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September 26, 1991 Virginia Electric and Power Company Surry Power Station P. 0. Box315 Surry, Virginia 23883 U. S. Nuclear Regulatory Commission Document Control Desk Serial No.:.91-573 Docket No.: 50-280 License No.: DPR-32 Washington, D. C. 20555 Gentlemen:
Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Unit 1.
REPORT NUMBER 91-019-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by the Corporate Management Safety Review Committee.
Very truly yours, M. R. Kansler Station Manager Enclosure cc:
Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323 9110010059 910926 PDR ADOCK 05000280 S
PDR
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NRC FORM 366 U.S. NUCLEAR REGU~ATORY COMMISSION APPROVED 0MB NO. 3150-0104 (6-891 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER)
INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) loocKET NUMBER 121 r
PAGE 131 Surry Power Station, Unit 1 o1s10101012,s,o 1 loF 0 14 TITLE (41 Loss of* Containment Integrity Due to a Crack in Component Cooling Water Piping EVENT DATE (51 LER NUMBER (61 REPORT DATE (71 OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR }?
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REVISION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(SI NUMBER NUMBER 0 Is Io I o I o I I
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I OPERATING THIS REPORT IS SUBMITIED PURSUANT TO THE RcQUIREMENTS OF 10 CFR §: (Chock on* or moro of th* following) (11)
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LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager 8 I O 14 31517 I -1311 1814 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 f::::::.::,:::.:::::::;:;:,::::::::::.::::::::::::,:,
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SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR EXPECTED
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ABSTRACT (Limit to 1400 sp8ces, i.e.. tJpproximately fifteen single-space typewritten lines/ 116)
On August 28, 1991, with Unit 1 at 100% power and Unit 2 at 60% power, while investigating the erratic behavior of a portion of the primary plant instrumentation inside Unit 1 containment, a through-wall crack was discovered in the Component Cooling Water (CCW) supply to the "B" Reactor Shroud Cooler (l-VS-E-6B).
This portion of the ccw System utilizes an automatic return line isolation valve and a
membrane barrier for containment isolation.
When the piping wall was breached, containment integrity no longer existed.
A six-hour action statement to hot shutdown was entered at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on August 28, 1991.
The leak was isolated, and the action statement exited at 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br />.
The health and safety of the public were not affected.
This event is reportable pursuant to 1 OCFR50. 73(a)(2)(i)(B ).
NRC Form 366 16-891 - ---- -------------16-891 FACILITY NAME 11 I e
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LEA)
TEXT CONTINUATION DOCKET NUMBER 121 APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-5301, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT 13150-01041, OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
LEA NUMBER 161 PAGE 131 Surry Power Station, Unit 1 o Is I o I o I o 12 I 8 Io 91 1 -
o 11 I 9 -
ol o o I 2 OF o I 4 TEXT /If morw _,,. ia,wqund, u,. addltioMI NRC Fonn 35fiA'a) 1171 1. O DESCRIPTION OF THE EVENT 2.0 At 1950 hours0.0226 days <br />0.542 hours <br />0.00322 weeks <br />7.41975e-4 months <br /> on August 27, 1991, with Unit 1 at 100% power and Unit 2 at 60% power, a portion of the Unit 1 Reactor Coolant System (RCS) Loop "B" instrumentation (EIIS-IM) began to behave erratically.
The erratic instrumentation was declared inoperable and the affected channels were placed in "trip" at 2007 hours0.0232 days <br />0.558 hours <br />0.00332 weeks <br />7.636635e-4 months <br />.
At about the same time, operators noted an increase in containment sump in-leakage (0.61 gpm versus an initial value of about 0.1 gpm).
Upon sampling, the sump was found to contain chromates at the same concentration as that of the Component Cooling Water (CCW) System (EIIS-CC).
A containment entry was made, and a through-wall crack was discovered in the three-inch CCW supply line to the "B" Reactor Shroud Cooler (1-VS-E-6B) (EIIS-CD-HX).
Water from the leak was spraying on the "B" Loop Resistance Temperature Detector Manifold and had caused the earlier noted ~nstrumentation problems.
At 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on August 28, 1991, a six-hour action. statement to hot shutdown was entered because of the violation of containment integrity.
