LER-1981-005, Forwards LER 81-005/01T-0.Detailed Event Analysis Encl |
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e-Duxz Pown COMPA,NY Pows Bintmswo 422 Soeta Cnuncu Stazzr, CaAntortz, N. C. sea 4a S/- o/ 6 ^
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March 9, 1981
'" * *"* ' *!'/3,'.],3
, '[Q, Mr. James.P. O'Reilly, Director
,g U.S. Nuclear Regulatory Consnission Region II f 3Q ' ? Vj 101 Marietta Street, Suite 3100
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Atlanta, Ceorgia 30303.
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- j st Re: Oconee Nuclear Station
- 3. <r u n uoAAtott -?)
Q, Docket No. 50-269 y/t 1\\'/
Dear'Mr. O'Reilly:
- - 6 i Please find attached Reportable Occurrence Report R0-269/81-5. This report is submitted pursuant to Oconee Nuclear Station Technical Specification 6.6.2.1.a(9), which concerns the discovery of a conditton that requires cor-rective action to prevent the existence of a potentially unsafe condition.
Very truly yours, j'/ f/krYL h-William O. Parker, Jr.
FTP:pv Attachment Mr. Bill Lavallee cc: Director Office of Management & Program Analysis Nuclear Safety Analysis Center U. S. Nuclear Regulatory Commission P. O. Box 10412 Washington, D. C.
20555 Palo Alto, California 94303 Director Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D. C. 20555 l
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S 810701 O VD(o
DUKE POWER COMPANI OCONIE NUCLEAR STATION Report Number: R0-269/81-5 Report Date: " March 9, 1981 Occurrence Date: February 22, 1981 Facility: Oconee Unit 1, Seneca, South Caro)ina Identification of-Occurrence: Leaking LPI Check Valve
- Conditions Prior'to Occurrence:- RCS Heatup (N300*F, 750 pois)
Description of Occurrence: At approximately 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on February 22, 1981, a check valve in the Unit i Low Pressure Injection (LPI) System was discovered to be leaking excessively.during the performance of an intersystem LOCA leak test. The' leaking valve was 1 CF-12, which is the final valve in LPI, loop "B" before reaching the reactor vessel (see Figure 1).
The leakage of the valve is considered to constitute a condition that requires corrective action to prevent the existence of a potentially unsafe condicinn, and is thus re-l portable pursuant to Technical Specification 6.6.2.1.a(9).
Apparent Cause of Occurrence:
1 CF-12 is a 14-inch Crane Co. 1500 PSI Alloy Steel Swing Check Valve (design pressure of 2500 PSIG). Figure 2 provides i
some details about this type of valve. The disc *in this type of val *ve has a j
cylindrical " knob" on its back which is inserted through a hole in the hinge arm and then has a retainer ring welded to it to hold the assembly together 4
(see Figure 3). This method of assembly allows the valve disc to pivot to a certain extent on the hinge arm. By pivoting, the disc is allowed to find its seat properly should the mating surfaces become slightly altered. A manufactured tolerance of. 3.co 11. mils between the dise " knob" and the hinge at the pivot prevents the disc from swaying too freely.
Exsmination of the valva disc-hinge assembly in ! CF-12 has shown that the disc had become frozen at the pivot in a cocked position. Consequently, only about half of the dise was seating. The " freezing" of the disc at the
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pivot was apparently caused by a buildup of deposits in the gap between the hinge and the disc " knob" on the side of the knob closest to the hinge pin.
While there is flow through the valve, the disc is normally in a cocked i
position, and it is postulated that the flow could carry deposits into the l_
pivot gap area, where they could accumulate. The accumulation of deposits could then cause the disc to remain slightly cocked when the flow was stopped.
During examination of the valve disc, the retaining ring was rencved and un-successful attempts were made to remove the disc from che hinge.
Both the hinge and disc are made of the same type of stainless steel (ASTM Spec.
