text
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _. _ _ _. _ _. _ _. _ _ _ _ _ _ _ _ _. _
\\
NRC Form see U S. NUCLEAR 6 EGULATORY COamstN40ss 0 83' APPROYED OMS NO.3190410e LICENSEE EVENT REPORT (LER)
FACILITY NAMS til DOCKET NuesSER 12)
PAGE43 Duane Arnold Energy Center o Is l o g o g o l3 i 3l l i i lorl 0 l4 TITLE 444 Scram due to F. W. reduction and SRV actuation EVENT DATE (5)
LER NUMBER (S)
REPORT DATE 171 OTMER F ACILITIES INVOLVED (0, MONTMl DAY YEAR YEAR
,0 MONTH DAY YEAR F ACILsTV NAMES DOCKET NUMSERIS)
NONE oisioiogo, i ;
Ol1 0l 7 8 4 8 l4 0l0 l 1 0l0 0l2 0l6 8 l4 NONE o iss oioici i
~
i THIS REPORT 88 $USMITTED PURSUANT TC THE REQUIREMENTS OF 10 CFR l: (CAece one er more er the felsemes) titi OPE R AttesG j
N 20 40am n.Oswi eeni.iaH=>
n ?1m R
30.405teH1HG 30 3steH1) 90.73teH2Het 73.71(al nei 1 1 01 0 2"awHum a awim
=4y7;;y;gy;,,
anwH2H*
20 406teH1HWI to.731 alt 2Hil 90.724eH2HetelHAl 356AJ 20.e05teH1Hl.)
60.73hM2Hal go.73teH2Hvist(3) 20 40S(aH1Hvl 60.7NH2HW) 90.73(aH2Hal LICENSEE CONTACT FOR THIS LER 112)
NAME TELEPMONE NUMSER ARE A COOE Michael S. Harris, Technical Support Engineer 85l i73 O6 31,9 i i i i i COMPLETE ONE LINE FOR EACM COMPONENT FAILURE DESCRISED IN TMit aEPORT 113)
ORT
([
CAUSE
SYSTEM COMPONE NT
[
"E'n gp CAlsit SY STEM COMPONENT I
y y
g E
PR X
SlJ iTiBiG X 91 99 N
i i i i i i i i
A sib l l R IV D12l4 0 N
l l l l l l SUPPLEMENT AL REPORT EXPECTED (14 MONTH DAY YEAR Ytt 199 res, tem,rere EXPECTED SusMtSSION DA TE)
NO l
l l
A=T R ACT a,,,
,.oo s
, e.,..
. A,
,,,.w
., A n.i While in run mode at approximately 1001, power, the "B" Feedwater Recirculatica valve f ailed open, thereby decreasing feedwater flow to the vessel. Due to an unrelated error in the performance of an ongoing surveillance test procedure, a main steam relief valve was inadvertently opened 43 seconds later. Vessel level decreased to the low level setpoint (170" above top of active fuel) and initiated a scram as designed. The relief valve was reseated approximately 75 seconds later.
Both RFP's tripped on low suction pressure. The vessel level continued to fall until the HPCI/RCIC initiation setpoint was reached (119.5" above top of active fuel). Level was restored to 194" and HPCI/RCIC were secured within 4 minutes.
Prior to startup, both feedwater recirc valves were repaired or inspected and the surveillance test procedure was revised to reduce the margin for personnel error in the future.
Ohhh PDR
""S i I
esRC perm 3e4A U S NUCLE A21 KEEULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AaPaoveo ove =o sino-moa EaPiRES S/31115 f
F ACIUTV NAA88 (1D Docket m#Unselm (21 (gn gunseg A (83 PAGE 131 Duane Arnold Energy Center m:;;pp
=,3 o ls jo lo lo l3 ]3 l1 8l 4 0 j 0l 1 0l 0 0l2 0F 0 l4 rixi n -.
e uc =.anw. m At 08:08:26 (T=0), while the reactor was at 99.8% power, the "B" Feedwater Recirculation Valve (SJ-FCV-1611) f ailed open due to a broken air supply line fitting. As a result, a portion of "B" reactor feedwater flow was returned to the condenser and the vessel level imediately began to drop.
