LER-1981-035, Forwards LER 81-035/01T-0.Detailed Event Analysis Encl |
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PHILADELPHI A ELECTRIC COMPANY p
k 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 1881 -1981 1215)841-4000 July 6, 1981 Mr. Boyce H.
Grier, Director Office of Inspection and Enforcement Region I US Nuclear Regulatory Ccmmission 631 Park Avenue King of Prussia, PA 19406 SUBJECT: LICENSEE EVENT REPORT NARRATIVE DESCRIPTION
Dear Mr. Grier:
The following occurrence was reported to Mr. Knapp, Region I, Office of Inspection and Enforcement on June 22, 1981.
Reference:
Docket No. 50-277 Report No.:
2-81-35/1T-0 Report Date:
July 6, 1981 Occurrence Date:
June 22, 1981 Facility:
Peach Bottom Atomic Power Station RD #1, Delta, PA 17314 Technical Specification Reference:
Technical specification 3.8.C.1 states that, "The release rate of gross activity except for halogens and particulates with half lives longer than eight days shall not exceed:
Os E y
Qiv MPC( i 1
+
0.24 2.0 x 105 Where:
Os = combined units 2 and 3 off gas stack release rate in Ci/sec.
'T 6D average Y energy of release in Mev.
E
=
4
/
8108030430 810706 PDR ADOCK 05000277 S
PDR
i o
o Page 2 e
Qiv = combined units 2 and 3 release rate in i
Ci/sec from reactor building ventilation exhaust i
stack.
MPC'. = as defined for radionuclide i in column 1, Table II of Appendix B 10 CFR 20 assuming a 10 minute old off gas mixture."
i 1,
Description of the Event:
)
On 6/21/81 the recombiner mechanical compressors tripped due to high hydrogen gas levels downstream of the recombiner.
This resulted in the recombiner mechanical compressor suction header pressure increasing to a positive level.
When this happened, a release occurred through the Unit 3 reactor building vent, with activity levels w.ithin Tech. Spec. limits.
On 6/22/81, as previously reported in the Prompt Notification of l
this event, a second release occurred shortly after Unit 2 had shutdown automatically due to loss of a plant load bus.
The i
plant load bus which was lost also caused the trip of a recombiner mechanical compressor resulting in the compressor 1
suction line pressure again increasing to a positive value, and this again caused leakage to occur which resulted in a release which exceeded Tech. Spec. limits.
The Unit 3 roof vent monitor spiked for a seven minute period at 0930 AM on 6/22/81, releasing 12 mci /sec. peak (6.6 mci /sec.
average) for a total release of 2.8 curies during the peak period l
(182% of Tech spec limit).
The peak tailed off above background i
for three hours releasing 0.760 mci /sec. average for a total l
release of 8.6 curies over the tailing off period.
The total i
release over the entire period is calculated to be 11.4 curies.
l Four additional releases well within Tech. S.nc. limits, occurred j
between 6/2?/81 and 6/29/81 with a total ca'aalated additional j
release of 3.0 curies.
Analysis of roof vent iodine and particulate samples indicates no ii increase in the relea:!-
m.e during any of the gaseous act v ty spikes.
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Page 3 Probable Consequences of the Occurrence All of the releases identified above were of short duration.
The maximum dose at the site boundary was.08 mR on 6/22/81 and the total offsite dose for all releases during this period is calculated to be approximately.14 mR.
Cause of the Event
On 6/21/81, the recombiner mechanical compressors tripped, allowing the compressor suction line pressure to increase to a positive level.
A release occurred with an instaneous peak 45%
of Tech. Spec. limits and total activity released of 6.65 Ci.
Initially, the sole cause of this occurrence was thought to be a leaking 2B recombiner mechanical compressor suction line snubber drain valve.
Pending repairs to the valve, suction pressure was controlled negative.
However, before repairs could be made, on 6/22/81 the compressota tripped off again, and the release in excess of Tech. Spec. limits as described in " Detailed Description of Event" o'.'Irred.
Subsequent to removal of the leaking valve and capping of the line, several more losses of recombiner system negative preasure resulted in releases well within Tech. Spec. limits.