This section of CCW piping utilizes an automatic return line isolation valve and a membrane barrier for containment isolation.
A membrane barrier consists of either pipe, tubing, or component wall.
When the pipe wall was breached, containment integrity no longer existed.
Operation above cold shutdown in this condition is prohibited by Technical Specification 3. 8.A.1.
The leak was isolated and the action statement was exited at 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br /> on August 28, 1991.
This.event is reportable pursuant to 10CFR50.73(a)(2)(i)(B).
SIGNIFICANT SAFETY CONSEQUENCES *AND IMPLICATIONS The Surry Power Station Updated Final Safety Analysis Report describes the design bases for containment isolation during incident conditions as at least two barriers between the atmosphere outside containment and
- the atmosphere inside containment
The failure of one valve or barrier does not prevent isolation.
For CCW
- piping, the two barrier arrangement is provided by a
membrane barrier inside containment and isolation valve arrangements in the piping entering and exiting containment.
The incoming isolation valve arrangement includes a
manual isolation valve in series with a check valve.
The outgoing piping is isolated by an automatic isolation valve.
During this event, bath the incoming and outgoing valve isolation arrangements remained
- operable, thereby maintaining one containment integrity barrier intact.
Since containment was accessible, the leaking section of piping was isolated
,, (6-89)
FACILITY NAME (11 e
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER (21 EXPIRES: 4/30/92 APPROVED 0MB NO. 3150-0104 MATEO BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
LER NUMBER (81 PAGE (31 Surry Power Station, Unit 1 o Is I o I o I o 12 1 a I o 91 1 _ o 11 1 9 _ o I o o 1 3 oF o 1 4 TEXT.(If mota -
ia 19qund, u*.,JdltionlJI NRC Fonn.BA '1) !171 3.0 by shutting manual supply and return valves 1-CC-30 and 1-CC-33 (EIIS-CC-ISV) inside containment, restoring the integrity of the remainder of the membrane barrier.
Since one containment integrity barrier remained operable and no event occurred which would have required isolation of the containment, the health and safety of the public were not affected.
CAUSE QF THE EVENT The cause of the leak in the three-inch CCW p1pmg was a through-wall crack which originated in the toe of a weld and propagated for about 25° around the circumference of the pipe.
Replacement of the affected piping is planned for the next cold shutdown of sufficient duration.
It is planned to conduct a failure analysis on the failed piping.
- 4. O IMM~DIATE CORRECTIVE ACTION<Sl The leak was isolated by closing the manually operated valves inside containment.
These valves were placed under
- 5. O ADDITIONAL CORRECTIVE ACTION<Sl The affected section of piping will be replaced during the next cold shutdown of sufficient duration.
- 6. O ACTIONS TO PREVENT RECURRENCE The remaining Reactor Shroud Cooler CCW piping in both. units will be walked down and visually inspected for leaks.
Because of ALARA concerns, these walkdowns will be conducted during the next outages of sufficient duration.
Additional inspections will be scheduled as appropriate after the failure analysis has been completed and the results evaluated.
In addition, strengthened requirements barriers.
