 July 2024 – Interim Audit Summary Report in Support of Review of License Amendment Requests Regarding Fleet Emergency Plan ML24149A2862024-06-12012 June 2024 NextEra Fleet - Proposed Alternative Frr 23-01 to Use ASME Code Case N-752-1, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems Section X1, Division 1 (EPID L-2023-LLR-0009) - Letter ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities NG-24-0004, 2023 Annual Radiological Environmental Operating Report2024-05-0808 May 2024 2023 Annual Radiological Environmental Operating Report NG-24-0003, Submittal of 2023 Annual Radioactive Material Release Report2024-04-24024 April 2024 Submittal of 2023 Annual Radioactive Material Release Report ML24072A0292024-03-29029 March 2024 Nextera Energy Duane Arnold, Llc. Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) NG-24-0001, 2024 Annual Decommissioning and Spent Fuel Management Funding Status Report and Independent Spent Fuel Storage Installation (ISFSI) Decommissioning Financial Assurance Update2024-03-0606 March 2024 2024 Annual Decommissioning and Spent Fuel Management Funding Status Report and Independent Spent Fuel Storage Installation (ISFSI) Decommissioning Financial Assurance Update NG-24-0002, 2023 Annual Exposure Report - Form 5s2024-03-0606 March 2024 2023 Annual Exposure Report - Form 5s L-2024-010, Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3)2024-01-25025 January 2024 Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3) NG-23-0010, Supplement to Duane Arnold Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule2023-12-0606 December 2023 Supplement to Duane Arnold Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule NG-23-0009, Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule2023-11-16016 November 2023 Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule ML23201A0872023-08-0303 August 2023 Audit Plan in Support of Review of License Amendment NG-23-0006, Independent Spent Fuel Storage Installation (ISFSI) Financial Assurance Update2023-05-23023 May 2023 Independent Spent Fuel Storage Installation (ISFSI) Financial Assurance Update ML23137A1672023-05-11011 May 2023 Submittal of 2022 Annual Radiological Environmental Operating Report NG-23-0004, 2022 Annual Radioactive Material Release Report2023-04-25025 April 2023 2022 Annual Radioactive Material Release Report NG-23-0003, 2022 Annual Exposure Report - Form 5s2023-04-21021 April 2023 2022 Annual Exposure Report - Form 5s NG-23-0002, 10 CFR 50.59 Report, Commitment Changes, 10 CFR 72.48 Report, Quality Assurance Program Changes, Technical Specification Basis Changes, and Revision of the DAEC Defueled Safety Analysis Report2023-03-27027 March 2023 10 CFR 50.59 Report, Commitment Changes, 10 CFR 72.48 Report, Quality Assurance Program Changes, Technical Specification Basis Changes, and Revision of the DAEC Defueled Safety Analysis Report NG-23-0001, 2023 Annual Decommissioning and Spent Fuel Management Funding Status Report2023-03-27027 March 2023 2023 Annual Decommissioning and Spent Fuel Management Funding Status Report L-2023-029, And Point Beach Units 1 and 2 Nuclear Property Insurance - 10 CFR 50.54(w)(3)2023-03-10010 March 2023 And Point Beach Units 1 and 2 Nuclear Property Insurance - 10 CFR 50.54(w)(3) ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities ML22339A0012022-12-22022 December 2022 – Acceptance of Requested Licensing Action Amendment Request for Common Emergency Plan IR 05000331/20220032022-12-13013 December 2022 NRC Inspection Report No. 05000331/2022003 (Drss) ML22285A0072022-10-13013 October 2022 NRC Analysis of NextEra Energy Duane Arnolds Decommissioning Funding Status Report, Docket No. 50-331 IR 05000331/20220022022-07-13013 July 2022 NRC Inspection Report Nos. 05000331/2022002(DNMS) and 07200032/2022002(DNMS) ML22090A1922022-05-26026 May 2022 Letter to B. Coffey, FPL from M. Doell - Duane Arnold Post Shutdown Activities Report Review Letter