| | | Reporting criterion |
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| 05000259/LER-1985-001-02, :on 850121,unidentified Drywell Leakage Rate in Excess of Tech Spec,Noted.Shutdown Initiated.Caused by Leak in Temporary Hose & Weld Crack Inside Drywell.Repairs Made & Pertinent Procedures Revised |
- on 850121,unidentified Drywell Leakage Rate in Excess of Tech Spec,Noted.Shutdown Initiated.Caused by Leak in Temporary Hose & Weld Crack Inside Drywell.Repairs Made & Pertinent Procedures Revised
| |
| 05000296/LER-1985-001, :on 850104,during Normal Operation,Employee Accidentally Caused RCIC Sys to Be Inoperable for Approx 2 Minutes.All Other Required Core Standby Cooling Sys Fully Operable |
- on 850104,during Normal Operation,Employee Accidentally Caused RCIC Sys to Be Inoperable for Approx 2 Minutes.All Other Required Core Standby Cooling Sys Fully Operable
| |
| 05000259/LER-1985-001-01, :on 850121,drywell Leakage Rate in Excess of Tech Specs Noted.Caused by Leak in Temporary Hose Used to Test Check Valve & Small Weld Crack Inside Drywell.Crack Repaired.Procedures Revised |
- on 850121,drywell Leakage Rate in Excess of Tech Specs Noted.Caused by Leak in Temporary Hose Used to Test Check Valve & Small Weld Crack Inside Drywell.Crack Repaired.Procedures Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1985-001-03, :on 850221,removal of Thermocouple Revealed 1-inch Long Wall Crack at Weld Located at Junction of Recirculation Sys Header & Riser.Cause Unknown.Crack Will Be Repaired by Weld Overlay |
- on 850221,removal of Thermocouple Revealed 1-inch Long Wall Crack at Weld Located at Junction of Recirculation Sys Header & Riser.Cause Unknown.Crack Will Be Repaired by Weld Overlay
| |
| 05000259/LER-1985-002-03, :on 850124,all Eight Diesel Generators & Core Spray Pumps 3A & 3C Started During Performance of Core Spray Logic Functional Surveillance Instruction.Caused by Personnel Error.Personnel Cautioned |
- on 850124,all Eight Diesel Generators & Core Spray Pumps 3A & 3C Started During Performance of Core Spray Logic Functional Surveillance Instruction.Caused by Personnel Error.Personnel Cautioned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-002-01, :on 850107,power Cable Accidentally Shorted to Ground,Tripping Breaker That Supplies Several Instrument Panels.Caused by Bad Card.Personnel Briefed on Cause of Event |
- on 850107,power Cable Accidentally Shorted to Ground,Tripping Breaker That Supplies Several Instrument Panels.Caused by Bad Card.Personnel Briefed on Cause of Event
| |
| 05000260/LER-1985-002-04, :on 850307,during Refueling Outage Initial Test Results Received for Main Steam Relief Valves.Tech Spec Criteria Not Met by Eight Valves.Caused by Pilot Disc Sticking.Valve Setpoints Will Be Reset |
- on 850307,during Refueling Outage Initial Test Results Received for Main Steam Relief Valves.Tech Spec Criteria Not Met by Eight Valves.Caused by Pilot Disc Sticking.Valve Setpoints Will Be Reset
| 10 CFR 50.73(a)(2)(1) |
| 05000296/LER-1985-003-02, :on 850111,during Scheduled Test,Hpci & RCIC Sys Failed to Reach Rated Flow within Allotted Time.Hpci Sys Declared Inoperable.Caused by Incorrect Setting of Limit Switch |
- on 850111,during Scheduled Test,Hpci & RCIC Sys Failed to Reach Rated Flow within Allotted Time.Hpci Sys Declared Inoperable.Caused by Incorrect Setting of Limit Switch
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000260/LER-1985-003-04, :on 850227,automatic Scram Occurred When Fuses Removed from Reactor Protection Sys Circuitry During Mod. Caused by Deficient Work Plan.Plan Revised |
- on 850227,automatic Scram Occurred When Fuses Removed from Reactor Protection Sys Circuitry During Mod. Caused by Deficient Work Plan.Plan Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-003-03, :on 850205,diesel Generators C & D Inadvertently Started.Caused by Voltage Spike Trip Causing Cooling Tower Transformer Overpressurization Relays to Operate.Caution Signs Posted |
- on 850205,diesel Generators C & D Inadvertently Started.Caused by Voltage Spike Trip Causing Cooling Tower Transformer Overpressurization Relays to Operate.Caution Signs Posted