administrative control procedures will be reviewed and as necessary to assure that containment integrity are met in systems which depend upon membrane
- 7. o
SIMILAR EVENTS
LER 89-042-00 (Unit 1)
Leakage Through Fault in Letdown System Drain Line in Excess of Allowable Type "C" Leakage
(
- -----(6-89)
FACILITY NAME (11 e
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER (21 Surry Power Station, Unit 1 0 IS IO Io Io,2 I s, 0 TEXT (If more -
ia r.qund, u* ttdditional NRC Fonn 3'i6A'*J (171 8.0
ADDITiONAL INFORMATION
None. A APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
LER NUMBER (61 PAGE (3)
- SEQUENTIAL ::::::::::* REVISION YEAR NUMBER
- NUMBER 91 1 _
0 I ~ 9 _ 0 I O 01 4 OF O I 4
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| 05000281/LER-1991-001-02, :on 910307,block Valves Declared Inoperable Until Required Surveillance Testing Satisfactorily Complete. Caused by Personnel Error.Task Team Formed to Address Missed Surveillance & Other Recent Similiar Events |
- on 910307,block Valves Declared Inoperable Until Required Surveillance Testing Satisfactorily Complete. Caused by Personnel Error.Task Team Formed to Address Missed Surveillance & Other Recent Similiar Events
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-001-01, :on 910309,frequency for Visual Insp of High Energy Lines in Main Stream House Had Exceeded Limit.Caused by Administrative Inadequacies.Task Team Formed to Generically Address Problem of Missing Tests |
- on 910309,frequency for Visual Insp of High Energy Lines in Main Stream House Had Exceeded Limit.Caused by Administrative Inadequacies.Task Team Formed to Generically Address Problem of Missing Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-002-02, :on 910326,two Charging Pumps & One Charging Pump Svc Water Pump Inoperable Causing Instrument Air Failure.Caused by Personnel Error.Charging Pump Returned to Svc |
- on 910326,two Charging Pumps & One Charging Pump Svc Water Pump Inoperable Causing Instrument Air Failure.Caused by Personnel Error.Charging Pump Returned to Svc
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000281/LER-1991-002-01, :on 910326,main Stream Safety Valves Out of Tolerance.Caused by Minor Setpoint Drift.Affective Valve Adjusted & Valve Tested to Verify Setpoint to Be within Required Tolerance |
- on 910326,main Stream Safety Valves Out of Tolerance.Caused by Minor Setpoint Drift.Affective Valve Adjusted & Valve Tested to Verify Setpoint to Be within Required Tolerance
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000281/LER-1991-003-02, :on 910424,pressurizer Safety Valves Found to Have Lift Setpoints Lower than Min Due to Minor Damage/Wear. Valves Refurbished,Reset & re-installed |
- on 910424,pressurizer Safety Valves Found to Have Lift Setpoints Lower than Min Due to Minor Damage/Wear. Valves Refurbished,Reset & re-installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-003-01, :on 910408,discovered That Periodic Test, Conducted on 910103,to Check for Proper Operation of Records Storage Vault Halon Sys Performed Improperly.Caused by Personnel Error.Test Procedure Revised |
- on 910408,discovered That Periodic Test, Conducted on 910103,to Check for Proper Operation of Records Storage Vault Halon Sys Performed Improperly.Caused by Personnel Error.Test Procedure Revised
| | | 05000281/LER-1991-004-02, :on 910514,inadvertent Overfilling of Refueling Water Storage Tank Occurred.Cause Unknown.Architect/Engineer Consulted to Review Tank Design |
- on 910514,inadvertent Overfilling of Refueling Water Storage Tank Occurred.Cause Unknown.Architect/Engineer Consulted to Review Tank Design
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-004-01, :on 910409,discovered That One of EDG 3 Had Been Erroneously Tagged Out & Rendered Inoperable Due to Personnel Error.Incorrectly Tagged Pump Tested & Restored to Operability |
- on 910409,discovered That One of EDG 3 Had Been Erroneously Tagged Out & Rendered Inoperable Due to Personnel Error.Incorrectly Tagged Pump Tested & Restored to Operability
| | | 05000281/LER-1991-005-02, :on 910602,reactor Coolant Sys Leakage Exceeded Tech Spec Limits.Caused by Mechanical Failure of Isolation Valve.Preparation of Design Change Has Been Underway That Will Install RTDs on Main RCS Lines |
