05000286/FIN-2010002-01
From kanterella
Jump to navigation
Jump to search
Finding | |
|---|---|
| Title | |
| Description | A self-revealing finding of very low safety significance was identified because Entergy personnel did not have adequate procedures appropriate for the circumstances for maintenance associated with the steam-driven auxiliary feedwater (AFW) pump. Specifically, Entergy implemented maintenance procedures associated with the 32 AFW pump, which contained coupling gap dimensions inconsistent with vendor requirements, and did not ensure appropriate shaft axial alignment for continued, reliable pump operation. As a result, in February 2010, high pump axial vibrations exceeded operability limits during scheduled surveillance testing, the pump was removed from service, and troubleshooting was initiated to determine the cause. Entergy personnel performed turbine-end bearing replacements, oil flush and refill of all bearing housings, performed coupling inspections and shaft alignment, successfully performed post-maintenance surveillance testing, and performed an appar.ent cause evaluation within the corrective action program under condition report (CR)-IP3-2010-00541 and IP3-2009-04592.The inspectors determined the finding is more than minor because the finding is associated with the procedure quality objective of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inadequate procedures resulted in increased unavailability to evaluate and correct vibration and other issues between November 2009 and February 2010. The inspectors evaluated the significance of the finding using IMC 0609, Attachment 4, and determined this finding was not a design or qualification deficiency, did not result in a loss of safety function, and was not impacted by external events. Consequently, the finding is of very low safety significance. The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance because Entergy staff did not ensure that complete, accurate and up-to-date procedures were available to perform appropriate maintenance on a safety-related AFW pump. |
| Site: | Indian Point |
|---|---|
| Report | IR 05000286/2010002 Section 1R19 |
| Date counted | Mar 31, 2010 (2010Q1) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71111.19 |
| Inspectors (proximate) | E Keighley J Noggle M Gray M Halter P Cataldo S Barr |
| CCA | H.7, Documentation |
| INPO aspect | WP.3 |
| ' | |
Finding - Indian Point - IR 05000286/2010002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Indian Point) @ 2010Q1
Self-Identified List (Indian Point)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||