05000327/FIN-2012003-02
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Finding | |
|---|---|
| Title | Turbine Throttle Valve Reactor Trip Function Degraded |
| Description | The inspectors identified a Green NCV of Unit 1 TS 6.8, Procedures & Programs, for the licensees failure to provide adequate procedures for maintenance and surveillance activities involving the main turbine throttle valves and the associated solid state protection system (SSPS) function which provides a reactor trip on turbine trip signal. The failure to include applicable torque requirements for set screws associated with the limit switch lever arm assembly resulted in one of the four turbine throttle valve position limit switches being in an inoperable condition such that the SSPS function of reactor trip on turbine trip, which involves a four-out-of- four logic, was inoperable and could not have functioned if required. This issue was entered into the licensees corrective action program as Problem Evaluation Reports (PERs) 419594 and 518647 The finding was determined to be greater than minor because it was associated with the procedure quality attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the finding resulted in the inability of the SSPS to provide the required reactor trip signal upon closure of all four turbine throttle valves above 50 percent RTP. Using Inspection IMC 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the finding was determined to be of very low safety significance (Green) since the trip is not credited in any Updated Final Safety Analysis (UFSAR) Chapter 15 accident analysis and the redundant reactor trip on turbine trip function that is based on low auto stop oil pressure was unaffected. The cause of this finding was determined to have a cross-cutting aspect in the area of Human Performance, Resources component, and the aspect of complete and accurate procedures and work packages. The procedures for performing maintenance and surveillance activities associated with the turbine throttle valves and associated SSPS function were not adequate to assure nuclear safety due to the failure to include applicable torque requirements for the components associated with the valve limit switch assembly. |
| Site: | Sequoyah |
|---|---|
| Report | IR 05000327/2012003 Section 4OA2 |
| Date counted | Jun 30, 2012 (2012Q2) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71152 |
| Inspectors (proximate) | S Shaeffer C Young R Carrion W Deschaine |
| CCA | H.7, Documentation |
| INPO aspect | WP.3 |
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Finding - Sequoyah - IR 05000327/2012003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Sequoyah) @ 2012Q2
Self-Identified List (Sequoyah)
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