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1985-004-02, :on 850611,pH Value Below Tech Spec Limits. Cause Unknown.Formal Procedures for Handling of Chemistry Deviations in Special Operating Instructions for Future Safe End Replacement Work Established |
- on 850611,pH Value Below Tech Spec Limits. Cause Unknown.Formal Procedures for Handling of Chemistry Deviations in Special Operating Instructions for Future Safe End Replacement Work Established
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1985-004-04, :on 850610,low Ph Value Identified in Reactor Water Chemistry Sample.Caused by Inleakage Into Reactor Water Cleanup Sys.Impurity Removed by Sys Operation |
- on 850610,low Ph Value Identified in Reactor Water Chemistry Sample.Caused by Inleakage Into Reactor Water Cleanup Sys.Impurity Removed by Sys Operation
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1985-004-03, :on 850223,generator End of LPCI Motor Generator 1EA Found Overheated.Caused by Diode Failure Due to Vibration of Rectifier Ring.Phenolic Coil Clamps Replaced & Rectifier Rings Tightened |
- on 850223,generator End of LPCI Motor Generator 1EA Found Overheated.Caused by Diode Failure Due to Vibration of Rectifier Ring.Phenolic Coil Clamps Replaced & Rectifier Rings Tightened
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000296/LER-1985-004-01, :on 850122,surveillance Instruction Not Performed within Required Frequency Band.Caused by Operator Error.Operator Cautioned to More Carefully Apply Frequency Requirements in Future |
- on 850122,surveillance Instruction Not Performed within Required Frequency Band.Caused by Operator Error.Operator Cautioned to More Carefully Apply Frequency Requirements in Future
| 10 CFR 50.73(a)(2)(1) |
| 05000296/LER-1985-004, :on 850122,Surveillance Instruction 4.3.A.2 Performed 1 Day Later than Allowed by Tech Specs.Caused by Personnel Error in Interpreting Frequency Requirements. Procedures Re Performance Dates Revised |
- on 850122,Surveillance Instruction 4.3.A.2 Performed 1 Day Later than Allowed by Tech Specs.Caused by Personnel Error in Interpreting Frequency Requirements. Procedures Re Performance Dates Revised
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1985-005-04, :on 850611,reactor Water Cleanup Sys Isolated Due to Blown Fuse.Caused by Electrician Shorting Out Wires on Relay During Removal.Personnel Cautioned.Fuse Replaced. Sys Reset |
- on 850611,reactor Water Cleanup Sys Isolated Due to Blown Fuse.Caused by Electrician Shorting Out Wires on Relay During Removal.Personnel Cautioned.Fuse Replaced. Sys Reset
| |
| 05000296/LER-1985-005-01, :on 850210,cracked Weld on 3/4-inch Test Connection Line Discovered During Insp Following Shutdown to Investigate for Drywell Unidentified Leakage.Caused by Increased Vibration Due to Missing Pipe Clamp |
- on 850210,cracked Weld on 3/4-inch Test Connection Line Discovered During Insp Following Shutdown to Investigate for Drywell Unidentified Leakage.Caused by Increased Vibration Due to Missing Pipe Clamp
| |
| 05000259/LER-1985-005-03, :on 850227,during HPCI Sys Surveillance Testing,Time to Reach Rated Flow 2 Longer than Surveillance Instruction Spec of 25 S.Caused by Inadvertent Closing of Ball Valve on Turbine Hydraulic Sys |
- on 850227,during HPCI Sys Surveillance Testing,Time to Reach Rated Flow 2 Longer than Surveillance Instruction Spec of 25 S.Caused by Inadvertent Closing of Ball Valve on Turbine Hydraulic Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000296/LER-1985-006, :on 850213,mismatch Between Gemac Water Level Indicators Developed While at Low Pressure.Cause Attributed to Leak in Channel a Ref Leg Line X-28a.Operators Trained to Diagnose Water Level Problems |
- on 850213,mismatch Between Gemac Water Level Indicators Developed While at Low Pressure.Cause Attributed to Leak in Channel a Ref Leg Line X-28a.Operators Trained to Diagnose Water Level Problems
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1985-006-04, :on 850620,secondary Containment Isolation Initiated Due to Spike in Refuel Zone Exhaust Channel B Radiation Detector.Cause of Spike Unknown.Detector Successfully surveillance-tested |
- on 850620,secondary Containment Isolation Initiated Due to Spike in Refuel Zone Exhaust Channel B Radiation Detector.Cause of Spike Unknown.Detector Successfully surveillance-tested