No. A351 GR. CF8M) and under the high temperature of unit operation, some j
galling could have occurred. At the time of chis report, the disc is still
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. Analysis of Occurrence: Prior to the testing of I CF-12, backup check valves 1 CF-11 and 1 LP-47 (see Figure 1) had been leak tested. and both had shown zero leskage. In addition, the LPI loop "B" motor operated valve 1 LP-18 was in its normal closed position during this period of time. Thus, the prevention of leakage from the RCS to the low prescure section of the LPI system was assured.
Examination of I CF-12 showed that although the disc was not seating properly, it remained capable of swinging up to its cocked position under LPI flow con-ditions. Additionally, all equipment required to mitigate the consequences of an accident at the conditions during the time of this incident were operable. Therefore, LPI flow through loop "B" was always available if needed.
1 CF-12 is the first valve, out of a total of 18 of the same type of valve leak tested-at Oconee, which has shown any leakage problem. During.the final preparation of this repart, another check valve of the same type was found to be leaking on Oconee Unit 3.
The details of this incident will be provided in a separate report. Duke Power Company will be continuing its investigation into the leakage problems observed with these two valves to determine if generic implications exist. Duke will keep the NRC informed of any signifi-cant developments during this investigation.
Corrective Action
The unit was re.t;ned to cold sh;tdown conditions so that the valve could be repaire'd. The valve seat of 1 CF-12 was lapped and the internals (disc, hinge, and hinge pin) were replaced with new parts. The valve was retested on March 2, 1981 and revealed zero leakage by the seat.
An analysis will be performed on the substance in the pivot gap of the valve to determine its origin. Extreme contamination of the 1 CF-12 internals, j
however, has made examination of these parts undesirable at this point with a
respect to personnel exposure. These parts remain in the Unit I reactor j
building. It is expected that examination of these it'.ernals will be feasible during the Unit l' refueling outage' scheduled for this summer. A report on the results of the analysis of the pivot gap substance in 1 CF-12 will be provided to tKe NRC when this information becomes available.
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| 05000269/LER-1981-001, Forwards LER 81-001/03L-0.Detailed Event Analysis Encl | Forwards LER 81-001/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-001-03, /03L-0:on 810105,turbine Trip from 90% Full Power Occurred.Caused by Loss of Excitation on Generator Field Resulting from Mismatch During Personnel Attempt to Raise Volt Amperes Reactive on Units 1 & 2 | /03L-0:on 810105,turbine Trip from 90% Full Power Occurred.Caused by Loss of Excitation on Generator Field Resulting from Mismatch During Personnel Attempt to Raise Volt Amperes Reactive on Units 1 & 2 | | | 05000270/LER-1981-001-03, /03X-1:on 810120,discovered That Low Pressure Svc Water Was Not Flowing to HPI Pump 2A.Caused by Blockage Due to Crud Buildup.Portions of Carbon Steel Piping Will Be Replaced W/Stainless Steel | /03X-1:on 810120,discovered That Low Pressure Svc Water Was Not Flowing to HPI Pump 2A.Caused by Blockage Due to Crud Buildup.Portions of Carbon Steel Piping Will Be Replaced W/Stainless Steel | | | 05000270/LER-1981-001, Forwards LER 81-001/03X-1.Detailed Event Analysis Encl | Forwards LER 81-001/03X-1.Detailed Event Analysis Encl | | | 05000270/LER-1981-002, Forwards LER 81-002/01T-0.Detailed Event Analysis Encl | Forwards LER 81-002/01T-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-002-01, /01T-0:on 810211,electrical Penetration EMV-2 Could Not Be Pressurized.Caused by Leak at Interior Bushing. Penetration to Be Repaired or Replaced During Next Outage | /01T-0:on 810211,electrical Penetration EMV-2 Could Not Be Pressurized.Caused by Leak at Interior Bushing. Penetration to Be Repaired or Replaced During Next Outage | | | 05000269/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-003-03, /03L-0:on 810125,dc Input Fuse in 1DID Vital Inverter Blew,Causing Inverter to Lose Power source.1DIB Inverter Tripped When Ac Output Breaker Apparently Opened. 