While operators were diagnosing and compensating for the decrease in vessel level, the "B" Reactor Feedwater Pump tripped on low suction pressure and 1 of 2 safety / relief valves (SB-RV-4401) utilizing 10-10 set logic cycled open at T +43 ;econds.
After the relief valve opened, a momentary upswing in vessel level was experienced, followed by an rapid decrease in level to the low level trip setpoint (170") and an autc.natic scram initiation at T +44 seconds. At T +57 seconds, the "B" feedwater pump breaker was reset. At T +66 seconds, both feedwater pump, tripped on low suction pressure (due to condansate pumps being unable to match RFP flow with the high vessel demand and return flow to the condenser).
Ouring this time, the vessel level was continuing to fall until the 10-10 level HPCI/RCIC initiation setpoint of 119.5" was reached at T +73 seconds. At this point, HPCI and RCIC initiated per design and the level began to rise. As the vessel level fell to the 10-10 level setpoint momentarily, HPCI initiated but did not inject at any time in the event. HPCI control logic requires low-low level signal to remain present fnr the duration of the injection valve initiating time (aroroximately 15 seconds) to have HPCI actually inject. At T +112 seconds, the "B" reactor feedwater pump breaker was again closed to provide additional makeup and remaired closed with no further trips. The open safety / relief valve was reseated at T +118 seconds after operator action and remained closed. As RCIC was injecting and the "B" feedwater pump was functionino, the level quickly recovered to normal operating level (Maximum level reached uss 204.4" at T +4 min. 30 sec.).
After the level had recovercd, RCIC was secured at T +3 min. 50 sec. and HPCI was secured at T +4 min.
30 sec..
At this point, the vessel level and pressure were stable at 194" and 810 psig respectively.
All systems necessary for remaining in a safe shutdown condition were operable, and no further system perturbations were experienced.
In retrospect, the following causes and determinations can be made as to the exact component failures and related events leading up to, and af ter, the scram.
The feedwater recirculation valve (SJ-FCV-1611) is an air actuated, f ail open, control valve, Contrei Components model no. PDA964-96BW.
Investigation revealed that a flexible air supply line fitting broke due to fatigue. When the air supply was lost, the valve cycled open.
Prior to startup, the broken airline on the 'B' recirc valve was repaired. As an additional precaution, the identical airline on l
the ' A' recirc valve (SJ-FCV-1569) was inspected and found satisfactory. As a long 8
term corrective action, a maintenance action request has been generated to replace the fittings subject to fatigue with higher strength fittings.
Main steam safety / relief valve (SB-RV-4401) is one of two non-ADS safety relief valves that are utilized in the 10-10 set logic.
Following an event that has opened one of the six (6) safety / relief valves, the 10-10 set logic establishes a lower opening pressure (lifting pressure: 1020/1025 psig, reseating pressure:
900/905 psig) respectively.
Investigation revealed that the lifting of the SRV was totally unrelated to the failure of the feedwater recirc valve.
Prior to the recirc valve f ailure, a 10-10 set instrument functional test had comenced. While
- g.o...
i
eseC form 306A U S NUCLt131 KELULATORY COMM888&ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APmoveo ove *o 3 iso-oio.
E RPimf 8 8/3115 FACsLITV esAMeIH DOCA t T NUedt R (2)
LER NUMGER lt' PAGE13) vtan 580WENT'ab
Duane Arnold Energy Center 010 01 3 0F 014 o 1510 lo lo 131311 84
-- 01011 rm,
--c, w.nm performing the routine surveillance procedure, the instrument technician erroneously placed an ohnneter across the hi pressure switch contacts too early in the procedure. As a result, the SRV actuation solenoid relay was falsely energized with a hi pressure test signal, which, in conjunction with the procedure step to push the test button, caused the valve to cycle open (approx 40 seconds af ter the recirc valve f ailure). Approximately 75 seconds after the SRV had opened, the operators reset the 10-10 SRV logic, thereby disarming the solenoid and cycling the valve closed.