ML22132A2872022-05-24024 May 2022 ISFSI DQAP Approval Letter ML22111A0332022-05-20020 May 2022 Operating License Page Correction Letter to B. Coffey, Florida Power and Light, from M. Doell NG-22-0055, Revision to Duane Arnold Energy Center (DAEC) ISFSI-Only Emergency Plan2022-05-20020 May 2022 Revision to Duane Arnold Energy Center (DAEC) ISFSI-Only Emergency Plan ML22089A0492022-05-12012 May 2022 Sfmp Review Letter NG-22-0053, 2021 Annual Radiological Environmental Operating Report2022-05-0606 May 2022 2021 Annual Radiological Environmental Operating Report NG-22-0052, Regulatory Issue Summary 2000-11. NRC Emergency Telecommunications System, Statement of Intent to Implement the Proposed Voluntary Initiative2022-05-0404 May 2022 Regulatory Issue Summary 2000-11. NRC Emergency Telecommunications System, Statement of Intent to Implement the Proposed Voluntary Initiative IR 05000331/20224012022-04-27027 April 2022 Decommissioning Security Inspection Report 05000331/2022401 NG-22-0050, Revised Response to Request for Additional Information Relating to Decommissioning Quality Assurance Program, Revision 02022-04-26026 April 2022 Revised Response to Request for Additional Information Relating to Decommissioning Quality Assurance Program, Revision 0 NG-22-0049, 2021 Annual Radioactive Material Release Report2022-04-26026 April 2022 2021 Annual Radioactive Material Release Report ML22066A7632022-04-25025 April 2022 ISFSI-Only Emergency Plan License Amendment Approval L-2022-068, NextEra Energy Duane Arnold Quality Assurance Topical Report (FPL-3) Revision 22022-04-25025 April 2022 NextEra Energy Duane Arnold Quality Assurance Topical Report (FPL-3) Revision 2 NG-22-0035, Response to Request for Additional Information Relating to Decommissioning Quality Assurance Program. Revision 02022-04-13013 April 2022 Response to Request for Additional Information Relating to Decommissioning Quality Assurance Program. Revision 0 NG-22-0047, Registration of Independent Spent Fuel Installation Storage Cask and Notification of Permanent Removal of All Spent Fuel Assemblies from the Spent Fuel Pool2022-04-11011 April 2022 Registration of Independent Spent Fuel Installation Storage Cask and Notification of Permanent Removal of All Spent Fuel Assemblies from the Spent Fuel Pool NG-22-0042, Registration of Independent Spent Fuel Installation Storage Casks2022-04-0808 April 2022 Registration of Independent Spent Fuel Installation Storage Casks NG-22-0041, And Independent Spent Fuel Storage Installation, 2022 Annual Decommissioning and Spent Fuel Management Funding Status Report2022-03-31031 March 2022 And Independent Spent Fuel Storage Installation, 2022 Annual Decommissioning and Spent Fuel Management Funding Status Report NG-22-0030, Registration of Independent Spent Fuel Installation Storage Casks2022-03-23023 March 2022 Registration of Independent Spent Fuel Installation Storage Casks NG-22-0031, 2021 Annual Exposure Report - Form 5s2022-03-23023 March 2022 2021 Annual Exposure Report - Form 5s ML22080A1822022-03-22022 March 2022 Letter to B. Coffey from M. Doell - Duane Arnold ISFSI QAPD RAI Letter L-2022-012, Florida Power & Light Company Nuclear Property Insurance - 10 CFR 50.54(w)(3)2022-03-16016 March 2022 Florida Power & Light Company Nuclear Property Insurance - 10 CFR 50.54(w)(3) ML22059A7462022-03-10010 March 2022 ISFSI-Only Physical Security Plan License Amendment Approval NG-22-0025, Registration of Independent Spent Fuel Installation Storage Casks2022-03-0808 March 2022 Registration of Independent Spent Fuel Installation Storage Casks 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEARNG-18-0040, LER 2018-001-00 for Duane Arnold Energy Center Regarding Loss of RPS Function During MSIV and TSV Channel Functional Testing Due to Use of a Test Box2018-04-0404 April 2018 LER 2018-001-00 for Duane Arnold Energy Center Regarding Loss of RPS Function During MSIV and TSV Channel