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-006-02, :on 850304,during Performance of HPCI Sys Motor Operated Valve Operability Surveillance Instruction 4.5.E.1.c,HPCI Inverter Fuse Cleared.Caused by Blown Inverter Fuse.Fuse Replaced |
- on 850304,during Performance of HPCI Sys Motor Operated Valve Operability Surveillance Instruction 4.5.E.1.c,HPCI Inverter Fuse Cleared.Caused by Blown Inverter Fuse.Fuse Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000260/LER-1985-007-03, :on 850627,alternate Feeder Breaker Failed to Close,Resulting in Secondary Containment Isolation & Loss of Reactor Protection Sys Motor Generator.Caused by Breaker Failure Due to Loosened Bolts.Bolts Tightened |
- on 850627,alternate Feeder Breaker Failed to Close,Resulting in Secondary Containment Isolation & Loss of Reactor Protection Sys Motor Generator.Caused by Breaker Failure Due to Loosened Bolts.Bolts Tightened
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-007-02, :on 850318,handswitch Used for Purging Plant Stack Radiation Monitor Left in on Position,Allowing 2 H Unmonitored Release.Caused by Personnel Error.Switch Turned Off.Individual Reprimanded |
- on 850318,handswitch Used for Purging Plant Stack Radiation Monitor Left in on Position,Allowing 2 H Unmonitored Release.Caused by Personnel Error.Switch Turned Off.Individual Reprimanded
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 05000296/LER-1985-007-01, Canceled | Canceled | |
| 05000260/LER-1985-008-04, :on 850711,primary Containment Isolation Sys Group 3 Isolation Occurred When Incorrect Output Breaker of Reactor Protection Sys Motor Generator Set Opened.Caused by Personnel Error |
- on 850711,primary Containment Isolation Sys Group 3 Isolation Occurred When Incorrect Output Breaker of Reactor Protection Sys Motor Generator Set Opened.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-008, :on 850318,HPCI & RCIC Turbine Exhaust Valve Flanged Bonnets Not Local Leak Tested in Accordance w/10CFR50,App J Requirements.All Valves Will Be Repaired & Pass Leak Test |
- on 850318,HPCI & RCIC Turbine Exhaust Valve Flanged Bonnets Not Local Leak Tested in Accordance w/10CFR50,App J Requirements.All Valves Will Be Repaired & Pass Leak Test
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1985-008-02, :on 850315,discovered Listed Valves Not Local Leak Tested.Caused by Failure to Identify Valves Per 10CFR50.Two Valves Failed Subsequent Test & Unit Manually Scrammed.Two Other Valves to Be Modified |
- on 850315,discovered Listed Valves Not Local Leak Tested.Caused by Failure to Identify Valves Per 10CFR50.Two Valves Failed Subsequent Test & Unit Manually Scrammed.Two Other Valves to Be Modified
| 10 CFR 50.73(a)(2)(i) |
| 05000296/LER-1985-008-01, :on 850309,reactor Manually Scrammed Due to Problems W/Rod Worth Minimizer Program During Controlled Shutdown.Cause Not Stated |
- on 850309,reactor Manually Scrammed Due to Problems W/Rod Worth Minimizer Program During Controlled Shutdown.Cause Not Stated
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-009-04, :on 850320,during Investigation of Motor Noise, RHR Pump Motor 3D Failed.Caused by Failure of Lower Radial Guide Bearing Resulting in Failure of Stator Winding.On 850218,unrelated RHR Pump Motor Also Failed |
- on 850320,during Investigation of Motor Noise, RHR Pump Motor 3D Failed.Caused by Failure of Lower Radial Guide Bearing Resulting in Failure of Stator Winding.On 850218,unrelated RHR Pump Motor Also Failed
| |
| 05000296/LER-1985-009, :on 850320,RHR Pump Motor 3D Began to Smoke During Investigation of Unusual Motor Noise.Caused by Failure of Lower Radial Guide Bearing Resulting in Stator Winding Failure |
- on 850320,RHR Pump Motor 3D Began to Smoke During Investigation of Unusual Motor Noise.Caused by Failure of Lower Radial Guide Bearing Resulting in Stator Winding Failure
| |
| 05000260/LER-1985-009-03, :on 850712,during Unit 2 Refuel Outage, Inadvertent Containment Isolation Occurred When 480-V Shutdown Board Transferred to Deenergized Bus.Caused by Personnel Error.Employee Retrained on 850718 |
