05000280/LER-2076-004, Re Failure of Valve in Suction Line to Close
| ML19105A172 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 05/20/1976 |
| From: | Stallings C Virginia Electric & Power Co (VEPCO) |
| To: | Moseley N NRC/RGN-II |
| References | |
| Serial No. 041 LER 1976-004-00 | |
| Download: ML19105A172 (3) | |
| Event date: | |
|---|---|
| Report date: | |
| 2802076004R00 - NRC Website | |
text
I*,
I.
I.
1 *,
I*
......~. -
. I -..
- . ' ~sulatory ~~\\ fi..
VIRGINIA. ELECTRIC.AND *.POWER COMP.ANY R10:e:M0Nn, V1:i-l.ox'N1A* 23261
- May 20, 1,976
- Mr*~ Not'.!llan C. i1ose.ley, _Director.
Office.of* Irisp_ection.*and. Enforcement.'
u. S~_:Nuclear *Regulatory Conmission
- - Serial No~
- 041
..
- PO&M/ ALH:j lf.....
Docke't:- No.:,* 50-_2'81
_License *No. *DPR,:.37 Region< II ~ Suite ~ra*
230 Peachtree Street,:Northwe$t Atlanta,* Georgi.a.- ::*30303-,:..
- Dear-.'i1i-~ M~seley:.**.
. Pur~ua~t'. to S"t.irry *P~wer St::ation. Technical Specificati~n 6.6.2; the
... Virgi11,ia Electric. ~d Power Company here}?y sul:mits. a copy, of R~portable.
,Occurrence No. JJSRE~S2-76.. Q4.*_.:*
,,_.* The.substance ~f:th:tsireport'has b~en reviewed by the'st:at:.ion Nu;lear.*-:
- _ '> :_ : :Safety. arid Operating Comn'tttee-and *~rill-be* placed :-Qn_ the agend~ for the. ~ext
- .**~* 111eet:ing: of ~e-'Syst~ Nudear.:s*af~ty-arid.Operating;G9Jmnittee~..
Enclosure c,*
'-\\._.....
. /.*.. Very truly yours,.
. Original. Signed B~ * * : *.
W~l\\ Pr6f:f1t**';**:
tor.
.. c~ M. stalling{*,..
..* *. Vice. Presiderit..,Power :supply,
'.*. :_and *Produ*~tion-.dperations.
.. cc:
- Mr.: R~bert W_. Reid, -C4i~f* (40). ;.: *
- * :operating _React9rs*: Branch ll :*
USRE-S2-75-04 CONTROL BLOCK:... I _.___.___,_ _ _.___.____,
LICENSEE EVENT REPOR.T tDln
- .1* ~
, iDocket..:ill
. u~gu atoTY tt.,,
LICENSEE
- ~~~
- .~<~~,-.S/.S
- :i,~~[t!~t~. *.
- .,~:LEASE PRINT ALL REQUIRED INFORMATION)
.':ej LICENSE EVENT 1
NAME LICENSE NUMBER TYPE TYPE
@El Iv I A I s I Pis l 2 I Io Io 1-1 o I al al o i o I~ I o I o I I 1~ I 1 I 1 I 1 I O I I O I 3 I 7
8 9 14 15 25 26 30 31 32 CATEGORY REPORT TYPE.
REPORT SOURCE DOCKET NUMBER EVENT OATE REPORT DATE
@E]coN'T IM I I I uJ ~ lol sl oj-~I ol 2ls 11 I ]ol412l2)1l6l !olsl1)1l1l6I 7
8.
57 58 59 60 61 68 69 74 75 80
EVENT DESCRIPTION
@:@l I With Unit 2 at intermediate shutdown prior to refueling shutdown, MOV-SW-202B, a valvej 7
8 9 80
~
- I __,i...
- n"'--t=h=e--=-s-=u;.;;;c...;;;t'""i'-=oc.::n;;..._:l:..:i:..:n;.:.;e:;__t.::.o.;;.......::t:;.;h..::e--=s..:e:..;:r:...:v..:i::..:c:...:e:.......ip::..:u=rn::.ip.:..:s~f::..r::..o.::..rn=--=t=h-=e~c-=i-=r~c~u::.:l:.:a:.:t:..:J.:::* n~g~w~a:..:t:..:e:..:r_:c:..:a::n:.:a:.:l::..:,~f:.:a::i:..* l=-=e..:d_:t_:o__JI 7
8 9 80 joj41 I close when a CLS Hi-Hi,. Train B signal was actuated during a routine functional testn-l 7
8 9
~( L (PT-8,5A)..
This event is in violation of Technical 80 Specification 3.4oA.5 and report-J 7
8 9 [filfil I ab le 7
8 9 per Technical Specification 6.6.2eb(2)o The immediate corrective action was 80 (CONTrD)
SYSTEM GODE
@EJ rn..l~
7 8 9 10
CAUSE
CODE uJ 11 CAUSE DESCRIPTION COMPONENT CODE LYl__Al Lj V I E I X I 12 17 PRIME COMPONENT SUPPLIER
~
43 COMPONENT MANUFACTURER IP,-314 lo r 44 47 VIOI.AllON w
48
~
jA maintenance order 7
8 9 was initiated to repair the valvec The contacts of the torque 80 I
BO
@El !switch.were corroded. causing an open circuit 7
8 9 condition in the valve closing circuit. J 80 the valve was demonstrated-~
[i@I IA new toraue switch was installed~ After this maintenance 7
8 9 (CONT I DJ BO FACILITY STATUS
- % POWER OTHER STATUS EE]
w ltlgj_QJ z
7 B
g 10 12 13 FOAM OF ACTIVITY CONTENT [1 !21 RELEASED OF RELEASE AMOUNT OF ACTIVITY w
~J I N/A 7
8 9
10 11 PERSONtllEL EXPOSURES NUMBER TYPE
DESCRIPTION
~ l_gj_oj_gj w N/A 7
B g 11 12 13 PERSDNNEL INJURIES NUMBER
DESCRIPTION
EB l_gj_gj__gj L
'N / A 7
8 9 11 12 OFFSITE CONSEQUENCES 44 44 METHOD OF DISCOVERY w
45 DISCOVERY DESCRIPTION I~ _N/_A __________ _J 46 BO LOCATION OF RELEASE N/A 45 80 BO 80 [ili] LN:.;.L.'=A _______________________________
____J 7
B 9 BO LOSS OR DAMAGE TO FACILITY TYPE
DESCRIPTION
Q]J.W I NIA 7
8 9 10 80 PUBLICITY EI?.] l N/A 7
8 9 80 ADDITIONAL FACTORS
~ ! 'rhis valve could have been manually closed had this been requi:!'.'ed_ in an accident con-I 7
8 9 dition; hence, its failure to close did not adversely affect the health or safety of 80 rili:J ~.. the public*-"----
7 8 9 NAME.:J..., M~ Swee~~-"'---*
PHONE: (804) 357-3j_84 80 GPO 6 6 I
- 6 6 7
EVENT DESCRl._PTION (GDNT 1D~
to manually close the valve (USRE-S2-76-04).
CAUSE DESCRIPTION(CONT 1D) be operable.
The other valve in the same valve pit, MOV-SW-202A, did not experience a similar problem since it was proven operable during functional test PT8.SA.
Because this similar*
valve was exposed to the same environmental conditions and did not fail, it is felt that this was an isolated occurrence and therefore no further.oorrective action is deemed
- necessarye