- on 910602,reactor Coolant Sys Leakage Exceeded Tech Spec Limits.Caused by Mechanical Failure of Isolation Valve.Preparation of Design Change Has Been Underway That Will Install RTDs on Main RCS Lines
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2)(vii) 10 CFR 50.73(o)(2)(i) | | 05000280/LER-1991-005-01, :on 910413,failure to Sample Svc Water from Component Cooling HX Discovered.Caused by Personnel Error. Radiation Monitor Sys for Svc Water Discharge from Component Cooling HXs Replaced W/Improved Sys |
- on 910413,failure to Sample Svc Water from Component Cooling HX Discovered.Caused by Personnel Error. Radiation Monitor Sys for Svc Water Discharge from Component Cooling HXs Replaced W/Improved Sys
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2)(v) 10 CFR 50.73(o)(2)(vii) 10 CFR 50.73(o)(2)(i) | | 05000281/LER-1991-006-02, :on 910719,safety Injection Sys Interlock Rendered Inoperable & Unit Not Placed in Shutdown within Six H Due to Personnel Error.Failed Amplifier Circuit Board & Calibr Circuit Board Replaced |
- on 910719,safety Injection Sys Interlock Rendered Inoperable & Unit Not Placed in Shutdown within Six H Due to Personnel Error.Failed Amplifier Circuit Board & Calibr Circuit Board Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-006-01, :on 910419,AFW Pump 2-FW-P-3B Rendered Inoperable Due to Drawing Error.Pump Suction Line Plug Removed from Ecst,Satisfactorily Tested & Returned to Svc |
- on 910419,AFW Pump 2-FW-P-3B Rendered Inoperable Due to Drawing Error.Pump Suction Line Plug Removed from Ecst,Satisfactorily Tested & Returned to Svc
| | | 05000281/LER-1991-007, :on 910802,safety Injection/Reactor Trip Occurred.Caused by Intermittent Loss of Voltage to Channel Iva Protection Instrumentation.Channel Iva Instrumentation Stabilized |
- on 910802,safety Injection/Reactor Trip Occurred.Caused by Intermittent Loss of Voltage to Channel Iva Protection Instrumentation.Channel Iva Instrumentation Stabilized
| | | 05000280/LER-1991-007-01, :on 910422,both Trains of Auxiliary Ventilation Exhaust Discovered Inoperable Due to Personnel Error.Train a Auxiliary Ventilation Exhaust Fan Tested & Restored to Operability |
- on 910422,both Trains of Auxiliary Ventilation Exhaust Discovered Inoperable Due to Personnel Error.Train a Auxiliary Ventilation Exhaust Fan Tested & Restored to Operability
| | | 05000281/LER-1991-007-02, :on 910802,ESF Actuated & Safety Injection & Reactor Trip Occurred as Result of High Steam Flow Signal Coincident W/Low Steam Line Pressure Signal.Caused by Loss of Voltage to Protection Instrumentation |
- on 910802,ESF Actuated & Safety Injection & Reactor Trip Occurred as Result of High Steam Flow Signal Coincident W/Low Steam Line Pressure Signal.Caused by Loss of Voltage to Protection Instrumentation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000281/LER-1991-008-02, :on 910814,charging Pump Component Cooling Pump a Tagged Out to Replace Pump Discharge Check Valve & Exceeded 24 H Lco.Caused by Unanticipated Delays During Maint.Engineering Evaluation Performed |
- on 910814,charging Pump Component Cooling Pump a Tagged Out to Replace Pump Discharge Check Valve & Exceeded 24 H Lco.Caused by Unanticipated Delays During Maint.Engineering Evaluation Performed
| 10 CFR 50.73(b)(2)(i) | | 05000280/LER-1991-008-01, :on 910425,two Main Control Room/Emergency Switchgear Room Chillers Declared Inoperable.Caused by Failure of Reset Relay for Oil Pressure/Overload Trip.Edg Returned to Svc & Relay Installed |
- on 910425,two Main Control Room/Emergency Switchgear Room Chillers Declared Inoperable.Caused by Failure of Reset Relay for Oil Pressure/Overload Trip.Edg Returned to Svc & Relay Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000281/LER-1991-009-02, :on 910903,determined That Check Valve 2-RH-47 Not Full Flow Tested During Cycle 10 Refueling Outage.Caused by Personnel/Procedural Error.Procedure Changed & Testing Performed on 910908 |
- on 910903,determined That Check Valve 2-RH-47 Not Full Flow Tested During Cycle 10 Refueling Outage.Caused by Personnel/Procedural Error.Procedure Changed & Testing Performed on 910908
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-009-01, :on 910509,discovered That Visual Exams of Reactor Vessel Partial Penetration Welds & Bottom of Reactor Vessel Not Performed During 1990 Refueling Outage.Caused by Personnel Error.Exam Frequency Increased |