- on 850712,during Unit 2 Refuel Outage, Inadvertent Containment Isolation Occurred When 480-V Shutdown Board Transferred to Deenergized Bus.Caused by Personnel Error.Employee Retrained on 850718
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-009-01, :on 850322,analysis of Primary Containment Isolation Sys Circuitry Revealed That Combination of Switches Could Lead to Failure of Listed Sys to Function. Caused by Design Oversight |
- on 850322,analysis of Primary Containment Isolation Sys Circuitry Revealed That Combination of Switches Could Lead to Failure of Listed Sys to Function. Caused by Design Oversight
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1985-010-04, :on 850626,inadvertent Secondary Containment Isolation Occurred Due to Failure of Fuse in Panel 9-42. Cause Not Determined.Blown Fuse Replaced.Isolation Signal Reset.Failure Considered Random |
- on 850626,inadvertent Secondary Containment Isolation Occurred Due to Failure of Fuse in Panel 9-42. Cause Not Determined.Blown Fuse Replaced.Isolation Signal Reset.Failure Considered Random
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-010-02, :on 850421,inadvertent Initiation of Safety Sys Associated W/Primary Containment Isolation Signal Occurred Due to Short Caused During Fuse Removal.Caused by Personnel Error.Sys Returned to Standby Readiness |
- on 850421,inadvertent Initiation of Safety Sys Associated W/Primary Containment Isolation Signal Occurred Due to Short Caused During Fuse Removal.Caused by Personnel Error.Sys Returned to Standby Readiness
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-010-01, :on 850403,following Upscale Alarm of CAM-1-90-250,chemical Analyst Failed to Continue CAM Hourly Sampling Per Surveillance Instruction 4.8.B.1.a.Caused by Personnel Error.Personnel Given Addl Training |
- on 850403,following Upscale Alarm of CAM-1-90-250,chemical Analyst Failed to Continue CAM Hourly Sampling Per Surveillance Instruction 4.8.B.1.a.Caused by Personnel Error.Personnel Given Addl Training
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1985-011-02, :on 850716,reactor Water Cleanup Sys Isolation Occurred When Two Isolation Circuit Fuses Failed During Refueling Outage.Cause Undetermined.Fuses Replaced |
- on 850716,reactor Water Cleanup Sys Isolation Occurred When Two Isolation Circuit Fuses Failed During Refueling Outage.Cause Undetermined.Fuses Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-011-01, :on 850411,control Circuit Fuse Blew,Causing Partial Initiation of Primary Containment Isolation Sys. Caused by Failure of Relay 16AK72 Coil.Coil Replaced.New Fuse Installed.Recurrence Control Not Required |
- on 850411,control Circuit Fuse Blew,Causing Partial Initiation of Primary Containment Isolation Sys. Caused by Failure of Relay 16AK72 Coil.Coil Replaced.New Fuse Installed.Recurrence Control Not Required
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-012, :on 850405,deficiency in Standby Gas Treatment Cable Routing Discovered.Caused by Drawing Design Error. Junction Box Remounted to Meet Seismic Criteria & Design Personnel Counseled |
- on 850405,deficiency in Standby Gas Treatment Cable Routing Discovered.Caused by Drawing Design Error. Junction Box Remounted to Meet Seismic Criteria & Design Personnel Counseled
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1985-012-03, :on 850812,during Routine Surveillance Instruction,Esf Actuations Occurred.Caused by Slight Maladjustment of Refuel Zone Exhaust Radiation Monitor RI-90-144 Bug Source Due to Normal Wear |
- on 850812,during Routine Surveillance Instruction,Esf Actuations Occurred.Caused by Slight Maladjustment of Refuel Zone Exhaust Radiation Monitor RI-90-144 Bug Source Due to Normal Wear
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-012-02, :on 850425,0507 & 09,momentary Loss of Secondary Containment Occurred.Caused by Personnel Airlock Door Problems.Problems Considered Random Failures W/No Recurrence Control Required |
- on 850425,0507 & 09,momentary Loss of Secondary Containment Occurred.Caused by Personnel Airlock Door Problems.Problems Considered Random Failures W/No Recurrence Control Required
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1985-012-01, :on 850408,discovered Standby Gas Treatment Sys Divisional Cables Routed Through Fire Stop/Pressure Seals Using Spare Cables Designated for nonsafety-related Use. Junction Box Also Determined Seismically Unqualified |