It was later theorized that due to the relatively low internal impedance of the ohmmeter, the meter acted as a jumper and bypassed the contacts.
It is noteworthy that prompt identification of the cause of the SRV actuation was greatly aided by the technician volunteering that he had indeed committed an error.
This theory was confirmed prior to startup after running a special test procedure.
This procedure recreated the applicable sequence of test steps leading up to the opening of the SRV and revealed that the connection of an ohnneter across the contacts in question in conjunction with pressing the test button, would in fact energize the SRV solenoid.
To preclude recurrence of similar situations, all instrument technicians ware assembled and shown during a step by step reconstruction, the exact cause of the event. The importance of proc? dural complianre without deviating from the prescribed testing sequence was impressed upon them.
To reduce the margin for personnel error, the surveillance test procedure has been revised to utilize a volt meter in lieu of an ohmmeter.
This revision will eliminate the possibility of the meter acting as a jumper in a circuit under test, regardless of when it is inserted. As a long term corrective action, selected surveillance test procedures are continuing to be revised to simplify and clarify the testing sequence, thereby reducing the possibility of personnel error.
In addition to this, a joint management /uninq task force is being forme 6 to determine and implement methods of maintaining a heightened awareness of the importance of minimizing personnel errors.
Prior to startup, all systems initiated during the scram and subsequent evolutions were reviewed to determine whether they had functioned per design and technical specifications. At 170" reactor water level, the reactor scramed, valve groups 2, 3, 4 and 5 isolated, and both trains of the standby gas treatment system initiated per design. At 119.5" reactor water level valve group 8 isolated, LPCI logic tripped both recirc pumps, loop select logic initiated and performed its' function, and HPCI/RCIC initiated per design.
During and after the transient, the operators observed a normal SRV tail pipe temperature response. As an additional precaution, a walkdown was performed on the tailpipe of the opened SRV. The piping and restraints were inspected and found satisfactory.
geo.. m.
j
senC Pere 3e64 U S NUCLEAR KEEULATOTY COMMIShiON UCENSEE EVENT REPORT (LER) TEXT CONTINUATION
E mPimES S/3155 PactLITV NAAlte (1)
DOCKli NUMSER (21 LER GIUMSER IS PAGE131 Duane Arnold Energy Center "edl:;r
- 'JJ,q i.a 0l0 01 4 0F 014 010l 1 o1510l0l013l3l1 814 rarra -. - - m,ami.mn It was also observed that only one " side" of the reactor 10-10 level switches initiated HPCI/RCIC. This was later attributed to the location of the level switches' sensing lines in relation to the opened SRV.
It appears that when the SRV opened, the resultant pressure profile across the top of the vessel skewed the actual level such that the low level was only seen by the switches whose sensing lines were attached to the vessel opposite the steam line on which the relief valve lifted.
It appears that vessel level just reached the 119.5" setpoint and did not decrease appreciably below that level. To ensure that the low level indicating switches were functioning properly, a surveillance test procedure was performed on both sides (4 channels) of the HPCI/RCIC initiation level switches.
Prior to diartup, both sides were found to be in calibration and functioning per design.
With the exception of the unrelated failure of the recirc valve and safety / relief valve, all components and systems functioned per design throughout the event. At no time was the safety of the plant or public endangered. Apart from the corrective actions outlined above, no further action is warranted or planned at this time.
g 4 0..
t J
Iowa Electric Light and Ibwer Company February 6, 1984 DAEC 64 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C.
20555 Subject: Duana Arnold Energy Center Docket No. 50-331 Op. License DPR-49 Licensee Event Report No.84-001 Gentlemen:
In accordance with 10 CFR 50.73 please find attached a copy of the subject Licensee Event Report.