- on 910509,discovered That Visual Exams of Reactor Vessel Partial Penetration Welds & Bottom of Reactor Vessel Not Performed During 1990 Refueling Outage.Caused by Personnel Error.Exam Frequency Increased
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000281/LER-1991-010-01, :on 911031,determined That Damage to C Main Steam Trip Valve Bypass Valve 2-MS-155,rendered Valve Incapable of Immediate Closure.Valve 2-MS-155 Replaced & Failure Evaluation Will Be Performed |
- on 911031,determined That Damage to C Main Steam Trip Valve Bypass Valve 2-MS-155,rendered Valve Incapable of Immediate Closure.Valve 2-MS-155 Replaced & Failure Evaluation Will Be Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000281/LER-1991-010-03, :on 911031,determined That Damage to C Main Steam Trip Valve/Bypass Valve 2-MS-155 Rendered Valve Incapable of Immediate Closure.Caused by Failure of Yolk Bushing Threads in Valve.Valve Closed |
- on 911031,determined That Damage to C Main Steam Trip Valve/Bypass Valve 2-MS-155 Rendered Valve Incapable of Immediate Closure.Caused by Failure of Yolk Bushing Threads in Valve.Valve Closed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-010, :on 910530.ASME Section XI Inservice Testing Program Requirements Discovered Not Met.Caused by Personnel Error.Review of Inservice Testing Program Conducted to Identify Any Other Compliance Issues |
- on 910530.ASME Section XI Inservice Testing Program Requirements Discovered Not Met.Caused by Personnel Error.Review of Inservice Testing Program Conducted to Identify Any Other Compliance Issues
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-010-01, :on 910530,inservice Testing Instrumentation Discovered to Exceeded Limits.Caused by Personnel Error. Calibration Data for Installed Instrumentation Used to Perform Testing Evaluated |
- on 910530,inservice Testing Instrumentation Discovered to Exceeded Limits.Caused by Personnel Error. Calibration Data for Installed Instrumentation Used to Perform Testing Evaluated
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000280/LER-1991-011-01, :on 910406,simulated Design Basis Accident Conditions Resulted in Failure of Pumps to Develop Design Flow & Discharge Pressure.Caused by Inadequate Design. Permanent Mod of Radiation Sys Evaluated |
- on 910406,simulated Design Basis Accident Conditions Resulted in Failure of Pumps to Develop Design Flow & Discharge Pressure.Caused by Inadequate Design. Permanent Mod of Radiation Sys Evaluated
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000281/LER-1991-011-03, :on 911217,automatic Reactor Trip Occurred as Result of Turbine Trip Due to High SG Level.Caused by Failure of B Main FW Regulating Valve to Maintain Demand Position.Valve Inspected,Replaced & Tested |
- on 911217,automatic Reactor Trip Occurred as Result of Turbine Trip Due to High SG Level.Caused by Failure of B Main FW Regulating Valve to Maintain Demand Position.Valve Inspected,Replaced & Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000280/LER-1991-012-01, :on 910720,discovered That Pressurizer Level Channel Not Declared Inoperable,Per Acceptance Criteria Due to Personnel Error.Personnel Involved Reinstructed in Review of Recorded Data & Supervision of Trainees |
- on 910720,discovered That Pressurizer Level Channel Not Declared Inoperable,Per Acceptance Criteria Due to Personnel Error.Personnel Involved Reinstructed in Review of Recorded Data & Supervision of Trainees
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-013-01, :on 910723,MCC Room Fire Supression Sys Discovered Inoperable.Caused by Personnel Error.Continuous Firewatch Posted at Unit 1 MCC Room & Door Blocking Device Installed |
- on 910723,MCC Room Fire Supression Sys Discovered Inoperable.Caused by Personnel Error.Continuous Firewatch Posted at Unit 1 MCC Room & Door Blocking Device Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-014-01, :on 910724,determined That Main Steam Flow Setpoints in Excess of Max TS Allowed Value of 110%.Caused by Use of Incorrect Scaling Methodology.Flow & Feedwater Flow Transmitters Will Be Respanned |
- on 910724,determined That Main Steam Flow Setpoints in Excess of Max TS Allowed Value of 110%.Caused by Use of Incorrect Scaling Methodology.Flow & Feedwater Flow Transmitters Will Be Respanned
