05000277/LER-1982-021, Forwards LER 82-021/03L-0.Detailed Event Analysis Encl

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Forwards LER 82-021/03L-0.Detailed Event Analysis Encl
ML20064M778
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 08/25/1982
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20064M781 List:
References
NUDOCS 8209080100
Download: ML20064M778 (2)


LER-2082-021, Forwards LER 82-021/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2772082021R00 - NRC Website

text

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.. . t PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET P.O. BOX 8699 PHILADELPHIA. PA.19101  ;

I (2 t 51 e414003 August 25, 1982 Mr. R. C. Haynes, Administrator Region I Office of Inspection & Enforcemont U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406

Dear Mr. Haynes:

This LER deals with local leak rate testing during the refueling outage on Peach Bottom Unit 2. Combined leakage for the Appendix J Type B&C testing exceeded 0.6 La. Table I shows a summary of failed valves. Technical Specification 6.9.a.3 requires reporting of " Abnormal degradation discovered in fuel cladding, reactor coolant pressure boundary, or primary containment" promptly. However, it has been agreed to in the past with various NRC inspectors that the resulta of failed LLRT's conducted during outages would be reported within thirty days with multiple failures reported on one report, when possible.

Due to some degree of confusion and misunderstanding concerning the reporting requirements for Local Leak Rate Testing conducted during outages when primary containment integrity is not required, we are late with this report. We apologize for any inconvenience this may hava caused you.

Sincerely, k f M. J. Cooney Superintendent Generation Division-Nuclear JCN:lmd 1

cc: Director, NRC - Office of Inspection & Enforcement Mr. Norman M. Haller, NRC - Office of Management &

Program Analysis C. J. Cowgill, Site Inspector 8209080100 20825 3,1 PDFi ADOCK 05000277 f4 S 8 PDR

., I PEACH POTTOM Unit 2 4

Valve Name Malfunction Main Steam Line Drain MO-74 Improper Seating HPCI Pump Discharge MO-23-19 Improper Seating RCIC Pump Discharge MO-13-20 Improper Seating HPCI Turbine Exhaust Swing Check 23-65 Improper Seating Chilled Water Supply to Drywell MO-22-OlA Crud Buildup HPCI Turbine Exhaust Test Tap Improper Seating Drywell Floor Drain Pump Discharge Test Tap Improper Seating i

MSIV 80B Inboard Improper Seating Due to Damage Seats Plugs and Guides MSIV 80C Inboard Improper Seating Due to Damage S'ats Plugs and Guides MSIV 80D Inboard Improper Seating Due to Damage Seats Plugs and Guides

! NOTE: All valves repaired, retested satisfactorily and returned to service.

JCN:8/23/82 I

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