Very truly yours, Daniel L. Mineck Plant Superintendent - Nuclear Duane Arnold Energy Center DLM/MSH/pv attachment cc: Mr. James G. Keppler Regional Administrator Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 NRC Resident Inspector - DAEC File A-118a
.fEAA r
I;(
Uuane Arnold Energy Center P.O. Bo.x ::51 Cedarliapids, iowa 52406 319'852. 612 h
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000331/LER-1984-001, :on 840107,feedwater Recirculation Valve B, Failed Open,Decreasing Feedwater Flow to Vessel.Caused by Error in Performing Surveillance Test Procedure.Both Valves Repaired.Test Procedure Revised |
- on 840107,feedwater Recirculation Valve B, Failed Open,Decreasing Feedwater Flow to Vessel.Caused by Error in Performing Surveillance Test Procedure.Both Valves Repaired.Test Procedure Revised
| | | 05000331/LER-1984-002, :on 840103,HPCI Inboard Steam Supply Isolation Valve Declared Inoperable.Caused by Technician Mistakenly Installing Jumper Across Relay Contact.Jumper Removed Allowing Valve to Open & Return to Svc |
- on 840103,HPCI Inboard Steam Supply Isolation Valve Declared Inoperable.Caused by Technician Mistakenly Installing Jumper Across Relay Contact.Jumper Removed Allowing Valve to Open & Return to Svc
| | | 05000331/LER-1984-003, :on 840102,04,06 & 16,auto-initiations of Control Bldg Ventilation Sys,Isolation Mode,Occurred from Main Inlet Air Low Temp.Caused by Inadequate Circulation. Damaged Coils Removed for Repair |
- on 840102,04,06 & 16,auto-initiations of Control Bldg Ventilation Sys,Isolation Mode,Occurred from Main Inlet Air Low Temp.Caused by Inadequate Circulation. Damaged Coils Removed for Repair
| | | 05000331/LER-1984-004, :on 840110 & 11,normal Control Bldg Ventilation Sys Isolated Due to Low Inlet Air Temp & Both Trains of Makeup Air Standby Filter Units Failed to Initiate Properly. Cause Unknown.Investigation Under Way |
- on 840110 & 11,normal Control Bldg Ventilation Sys Isolated Due to Low Inlet Air Temp & Both Trains of Makeup Air Standby Filter Units Failed to Initiate Properly. Cause Unknown.Investigation Under Way
| | | 05000331/LER-1984-005, :on 840102,RHR/core Spray Fill Pump Motor Tripped by Circuit Breaker Thermal Overload Relay.Caused by Pressure Below 40 Psig Having Potential for Air Ingress. Tech Spec Amend Requested & Fill Pump Rebuilt |
- on 840102,RHR/core Spray Fill Pump Motor Tripped by Circuit Breaker Thermal Overload Relay.Caused by Pressure Below 40 Psig Having Potential for Air Ingress. Tech Spec Amend Requested & Fill Pump Rebuilt
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000331/LER-1984-007, :on 840127,invalid Group III Automatically Initiated on hi-hi Radiation Alarm.Caused by Spurious Electrical Signal.High Radiation Cable Being Inspected for Possible Damage |
- on 840127,invalid Group III Automatically Initiated on hi-hi Radiation Alarm.Caused by Spurious Electrical Signal.High Radiation Cable Being Inspected for Possible Damage
| | | 05000331/LER-1984-008, :on 840123,facility Experienced Reactor Scram While in Normal Run Mode.Caused by Power Supply Failure. Reactor Maintained in Hot Shutdown Until Reactor Startup Corrected |
- on 840123,facility Experienced Reactor Scram While in Normal Run Mode.Caused by Power Supply Failure. Reactor Maintained in Hot Shutdown Until Reactor Startup Corrected
| | | 05000331/LER-1984-009, :on 840131,during Performance of LPCI Surveillance Test,Rhr Sys Discharge Piping Pressure Dropped to 0 Psig.Caused by Equipment Maladjustment.Position Indication on Two Valves in Question Adjusted |