- on 850408,discovered Standby Gas Treatment Sys Divisional Cables Routed Through Fire Stop/Pressure Seals Using Spare Cables Designated for nonsafety-related Use. Junction Box Also Determined Seismically Unqualified
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1985-013-03, :on 851002,during Performance of Plant Surveillance Instruction,Inadvertent Secondary Containment Isolation Occurred When Alternate Feeder Breaker to Shutdown Board Tripped.Caused by Binding Trip Button |
- on 851002,during Performance of Plant Surveillance Instruction,Inadvertent Secondary Containment Isolation Occurred When Alternate Feeder Breaker to Shutdown Board Tripped.Caused by Binding Trip Button
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-013-02, :on 850430,four Primary Containment Isolation Valves Failed Closure Time Surveillance Test.Caused by Revised Timing Procedure.Valves Will Be Repaired as Necessary & Timing Adjusted |
- on 850430,four Primary Containment Isolation Valves Failed Closure Time Surveillance Test.Caused by Revised Timing Procedure.Valves Will Be Repaired as Necessary & Timing Adjusted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000259/LER-1985-013-01, :on 850418,util Ofc of Engineering Determined That Existing Configuration of Startup Test Instrumentation Panels Cannot Be Determined to Be Seismically Qualified. Caused by Improper Mounting of Panels |
- on 850418,util Ofc of Engineering Determined That Existing Configuration of Startup Test Instrumentation Panels Cannot Be Determined to Be Seismically Qualified. Caused by Improper Mounting of Panels
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000296/LER-1985-014-01, :on 850429,radiation Indicator RI-90-142 Taken to Zero to Check Recorder Resulting in Inadvertent Initiation of Group 6 Containment Isolation Logic.Caused by Lack of Precautionary Note in Instruction |
- on 850429,radiation Indicator RI-90-142 Taken to Zero to Check Recorder Resulting in Inadvertent Initiation of Group 6 Containment Isolation Logic.Caused by Lack of Precautionary Note in Instruction
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-014, :on 850405,19,22,0501 & 24,while in Refueling/ Maint Outage,Diesel Generator & Shutdown Board Battery Racks Found Unqualified.Caused by Installation Errors.Racks Modified & Design Drawings Revised |
- on 850405,19,22,0501 & 24,while in Refueling/ Maint Outage,Diesel Generator & Shutdown Board Battery Racks Found Unqualified.Caused by Installation Errors.Racks Modified & Design Drawings Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1985-014-03, :on 851024,overcurrent Trip of Reactor Protection Sys Motor Generator Set & Inadvertent Partial Containment Isolation Occurred.Caused by Procedural Deficiency.Plant Maint Instruction Revised |
- on 851024,overcurrent Trip of Reactor Protection Sys Motor Generator Set & Inadvertent Partial Containment Isolation Occurred.Caused by Procedural Deficiency.Plant Maint Instruction Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1985-014-01, :on 850419,diesel Generator Racks & Shutdown Board Battery Rack 3EB Discovered to Be Seismically Unqualified.Caused by Installation Deficiency.Racks Modified to Meet Design Requirements |
- on 850419,diesel Generator Racks & Shutdown Board Battery Rack 3EB Discovered to Be Seismically Unqualified.Caused by Installation Deficiency.Racks Modified to Meet Design Requirements
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000296/LER-1985-014-02, :on 850429,Group 6 Containment Isolation Logic Inadvertently Initiated.Caused When RI-90-142 Taken to Zero Position to Check Recorder Reading.Containment Isolation Signal Reset |
- on 850429,Group 6 Containment Isolation Logic Inadvertently Initiated.Caused When RI-90-142 Taken to Zero Position to Check Recorder Reading.Containment Isolation Signal Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1985-014, Corrected Ltr Forwarding LER 85-014-00 Re Containment Isolation Initiation | Corrected Ltr Forwarding LER 85-014-00 Re Containment Isolation Initiation | 10 CFR 50.73(a)(2)(iv), System Actuation |