05000315/FIN-2012004-04
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Finding | |
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Title | Inadequate Procedures for Implementation of Annulus Cooling to Remain in a Analyzed Thermal Condition |
Description | A Severity Level IV NCV of very low safety significance of Title 10 of the Code of Federal Regulations (CFR) Part 72.150, Instructions, Procedures, and Drawings, was identified by the inspectors for the failure of the licensee to have procedures in place to ensure that the design basis peak fuel cladding temperature limit would not be exceeded during dry cask canister processing operations. The licensee took appropriate actions prior to conducting evolutions that may have challenged these limits. This has been documented in the licensees corrective action program as Action Request (AR) 2012-9676. Consistent with the guidance in Section 2.2 of the NRC Enforcement Manual, Independent Spent Fuel Storage Installation (ISFSIs) are not subject to the Reactor Oversight Process enforcement and, thus, traditional enforcement will be used for these facilities. Therefore the violation was dispositioned using the traditional enforcement process using Section 2.3 of the Enforcement Policy. The violation was determined to be of more than minor significance using IMC 0612, Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues, Example 3i, since the bounding conditions for the analyzed thermal condition was not reflected in the procedures to perform the port cap repair. Specifically, the licensees lack of evaluation did not ensure spent fuel cladding temperatures during canister processing operations would remain less than Spent Fuel Storage and Transportation Interim Staff Guidance-11, Cladding Considerations for the Transportation and Storage of Spent Fuel, safety limits. The inspectors determined that that the violation could be evaluated using Section 6.5.d.2 of the NRC Enforcement Policy, as a Severity Level IV violation, in that the licensee failed to establish, maintain, or implement adequate controls to ensure that the replacement of the port cap was performed under conditions bounded by a thermal analysis that ensured the integrity of the fuel would be maintained during the repair. Because the finding is associated only with traditional enforcement, there is not an associated cross-cutting aspect. |
Site: | Cook |
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Report | IR 05000315/2012004 Section 4OA5 |
Date counted | Sep 30, 2012 (2012Q3) |
Type: | TEV: Severity level IV |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | |
Inspectors (proximate) | M Mitchell J Lennartz J Neurauter J Ellegood V Meghani R Temps P Laflamme M Learn C Morrell R Edwards J Parrot |
INPO aspect | |
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Finding - Cook - IR 05000315/2012004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Cook) @ 2012Q3
Self-Identified List (Cook)
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