- on 840131,during Performance of LPCI Surveillance Test,Rhr Sys Discharge Piping Pressure Dropped to 0 Psig.Caused by Equipment Maladjustment.Position Indication on Two Valves in Question Adjusted
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000331/LER-1984-011, :on 840205,auto-isolation of Control Bldg Ventilation & Initiation of Intake Standby Filter Unit B Occured Due to Low Inlet Air Temp.Caused by Inadequate Circulation Through nonsafety-related Coils |
- on 840205,auto-isolation of Control Bldg Ventilation & Initiation of Intake Standby Filter Unit B Occured Due to Low Inlet Air Temp.Caused by Inadequate Circulation Through nonsafety-related Coils
| | | 05000331/LER-1984-012, :on 840229,during HPCI Surveillance Testing, HPCI Turbine Stop Valve Failed to Open After Auxiliary Oil Pump Started.Hpci Declared Inoperable.Caused by Faulty Automatic Depressurization Sys Reset Switch |
- on 840229,during HPCI Surveillance Testing, HPCI Turbine Stop Valve Failed to Open After Auxiliary Oil Pump Started.Hpci Declared Inoperable.Caused by Faulty Automatic Depressurization Sys Reset Switch
| | | 05000331/LER-1984-013, :on 840413,increase of Unidentified Leakage Into Drywell Observed.Shutdown of Reactor Commenced.Caused by Packing Leak in Recirculation Pump a Discharge Bypass Valve.Valves Repacked & Adjusted |
- on 840413,increase of Unidentified Leakage Into Drywell Observed.Shutdown of Reactor Commenced.Caused by Packing Leak in Recirculation Pump a Discharge Bypass Valve.Valves Repacked & Adjusted
| 10 CFR 50.73(a)(2)(1) | | 05000331/LER-1984-014, :on 840416,inboard Reactor Water Cleanup Inlet Valve Isolated When Group III Planned Isolation & Partial Group V Unplanned Isolation Occurred.Caused by Electrical Noise on Leak Temp Differential Switch |
- on 840416,inboard Reactor Water Cleanup Inlet Valve Isolated When Group III Planned Isolation & Partial Group V Unplanned Isolation Occurred.Caused by Electrical Noise on Leak Temp Differential Switch
| | | 05000331/LER-1984-015, :on 840430,reactor Scram Experienced Due to Upscale Trip of Intermediate Range Monitors (Irm).Caused by Operator Failing to Select Higher IRM.Post-scram Review Confirmed All Sys Functioned Per Design |
- on 840430,reactor Scram Experienced Due to Upscale Trip of Intermediate Range Monitors (Irm).Caused by Operator Failing to Select Higher IRM.Post-scram Review Confirmed All Sys Functioned Per Design
| | | 05000331/LER-1984-017, :on 840504,HPCI Turbine Inadvertently Initiated During Routine Surveillance Test of Reactor low-low Water Level Instrumentation.Turbine Manually Tripped Prior to Injection.Caused by Personnel Error |
- on 840504,HPCI Turbine Inadvertently Initiated During Routine Surveillance Test of Reactor low-low Water Level Instrumentation.Turbine Manually Tripped Prior to Injection.Caused by Personnel Error
| | | 05000331/LER-1984-018, :on 840507,RCIC Steam Leak High Differential Pressure Relay Inadvertently Jarred & Energized,Causing Spurious RCIC Isolation & Turbine Trip Signals.Cause Unknown.Signal Reset & Isolation Valve Opened |
- on 840507,RCIC Steam Leak High Differential Pressure Relay Inadvertently Jarred & Energized,Causing Spurious RCIC Isolation & Turbine Trip Signals.Cause Unknown.Signal Reset & Isolation Valve Opened
| 10 CFR 50.73(a)(2) | | 05000331/LER-1984-019, :on 840521,0603,05 & 06,unplanned Partial Group V Isolation Experienced.Caused by Random Noise in Circuit.Further Study to Reduce Susceptibility of Sys to Spurious Isolation Pursued |