Functional Testing Due to Use of a Test Box 05000331/LER-2017-0012017-03-27027 March 2017 Condition Prohibited by Technical Specification - Containment Vent and Purge Valve Leakage, LER 17-001-00 for Duane Arnold Energy Center Regarding Condition Prohibited by Technical Specification - Containment Vent and Purge Valve Leakage NG-17-0072, LER 17-001-00 for Duane Arnold Energy Center Regarding Condition Prohibited by Technical Specification - Containment Vent and Purge Valve Leakage2017-03-27027 March 2017 LER 17-001-00 for Duane Arnold Energy Center Regarding Condition Prohibited by Technical Specification - Containment Vent and Purge Valve Leakage 05000331/LER-2016-0032016-12-0606 December 2016 Main Steam Isolation Valve Leakage Exceeded Technical Specification Limit, LER 16-003-00 for Duane Arnold Energy Center Regarding Main Steam Isolation Valve Leakage Exceeded Technical Specification Limit 05000331/LER-2016-0022016-12-0606 December 2016 Unplanned RCIC Inoperability Results in Safety System Functional Failure, LER 16-002-00 for Duane Arnold Energy Center Regarding Unplanned RCIC Inoperability Results in Safety Functional Failure NG-16-0225, LER 16-003-00 for Duane Arnold Energy Center Regarding Main Steam Isolation Valve Leakage Exceeded Technical Specification Limit2016-12-0606 December 2016 LER 16-003-00 for Duane Arnold Energy Center Regarding Main Steam Isolation Valve Leakage Exceeded Technical Specification Limit NG-16-0226, LER 16-002-00 for Duane Arnold Energy Center Regarding Unplanned RCIC Inoperability Results in Safety Functional Failure2016-12-0606 December 2016 LER 16-002-00 for Duane Arnold Energy Center Regarding Unplanned RCIC Inoperability Results in Safety Functional Failure 05000331/LER-2016-0012016-08-18018 August 2016 Two Instances of Both Doors in Secondary Containment Airlock Opened Concurrently, LER 16-001-00 for Duane Arnold Energy Center Regarding Two Instances of Both Doors in Secondary Containment Airlock Opened Concurrently 05000331/LER-2015-0062016-02-18018 February 2016 HPCI and RCIC Condensate Storage Tank Suction Transfer Inoperable, LER 15-006-00 for Duane Arnold Regarding HPCI and RCIC Condensate Storage Tank Suction Transfer Inoperable 05000331/LER-2015-0022016-01-28028 January 2016 Unanalyzed Condition Due to Degraded Primary Containment Suppression Pool Coating, LER 15-002-01 for Duane Arnold Regarding Unanalyzed Condition Due to Degraded Primary Containment Suppression Pool Coating NG-15-0236, LERs 15-001-01 and 15-003-01 for Duane Arnold Regarding Both Doors in Secondary Containment Airlock Opened Concurrently2015-06-25025 June 2015 LERs 15-001-01 and 15-003-01 for Duane Arnold Regarding Both Doors in Secondary Containment Airlock Opened Concurrently NG-07-0355, LER 07-S01-00 for Duane Arnold Regarding Unauthorized Person Allowed Entry to Duane Arnold Energy Center Protected Area2007-05-0303 May 2007 LER 07-S01-00 for Duane Arnold Regarding Unauthorized Person Allowed Entry to Duane Arnold Energy Center Protected Area NG-03-0373, LER 03-S01-00, Duane Arnold Unattended Safeguards Information Outside of the Protected Area Caused by Personnel Error2003-05-15015 May 2003 LER 03-S01-00, Duane Arnold Unattended Safeguards Information Outside of the Protected Area Caused by Personnel Error 2018-04-04
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
I. Description of Event:
On October 18, 2016, with the unit shutdown for a planned refueling outage (Mode 5, Refueling, 0% power), an evaluation of data from the scheduled Main Steam Line Isolation Valve (MSIV) (System Code SB) and Main Steam Line Drain valve penetration Local Leak Rate Testing (LLRT) determined the 'as found' maximum pathway leakage for the 'B' Inboard MSIV, CV-4415, and the Outboard Main Steam Line Drain valve, MO-4424, in excess of the Technical Specification (TS) 3.6.1.3 leakage limit of 5 100 scfh for a single MSIV and 5 200 scfh for combined pathway leakage.