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000281/LER-1991-014, :on 910724,determined That Scaling for Main Steam Flow Transmitters Incorrect,Resulting in Setpoints in Excess of Max Allowed Value of 110%.Caused by Use of Incorrect Methodology.Scaling Program Underway |
- on 910724,determined That Scaling for Main Steam Flow Transmitters Incorrect,Resulting in Setpoints in Excess of Max Allowed Value of 110%.Caused by Use of Incorrect Methodology.Scaling Program Underway
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2)(iv) | | 05000280/LER-1991-015-01, :on 910809,two Main Control Room/Emergency Switchgear Room Chillers Discovered Inoperable.Caused by Thermostat Failure & Inoperable Emergency Power Source. Thermostat Replaced & Chiller Returned to Svc |
- on 910809,two Main Control Room/Emergency Switchgear Room Chillers Discovered Inoperable.Caused by Thermostat Failure & Inoperable Emergency Power Source. Thermostat Replaced & Chiller Returned to Svc
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-016-01, :on 910811,two Main Control Room/Emergency Switchgear Room Chillers Determined Inoperable.Caused by Inoperable Thermostat & Chiller Svc Water Pump.Thermostat Replaced on Chiller a |
- on 910811,two Main Control Room/Emergency Switchgear Room Chillers Determined Inoperable.Caused by Inoperable Thermostat & Chiller Svc Water Pump.Thermostat Replaced on Chiller a
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-017-01, :on 910509,EDG Rendered Inoperable Due to Personnel Error in That Specified Fast Start Test Was Not Performed.Governor for EDG Readjusted & Two Consecutive Fast Start Tests Performed Satisfactorily |
- on 910509,EDG Rendered Inoperable Due to Personnel Error in That Specified Fast Start Test Was Not Performed.Governor for EDG Readjusted & Two Consecutive Fast Start Tests Performed Satisfactorily
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-018-01, :on 910826,switchyard Transformer Fault Occurred Resulting in Loss of 4160 Volt Transfer Buses,Start of EDGs & Identification of EDG Underspeed Condition.Caused by Personnel Error.Governor Adjusted |
- on 910826,switchyard Transformer Fault Occurred Resulting in Loss of 4160 Volt Transfer Buses,Start of EDGs & Identification of EDG Underspeed Condition.Caused by Personnel Error.Governor Adjusted
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(o)(2)(i) | | 05000280/LER-1991-019, :on 910828,through-wall Crack Discovered in Component Cooling Water Supply to Reactor Shroud Cooler B.On 910827,RCS Loop B Instrumentation Behaved Erratically.Caused by Leak in Piping.Piping Will Be Replaced |
- on 910828,through-wall Crack Discovered in Component Cooling Water Supply to Reactor Shroud Cooler B.On 910827,RCS Loop B Instrumentation Behaved Erratically.Caused by Leak in Piping.Piping Will Be Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-020, :on 910821,potential Failure of Charging/High Head Safety Injection Pumps to Start Automatically in DBA Identified.Caused by Inadequate Review of Interlock Design. Operational Changes Being Reviewed |
- on 910821,potential Failure of Charging/High Head Safety Injection Pumps to Start Automatically in DBA Identified.Caused by Inadequate Review of Interlock Design. Operational Changes Being Reviewed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000280/LER-1991-021, :on 911028,discovered Emergency Diesel Generator 1 Room Rear Exit Door Tied Open & Fire Suppression Sys Inoperable.Caused by Contractor Personnel Error.Signs Installed on Both Sides of Door |
- on 911028,discovered Emergency Diesel Generator 1 Room Rear Exit Door Tied Open & Fire Suppression Sys Inoperable.Caused by Contractor Personnel Error.Signs Installed on Both Sides of Door
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(iv) 10 CFR 50.73(o)(2)(v) | | 05000280/LER-1991-022, :on 911204 Discovered That Containment Spray Pumps Had Not Been Demonstrated Operable Between 910101 & 0514,exceeding 92 Day Interval Between Surveillance Tests. Caused by Personnel Error.Task Team Formed |
- on 911204 Discovered That Containment Spray Pumps Had Not Been Demonstrated Operable Between 910101 & 0514,exceeding 92 Day Interval Between Surveillance Tests. Caused by Personnel Error.Task Team Formed
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