- on 840521,0603,05 & 06,unplanned Partial Group V Isolation Experienced.Caused by Random Noise in Circuit.Further Study to Reduce Susceptibility of Sys to Spurious Isolation Pursued
| | | 05000331/LER-1984-020, :on 840617,20 & 0710,spurious Initiation Signals from Control Bldg Air Intake Radiation Monitor a Automatically Started Standby Filter Unit A.Caused by High Moisture or Thunderstorms |
- on 840617,20 & 0710,spurious Initiation Signals from Control Bldg Air Intake Radiation Monitor a Automatically Started Standby Filter Unit A.Caused by High Moisture or Thunderstorms
| | | 05000331/LER-1984-021, :on 840617,during Surveillance Test for Standby Diesel Generator B Operability,Diesel Tripped on High Crankcase Pressure While Loaded to Approx 2,400 Kw.Caused by Scavenging Air Blower Failure.Blower Repaired |
- on 840617,during Surveillance Test for Standby Diesel Generator B Operability,Diesel Tripped on High Crankcase Pressure While Loaded to Approx 2,400 Kw.Caused by Scavenging Air Blower Failure.Blower Repaired
| | | 05000331/LER-1984-022, :on 840619,spurious Isolation Signal Caused Primary Containment Group III Isolation & Standby Gas Treatment Sys Actuation.Initiation Setpoint Not Reached.Sys Restored to Normal Operation |
- on 840619,spurious Isolation Signal Caused Primary Containment Group III Isolation & Standby Gas Treatment Sys Actuation.Initiation Setpoint Not Reached.Sys Restored to Normal Operation
| | | 05000331/LER-1984-023, :on 840619,w/plant at 75% Power,Surveillance Test Revealed Three of Four Reactor High Pressure Switches Out of Tolerance in Nonconservative Direction.Switches Recalibr,Returned to Svc & Retested |
- on 840619,w/plant at 75% Power,Surveillance Test Revealed Three of Four Reactor High Pressure Switches Out of Tolerance in Nonconservative Direction.Switches Recalibr,Returned to Svc & Retested
| | | 05000331/LER-1984-024, :on 840630,w/reactor Critical & Plant in Startup Mode,Isolation Valve on Inlet Line to Reactor Water Cleanup Sys Automatically Closed.Caused by Noise in Reactor Water Cleanup Sys |
- on 840630,w/reactor Critical & Plant in Startup Mode,Isolation Valve on Inlet Line to Reactor Water Cleanup Sys Automatically Closed.Caused by Noise in Reactor Water Cleanup Sys
| | | 05000331/LER-1984-025, :on 840808,electrical Supply Breaker for RCIC Steam Supply Valve Tripped Each Time Valve Cycled Closed. Caused by Torque Switch Out of Adjustment.Torque Switch Readjusted |
- on 840808,electrical Supply Breaker for RCIC Steam Supply Valve Tripped Each Time Valve Cycled Closed. Caused by Torque Switch Out of Adjustment.Torque Switch Readjusted
| | | 05000331/LER-1984-027, :on 840712,spurious Reactor Scram Occurred Due to Jarring of Instrument Rack in Reactor Bldg.Caused by Const of Scaffolding Adjacent to Instrument Rack 1C-56. Multicolored Demarcation Painted on Floor |
- on 840712,spurious Reactor Scram Occurred Due to Jarring of Instrument Rack in Reactor Bldg.Caused by Const of Scaffolding Adjacent to Instrument Rack 1C-56. Multicolored Demarcation Painted on Floor
| | | 05000331/LER-1984-028, :on 840714,degraded Voltage Condition on Offsite Power Grid Resulted in Automatic Switching of Buses to Onsite Power Initiating Scram.Caused by Spurious Isolation Upon Reenergizing from Temp Switches |
- on 840714,degraded Voltage Condition on Offsite Power Grid Resulted in Automatic Switching of Buses to Onsite Power Initiating Scram.Caused by Spurious Isolation Upon Reenergizing from Temp Switches
