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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 h
- Salem Generating Station ;
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'U. S. Nuclear Regul'atory Commission-Document Control = Desk Washington,' DC 20555-J
- Dear' Sir:
f SALEN GENERATING STATION LICENSE NO. DPR-75
' DOCKET.NO..50-311L UNIT NO. 2 LICENSEE: EVENT REPORT 90-005-00.
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.This Licensee' Event-Report is being submitted pursuant to the a
requirements,of the. Code'of Federal Regulations 10CFR
- - I 50.73 (a) (2) (i) (B). 'This-report is required within thirty (30)-days 1
ofidiscovery..
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.. Sincerely yoursi
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K. Miller General Manager -
- - l Salem Operations MJP:pc Distribution
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IJCENSEE EVENT REPORT (LER) easeks v smaass m ooCast souuosa m ass in Salen Generating Station - Unit 2 0l6l0l0l0l3l1 [1 1 l0Fl 014 YtThe eel L
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, o e, On January 17, 1990, at 0010 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, following the discovery and i
l subsequent isolation of a leak.from a welded pipe cap on the discharge side of No. 2 Boron Injection Tank (BIT), Technical Specification Action Statement 3.0.3 was entered due to the inoperability of two (2) high. head Emergency Core Cooling System subsystems.
The leak was physically located on a portion of the old BIT recirc line which was removed and capped by a design change during the Unit 2 refueling outage in November 1988.
The leak was promptly identified, isolated, and a Unit shutdown was initiated and completed in accordance with Technical Specification requirements.
The affected pipe-to-cap socket weld joint was removed and immediately shipped to Westinghouse for failure analysis.
The joint was repaired and hydrostatically tested with satisfactory results.
The integrity of the remaining joints-associated with the design change was verified by a combination of l
hydrostatic and dye-penetrant testing.
The root cause has been attributed to a defect in the root of the weld.
A crack may have been
(
initiated at this defect during the system hydrostatic test following l
the design change.
High frequency, low amplitude cyclic loading, which is characteristic of the positive displacement pump discharge, caused the crack to propagate through the weld.
Stress corrosion in the area of the defect may have contributed to the crack initiation.
The metallurgical investigation concluded that the normal cyclic loading characteristics of the system would not have initiated a crack in the absence of the weld defect.
Based on the failure analysis-report, testing performed, and subsequent investigations performed by System Engineers, it was determined that this was an isolated case, ge ses
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psw LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 7
L iSalem-Generating Statio'n
. DOCKET NUMBER LER NUMBER PAGE b
Unit 2 5000311 90-005-00 2 of<4 L
ELANT AND SYSTEM IDENTIFICATION:
- - Westinghouse
- - Pressurized Water Reactor 4
- - Energy Industry Identification System (EIIS) codes'are identified in the text as (xxl IDENTIFICATION'OF OCCURRENCE:
TechnicalLSpecification 3.0.3 entry and subsequent Unit. shutdown due toLthe'inoperability of two Emergency Core Cooling System Subsystems Event Date:
1/17/90-Repcrt Date:
2/15/90 This report was initiated by Incident Report No.90-044.
CONDITIONS PRIOR TO OCCURRENCE:
' Mode I - Reactor Power 100% - Unit Load 1155 MWe c
DESCRIPTION'OF OCCURRENCE:
On January 17, 1990, at 0010 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, following the discovery.and subsequent isolation of a leak from a welded pipe cap on the discharge L
side of No.-2 Boron Injection Tank (BIT) (BQl, Technical Specification L
Action Statement 3.0.3 was entered due to the inoperability of'two (2) 4 EnergencycCore' Cooling System (ECCS) (BQl subsystems.
During Modes I
'(POWER' OPERATION), II'(STARTUP) and III (HOT STANDBY), Technical Specification 3.5.2 requires two (2) independent ECCS subsystems to be L
operable.
