05000317/FIN-2014002-01
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Finding | |
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| Title | 11 and 12 AFW Pumps Inoperable due to Valves Misposition |
| Description | The inspectors identified a self-revealing problem consisting of NCVs of TS 3.7.3, Auxiliary Feedwater System, and TS 5.4.1, Procedures, because CENG Operations personnel did not adhere to procedures which resulted in a valve mispositioning event that inadvertently rendered the 11 and 12 turbine driven auxiliary feedwater (AFW) pumps inoperable for approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, a condition prohibited by TSs. Specifically, on February 7, 2014, operators did not perform draining of 11 turbine driven AFW pump steam supply drain line as stated in Operating Instruction (OI)-32A, Auxiliary Feedwater System, resulting in two main steam (MS) drain valves being left opened. With the drain valves open, an actual auxiliary feedwater actuation system (AFAS) signal would have resulted in steam blowing down into the room via the sump and causing room temperatures to exceed 130F, the maximum temperature allowed in the room to protect the pump air cooled bearings. Immediate corrective actions included restoring the proper AFW system valve lineup, entering this issue into their CAP, returning the valves to their normal position on Unit 1, and ensuring that similar valves were in the correct position on Unit 2. Planned corrective actions include conducting an apparent cause evaluation to understand the apparent and contributing causes of this event and determine additional corrective actions. The problem is more than minor because it is associated with the configuration control attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, Operations personnel lost configuration control of valves MS-225 and MS-228 resulting in the inoperability of the 11 and 12 AFW pumps for approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The inspectors evaluated the problem using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, The Significance Determination Process for Findings at Power, Exhibit 2, Mitigating Systems Screening Questions, issued June 19, 2012, and determined that the problem represented an actual loss of function of at least a single train for greater than its TS allowed outage time which required a detailed risk evaluation. The senior reactor analyst performed a detailed risk assessment utilizing the CCNPP Unit 1 simplified plant analysis risk model version 8.2.1 and determined that the problem is of very low safety significance (Green). Specifically, given a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> exposure period with both turbine driven AFW pumps assumed to fail-to-run, the change in the internal events core damage frequency (CDF) was calculated to be in the high 10-8 range (Green). This problem has a cross-cutting aspect in the area of Human Performance, Procedure Adherence, because CENG personnel did not follow processes, procedures, and work instructions. Specifically, after draining the 11 AFW pump mud leg, CENG plant operators did not restore MS-225 and MS-228 to their required position as stated in procedure OI-32A [H.8]. |
| Site: | Calvert Cliffs |
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| Report | IR 05000317/2014002 Section 1R15 |
| Date counted | Mar 31, 2014 (2014Q1) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71111.15 |
| Inspectors (proximate) | N Floyd P Kaufman S Kennedy T Burns A Bolger A Rosebrook D Schroeder E Torres H. Anagnostopoulus |
| Violation of: | Technical Specification - Procedures Technical Specification |
| CCA | H.8, Procedure Adherence |
| INPO aspect | WP.4 |
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Finding - Calvert Cliffs - IR 05000317/2014002 | ||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Calvert Cliffs) @ 2014Q1
Self-Identified List (Calvert Cliffs)
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