| | | 05000331/LER-1984-029, :on 840712,w/standby Filter Unit B Inoperable Due to Inoperable Radiation Monitor,Filter Unit a Failed to Function During Testing.Caused by Malfunction of Air Pilot Positioner.Monitors Will Be Replaced |
- on 840712,w/standby Filter Unit B Inoperable Due to Inoperable Radiation Monitor,Filter Unit a Failed to Function During Testing.Caused by Malfunction of Air Pilot Positioner.Monitors Will Be Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000331/LER-1984-029-01, :on 840718,standby Liquid Control Sys (Sblc) Isolated for 5 H After Improper Manipulation of Common Suction Valve from Sblc Tank to Sblc Pumps.Caused by Personnel Error.Procedures & Training Revised |
- on 840718,standby Liquid Control Sys (Sblc) Isolated for 5 H After Improper Manipulation of Common Suction Valve from Sblc Tank to Sblc Pumps.Caused by Personnel Error.Procedures & Training Revised
| | | 05000331/LER-1984-030, :on 840821,during Normal Operation,Momentary Violation of Second Containment Occurred When Two Secondary Containment Airlock Doors Opened Simultaneously.Caused by Personnel Error |
- on 840821,during Normal Operation,Momentary Violation of Second Containment Occurred When Two Secondary Containment Airlock Doors Opened Simultaneously.Caused by Personnel Error
| | | 05000331/LER-1984-031, :on 840903,barometric Condenser High Pressure Alarm in RCIC Sys Occurred.Caused by Inoperable Condenser Vacuum Pump.Rcic Declared Inoperable & 7-day Limiting Condition Initiated |
- on 840903,barometric Condenser High Pressure Alarm in RCIC Sys Occurred.Caused by Inoperable Condenser Vacuum Pump.Rcic Declared Inoperable & 7-day Limiting Condition Initiated
| | | 05000331/LER-1984-032, :on 840904,control Room Ventilation Sys B Started Automatically When Control Bldg Air Intake Radiation Monitor B Tripped.Caused by Spurious Initiations.Radiation Element Photomultiplier Tube Replaced |
- on 840904,control Room Ventilation Sys B Started Automatically When Control Bldg Air Intake Radiation Monitor B Tripped.Caused by Spurious Initiations.Radiation Element Photomultiplier Tube Replaced
| | | 05000331/LER-1984-033, :on 840906,electric Fire Pump Failed to Meet Flow Requirements & Plant Exceeded 7-day Limit for Pump Inoperability.Pump Impeller Adjusted to Increase Flow to Meet Requirement |
- on 840906,electric Fire Pump Failed to Meet Flow Requirements & Plant Exceeded 7-day Limit for Pump Inoperability.Pump Impeller Adjusted to Increase Flow to Meet Requirement
| | | 05000331/LER-1984-034, :Between 840821 & 0920,four Unintentional Momentary Violations Occurred When Two Secondary Containment Airlock Doors Simultaneously Opened.Caused by Defective Door Interlock & Latching Mechanisms |
- Between 840821 & 0920,four Unintentional Momentary Violations Occurred When Two Secondary Containment Airlock Doors Simultaneously Opened.Caused by Defective Door Interlock & Latching Mechanisms
| | | 05000331/LER-1984-035, :on 840921 & 26,four Violations Occurred Involving Two Secondary Containment Air Lock Doors Simultaneously Opening.Caused by Defective Door Interlock & Latching Mechanisms.Mechanisms Repaired |
- on 840921 & 26,four Violations Occurred Involving Two Secondary Containment Air Lock Doors Simultaneously Opening.Caused by Defective Door Interlock & Latching Mechanisms.Mechanisms Repaired
| | | 05000331/LER-1984-036, :on 840925,30 & 1020,reactor Water Cleanup Sys Isolated as Result of Momentary Spurious Signals in Leak Detection Logic.Cause Unknown.Sys Verified to Be Free of Actual Leakage |