Isolation of the leak eliminated the discharge flowpath' from both centrifugal charging pumps, rendering both high head ECCS subsystems inoperable; hence, entry into Technical Specification Action Statement 3.0.3.
l Technical Specification Action Statement 3.0.3 states:
1 6'
"When a Limiting Condition for Operation is not met except as provided in the associated ACTION requirements, within one hour l
action shall be initiated to place.the unit in a MODE in which the specification ~does not apply by placing it, as applicable, t
in:
L 1.
At'least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, L
2.
'At least HOT SKUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and 3.
At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Where corrective measures are completed that permit operation under the ACTION requirements, the ACTION may be taken in accordance with the specified time limits as measured from the l1 time of failure to meet the Limiting Condition of Operation.
Exceptions to these requirements are stated in the individual L
specifications."
The-sequence of events were as follows:
9
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LICENSEE: EVENT' REPORT (LER) TEXT CONTINUATION i
Salem' Generating Station-DOCKET NUMBER LER-NUMBER PAGE Unit-2 5000311 90-005-00 3 of 4 DESCRIPTION OF OCCURRENCE:
(contfdl J
The sequence of events were as follows:
2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br />, January 16, 1990 - Commenced performing Reactor Coolant System leak rate calculations due to the automatic initiation of
- - residual heat removal sump pump runs.
2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> - Leak discovered coming from the general area of SJ10 (BIT
- - Relief Valve).
Shut SJ4 and SJ5 valves 1(BIT inlet motor operated valves).
Visually verified leakage to stop.
i 0010 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, January 17,-19901-After gaining access to the immediate area, identifying the actual source of the leak, and discussing the situation with the System Engineers, immediately declared the cold leg injection line via the BIT inoperable and entered Technical 4
Specification 3.0.3.
- - 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> - Commenced Unit shutdown to comply with Technical Specification 3.0.3 requirements.
0105. hours - Notified the Nuclear Regulatory Commission of-the initiation of the plant shutdown in accordance with the requirements of 10CFR 50.72 (b) (1) (i) ( A).
0503 hours0.00582 days <br />0.14 hours <br />8.316799e-4 weeks <br />1.913915e-4 months <br /> - Entered Mode II.
0554 hours0.00641 days <br />0.154 hours <br />9.160053e-4 weeks <br />2.10797e-4 months <br /> - Entered Mode III.
1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> - Entered Mode IV, exited Technical Specification Action Statement 3.0.3, and entered Technical Specification Action Statement 3.5.3.a (applicable in_ Mode IV) which requires the Unit to be in Mode V (COLD SHUTDOWN) in twenty (20) hours due to an inoperable flowpath from the refueling water storage tank.
0808 hours0.00935 days <br />0.224 hours <br />0.00134 weeks <br />3.07444e-4 months <br />, January 18, 1990 - Entered Mode V and terminated Technical Specification Action Statement 3.5.3.a.
APPARENT CAUSE OF OCCURRENCE:
As previously stated, the cause of the Technical Specification 3.0.3 entry and subsequent Unit shutdown was the isolation of the BIT discharge flowpath.
Following metallurgical evaluation of the pipe-to-cap socket weld joint, the root cause has been attributed to a:
defect in the root of the weld.
A crack may have been initiated at this defect during the system hydrostatic test following the design change, which was performed at 1.5 times the design system pressure..
Stress corrosion in the area of the defect may have contributed to the crack initiation.
High frequency, low amplitude cyclic loading, which is characteristic of the positive displacement pump discharge, caused the crack to propagate through the weld, resulting in a system boundary leak path.
DThe leak was physically located on a portion of the BIT to BAST recirculation line (# 1091), a one and one-quarter inch line which
ty' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
- - Salem Generating Statio'n' DOCKET. NUMBER LER NUMBER PAGE
- - Unit ~2 5000311-90-005-00 4 of 4
- - ANALYSIS OF ' OCCURRENCE:
)
was removed and capped by a design change during.the Unit 2 refueling
)
outage in November 1988.
The metallurgical investigation performed by Westinghouse concluded that the normal cyclic loading characteristics 1
of the system would not have initiated a crack in the absence of the R
weld defect.