The dates of the releases and activity released are:
Release 1 6/23/81 Instantaneous Peak - 1.4% Tech Spec limit Total Calculated Release - 0.09 Ci Release 2 6/23/81 Instantaneous Peak - 4.7% Tech Spec limit Total Calculated Release - 1.63 Ci Release 3 6/28/81 Instantaneous Peak - 4.5% Tech Spec limit Total Calculated Release - 0.6 Ci Release 4 6/29/81 Instantaneous Peak - 6.4% Tech Spec limit Total Calculated Release - 0.68 Ci Investigation identified two other leakage paths; through a i
mechanical compressor common suction line loop saal isolation valve, and through a condenser conductivity element' drain valve.
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Corrective Actions
on 6/22/81 the line associated with the leaking 2B mechanical compressor suction valve was cut upstream of the valve, and a pipe cap installed to preclude further leakage.
This was accomplished as a modification, as the line is used for maintenance purposes only.
Following trip of the recombiner mechanical compressors on 6/23/81 (Releases 1 and 2) a 1ormally closed mechanical compressor common suction line loop seal isolation valve was found cracked open.
(The loop seal was drained, since several other system drains had been added to the system after initial installation and this loop seal drain was no longer required).
This valve is in a location where it could be used as a foothold and may have been accidentally cracked open by someone trying to gain access to other equipment in the area.
The valve was wired cloced.
On 6/28/81 release 3 occurred.
A hydrogen analyzer valve gas inlet valve was found cracked open, and at the ti -
4' as thoucht that this could have provided a furt.her re pa for radioactive gases.
Upon closer exaainatio determined that any gases passing through the unlve would nave gone to the main condenser.
On 6/29/81, again following loss of recombiner system negative pressure, release 4 occurred.
Recombiner equipment drain sump airborne activity levels wera found to be abnormally high, and it was determined that the reconbiner condenser conductivity element drain valve which drains to this sump was cracked open approximately one quarter turn.
The valve was closed.
Subs =guent losses of recombiner negative pressure on 6/29/81 and 7/1/81 resulted in no appreciable increase in Unit 3 reactor building vent activity levels.
Very truly yours, J
? f g@t
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.jp. Cooney Spperintendent Gdneration Division / Nuclear cc:
Director, NRC - Office of Inspection and Enforcement Sr. Norman M. Haller, NRC - Office of Management &
Program Analysis l
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| 05000277/LER-1981-001-04, /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. Instructions Posted at Chlorination Control Panel,Procedure Clarified & Individual Reinstructed | /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. 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Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | /03L-0:on 810227,core Spray Logic Sys B Failed. Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | | | 05000277/LER-1981-006-03, /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | | | 05000278/LER-1981-007-03, /03L-0:on 810206,main Steam Line Monitor a Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. 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Monitor Calibr & Returned to Svc | | | 05000277/LER-1981-007-03, /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gain | /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gains | | | 05000278/LER-1981-008-01, /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | | | 05000278/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000277/LER-1981-008-03, /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | | | 05000278/LER-1981-009-03, /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | | | 05000277/LER-1981-009-03, /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | | | 05000277/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000277/LER-1981-010-03, /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | | | 05000278/LER-1981-011-03, /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | | | 05000278/LER-1981-012-03, /03L-0:on 810428,snubber from a Recirculation Pump Discharge Header Found to Have Locking Velocity Under Compression Less than Acceptable Value.Cause Not Determined. 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Monitor Calibr & Returned to Svc | | | 05000277/LER-1981-013, Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | | | 05000278/LER-1981-013-01, /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | | | 05000278/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000277/LER-1981-014-03, /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | | | 05000278/LER-1981-014, Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | | | 05000278/LER-1981-014-01, /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | | | 05000278/LER-1981-015-01, /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | | | 05000278/LER-1981-015, Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | | | 05000278/LER-1981-016-03, /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | | | 05000277/LER-1981-016-03, /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | | | 05000277/LER-1981-017-03, /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | | | 05000278/LER-1981-017-03, /03L-0:on 811109,reactor Core Isolation Cooling High Steam Flow Isolation Switch Exceeded Tech Spec Limit. 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Caused by Dirt Buildup on Seating Surface,Preventing Proper Valve Disc Seating.Valve Cleaned & Returned to Svc | | | 05000278/LER-1981-018-03, /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | | | 05000277/LER-1981-019, Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | | | 05000277/LER-1981-019-01, /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | | | 05000278/LER-1981-019-03, /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | | | 05000277/LER-1981-020-03, /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | | | 05000278/LER-1981-020-03, /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | | | 05000277/LER-1981-021-03, /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | | | 05000278/LER-1981-021-03, /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | | | 05000277/LER-1981-022-01, /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | |
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