- on 840925,30 & 1020,reactor Water Cleanup Sys Isolated as Result of Momentary Spurious Signals in Leak Detection Logic.Cause Unknown.Sys Verified to Be Free of Actual Leakage
| | | 05000331/LER-1984-037, :on 840929,reactor Scrammed on hi-hi Intermediate Range Monitor Signals from Channel E & F. Cause May Be Attributed to Spurious Electrical Noise.Review of Design & Installation Performed |
- on 840929,reactor Scrammed on hi-hi Intermediate Range Monitor Signals from Channel E & F. Cause May Be Attributed to Spurious Electrical Noise.Review of Design & Installation Performed
| | | 05000331/LER-1984-038, :Between 841029-1115,two Secondary Containment Airlock Doors Simultaneously Opened Three Times.Caused by Defective Door Latch Mechanisms or Interlock Solenoids. Devices Repaired |
- Between 841029-1115,two Secondary Containment Airlock Doors Simultaneously Opened Three Times.Caused by Defective Door Latch Mechanisms or Interlock Solenoids. Devices Repaired
| | | 05000331/LER-1984-039, :on 841101,during Normal Operation,Reactor Water Cleanup Sys Isolated Due to Momentary Spurious Signal in Reactor Water Cleanup Isolation Logic.Cause Unknown.Sys Free of Valid Isolation Parameters |
- on 841101,during Normal Operation,Reactor Water Cleanup Sys Isolated Due to Momentary Spurious Signal in Reactor Water Cleanup Isolation Logic.Cause Unknown.Sys Free of Valid Isolation Parameters
| | | 05000331/LER-1984-040, :on 841104,auxiliary Transformer Failed,Causing Main Generator & Auxiliary Transformer Breakers to Nonessential Buses to Open.Caused by Short Circuit Between Turns in High Voltage Winding of Phase Coil |
- on 841104,auxiliary Transformer Failed,Causing Main Generator & Auxiliary Transformer Breakers to Nonessential Buses to Open.Caused by Short Circuit Between Turns in High Voltage Winding of Phase Coil
| | | 05000331/LER-1984-041, :on 841111,reactor Water Conductivity Increased Above Tech Spec Limit.Caused by Resin or Air Intrusion. Operating Procedures Improved to Minimize Sys Disturbances |
- on 841111,reactor Water Conductivity Increased Above Tech Spec Limit.Caused by Resin or Air Intrusion. Operating Procedures Improved to Minimize Sys Disturbances
| 10 CFR 50.73(a)(2)(1) | | 05000331/LER-1984-042, :on 841123,reactor Scram Occurred as Result of Loss of Nonvital Buses.Caused by Transformer Trip from Spurious Fire Protection Deluge Sys Activation.Deluge Sys Modified |
- on 841123,reactor Scram Occurred as Result of Loss of Nonvital Buses.Caused by Transformer Trip from Spurious Fire Protection Deluge Sys Activation.Deluge Sys Modified
| | | 05000331/LER-1984-043, :on 841206 & 850102,control Room Intake Standby Filter Unit Initiated.Caused by Low Inlet Air Temp Setpoint. Preheat Coils Repaired |
- on 841206 & 850102,control Room Intake Standby Filter Unit Initiated.Caused by Low Inlet Air Temp Setpoint. Preheat Coils Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000331/LER-1984-044, :on 841207,fire Hose Inoperable.Caused by Maint Activities.Special Wye Fitting Placed on Hose Station 22 to Route Water to Fire Hose |
- on 841207,fire Hose Inoperable.Caused by Maint Activities.Special Wye Fitting Placed on Hose Station 22 to Route Water to Fire Hose
| | | 05000331/LER-1984-045, :on 841219,two Secondary Containment Airlock Doors Opened Simultaneously.Caused by Ineffective Door Latching Mechanism |
- on 841219,two Secondary Containment Airlock Doors Opened Simultaneously.Caused by Ineffective Door Latching Mechanism
| |
|