Although the exact type of weld defect is indeterminate,-
i examination of the joint revealed proper fitup and analysis-revealed u
the use of proper filler metal (316 stainless steel).
Additionally, a review of records indicate that the welders qualifications are not in question.
Following repairs, a hydrostatic test verified' integrity of the replaced joint plus three (3) other joints installed during the design change (2EC-2187).
The remaining joints installed during the design change were verified to contain no through-wall leaks by dye-penetrant testing.
The weld detect is not common to this type of fillet weld.
No similar defec';s have been reported on either Unit.
Unit i has been in' service for over one fuel cycle with the same design change without incident.
This is considered an isolated case.
The leak was promptly located and isolated, and operations were in-accordance with Technical Specification requirements; therefore, the health or safety of the public was not affected by this event.
However, due to the completion of a plant shutdown which is required by the Technical Specifications, the event is reportable in accordance with the Code of Federal Regulations, 10CFR 50.73 (a) (2) (1) (A).
?
CORRECTIVE ACTION
o The leak was promptly identified, isolated, a Unit shutdown was initiated and completed in accordance with Technical Specification requirements, and the Commission was verbally notified in accordance l
with the requirements of the Code of Federal Regulations.
The l:
affected pipe-to-cap socket weld joint was removed'and immediately L
shipped.to Westinghouse for failure analysis.
Results of the investigation are documented in the " Apparent Cause" and " Analysis of
' Occurrence" sections of this report.
The joint was repaired and hydrostatically tested with satisfactory L
results.
The integrity of the remaining joints associated with the design change was. verified by a combination of hydrostatic and' dye-penetrant testing.
Based on the failure analysis report-by Westinghouse, testing performed, and subsequent investigations performed by System Engineers, which included review of the weld history,. design. change records, system configuration and previous system problems, it was determined that this was an isolated case.
Consequently, no further corrective actions are deemed necessary.
General Manager -
Salem Operations h
JLR:pc L
SORC Mtg.90-014
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| 05000272/LER-1990-001, :on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked |
- on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-001-01, :on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset |
- on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-002-01, :on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated |
- on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-002, :on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC |
- on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-003-01, :on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired |
- on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-003, :on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated |
- on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-004-01, :on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway |
- on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-004, :on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted |
- on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-005-01, :on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced |
- on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-005, :on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired |
- on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-006-01, :on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed |
- on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-006, :on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired |
- on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-007-01, :on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised |
- on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-007, :on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected |
- on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-008, :on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel |
- on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-008-01, :on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed |
- on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000311/LER-1990-009, :on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced |
- on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-009-01, :on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised |
- on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-010, :on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals |
- on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-010-01, :on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable |
- on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-011, :on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire |
- on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-011-01, :on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted |
- on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-012, :on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined |
- on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-012-01, :on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired |
- on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-013, :on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made |
- on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-013-01, :on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised |
- on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1990-014, :on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(b)(2)(ii) | | 05000272/LER-1990-014-01, :on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed |
- on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-015, :on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-015-01, :on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced |
- on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced
| | | 05000272/LER-1990-016-01, :on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design |
- on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-016, :on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised |
- on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-017-01, :on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed |
- on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-017, :on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated |
- on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-018, :on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike |
- on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike
| | | 05000272/LER-1990-018-01, :on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611 |
- on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-018, :on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced |
- on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-019-01, :on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway |
- on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-019, :on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation |
- on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-020-01, :on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control |
- on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-020, :on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed |
- on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-021, :on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns |
- on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-021-01, :on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel |
- on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1990-022-01, :on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722 |
- on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-022, :on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals |
- on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-023, :on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised |
- on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-023-01, :on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified |
- on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1990-024, :on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base |
- on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000272/LER-1990-024-01, :on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing |
- on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing
| | | 05000272/LER-1990-025-01, :on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08 |
- on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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