II. Assessment of Safety Consequences:
Reportability Evaluation CV-4415 'as found' leakage was measured at 253.8 scfh. TS Surveillance (SR) 3.6.1.3.9 requires verification of leakage rate through each MSIV is 5_ 100 scfh and that the combined maximum pathway leakage rate for all four main steam lines is 5 200 scfh when tested at ?. 24 psig. Failure to meet this SR requires entry into LCO 3.6.1.3.9, Condition D, restore leakage to within limits within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, or be in MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The as found results exceeded the TS SR limit for individual and combined MSIV leakage and is reportable as a condition prohibited by TS and requires a Licensed Event Report (LER) to be submitted under 10CFR50.73(a)(2)(i)(B).
MO-4424 'as found' leakage was measured at 710 scfh. As stated in Updated Final Safety Analysis Report (UFSAR) Section 6.7.1, the total main steam pathway, which includes the four main steam lines and the inboard MSIV Drain Line, is limited to 200 scfh (i.e., the main steam line drains are included in the total leakage limit for all MSIVs). Therefore, the Main Steam Line Drains valve LLRT failures are included in this LER.
Safety Significance
The Main Steam system conducts steam from the reactor vessel through the primary containment to the main turbine. In performing this function, it serves as part of the primary boundary to prevent radioactive release to the surrounding environment.
Duane Arnold Energy Center 05000-331 The MSIV Leakage Treatment Path is designed to mitigate the release of fission products following a Loss of Coolant Accident (LOCA). This is accomplished by directing any leakage past closed MSIVs and closed Main Steam drain line isolation valves to the main condenser via the Main Steam drain line. The volume and surface area of the condenser provides holdup time and plate-out surface for fission products.
Pathways to other systems connected to the Main Steam system are isolated to ensure leakage is processed through this path.
The NRC has previously assessed the consequences of BWR main steam line releases. In a paper published in 2002 (PRAB-02-01, "Assessment of BWR Main Steam Line Release Consequences"), the NRC determined an MSIV leakage rate that would be considered risk-significant and would warrant further investigation. This assessment is conservative since benefits of holdup time, plate-out, and gravitational settling are ignored. Given a greater than 20 factor of conservatism, the report concludes there should be no regulatory concern if the leakage past the best sealing valve in any single main steam line is less than 10,000 scfh. This result is reflected in the NRC's Inspection Manual Chapter 0609, Appendix H where a simple probabilistic risk framework is provided for use in identifying potentially significant findings related to containment integrity.
The as-found leakage rate in both the B' Main Steam line and in the Main Steam Line Drain line is well below the 10,000 scfh criterion. Therefore, this event was of low safety significance and had no impact on public health or safety.
This event did not result in a SSFF.
III. Cause of Event:
A Root Cause Evaluation (RCE) was completed. The RCE determined that the cause for the `13' MSIV failure was failure to perform periodic internal inspections of the MSIVs and the cause for the outboard MSL Drain valve was a non-optimal valve design for steam line drain application.
IV. Corrective Actions:
Immediate Corrective Action CV-4415 internals were re-machined to restore its leakage to below TS limits.
The MSL Drain penetration pathway was isolated in accordance with TS 3.6.1.3.
Corrective Actions for Cause of Event The frequency of internal inspections of MSIVs will be increased to once every 10 refueling cycles.
Actions are planned to replace the MSL Drain valves with a new valve design.
V. Additional Information:
Previous Similar Occurrences:
A review of NextEra Energy Duane Arnold LERs from the previous 10 years found no other instances of events related to Main Steam Lines failing "as found" LLRT testing.
ElIS System and Component Codes:
SB — Main Steam System Reporting Requirements:
This activity is being reported pursuant to the requirements of 10CFR50.73(a)(2)(i)(B).