1DID Trip Caused by Blown Fuse.Cause of 1DIB Trip Unknown | /03L-0:on 810125,dc Input Fuse in 1DID Vital Inverter Blew,Causing Inverter to Lose Power source.1DIB Inverter Tripped When Ac Output Breaker Apparently Opened. 1DID Trip Caused by Blown Fuse.Cause of 1DIB Trip Unknown | | | 05000287/LER-1981-003, Forwards LER 81-003/01T-0.Detailed Event Analysis Encl | Forwards LER 81-003/01T-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-003-01, /01T-0:on 810226,B Steam Generator Was Pressurized to 550 Psig.Caused by Procedural Deficiency. Once-through Steam Generator Pressure Lowered.Procedures for Opening Startup Block Valves Will Be Revised | /01T-0:on 810226,B Steam Generator Was Pressurized to 550 Psig.Caused by Procedural Deficiency. Once-through Steam Generator Pressure Lowered.Procedures for Opening Startup Block Valves Will Be Revised | | | 05000270/LER-1981-003-03, /03L-0:on 810302,alarm Sounded to Indicate High Temp on Reactor Bldg Cooling Unit.Caused by Grease Starvation.Reactor Bldg Cooling Unit 2C Was Secured & Grease Added to Motor Bearings.Cooling Unit Restarted | /03L-0:on 810302,alarm Sounded to Indicate High Temp on Reactor Bldg Cooling Unit.Caused by Grease Starvation.Reactor Bldg Cooling Unit 2C Was Secured & Grease Added to Motor Bearings.Cooling Unit Restarted | | | 05000270/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-004-03, /03L-0:on 810304,motor Driven Emergency Feedwater Pump 2B Was Declared Inoperable Due to Arcing in Motor.Cause Unknown.Motor Was Disassembled & Failure Found in Coil Slot | /03L-0:on 810304,motor Driven Emergency Feedwater Pump 2B Was Declared Inoperable Due to Arcing in Motor.Cause Unknown.Motor Was Disassembled & Failure Found in Coil Slot | | | 05000270/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-004-03, /03L-0:on 810212,primary Level Indication for Elevated Water Storage Tank Was Declared Inoperable Following Low Water Level Alarms.Caused by Loose Connectors on Air Compressor Starter Terminals.Connections Tightened | /03L-0:on 810212,primary Level Indication for Elevated Water Storage Tank Was Declared Inoperable Following Low Water Level Alarms.Caused by Loose Connectors on Air Compressor Starter Terminals.Connections Tightened | | | 05000269/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-004-03, /03L-0:on 810312,valve 3FDW-105 Failed to Close Electrically After Chemical Sampling of Steam Generator B. No Apparent Cause Found.Valve Manually Closed & Circuit Breaker Opened,Disabling Valve | /03L-0:on 810312,valve 3FDW-105 Failed to Close Electrically After Chemical Sampling of Steam Generator B. No Apparent Cause Found.Valve Manually Closed & Circuit Breaker Opened,Disabling Valve | | | 05000287/LER-1981-004, Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | Forwards LER 81-004/03L-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-005-03, /03L-0:on 810323,engineering Safeguard Valve 3CS-5 Failed to Operate.Caused by Operator Failure Since Valve Could Be Operated Manually.Valve Operator Will Be Inspected During Next Outage | /03L-0:on 810323,engineering Safeguard Valve 3CS-5 Failed to Operate.Caused by Operator Failure Since Valve Could Be Operated Manually.Valve Operator Will Be Inspected During Next Outage | | | 05000287/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-005, Forwards LER 81-005/01T-0.Detailed Event Analysis Encl | Forwards LER 81-005/01T-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-005, Forwards LER 81-005/01T-0.Detailed Event Analysis Encl | Forwards LER 81-005/01T-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-005-01, /01T-0:on 810222,low Power Injection Check Valve Discovered Leaking Excessively During Intersystem LOCA Leak Test.Caused by Buildup of Crud in Pivot Gap Area.Disc Hinge & Hinge Pin Replaced.Crud to Be Analyzed | /01T-0:on 810222,low Power Injection Check Valve Discovered Leaking Excessively During Intersystem LOCA Leak Test.Caused by Buildup of Crud in Pivot Gap Area.Disc Hinge & Hinge Pin Replaced.Crud to Be Analyzed | | | 05000270/LER-1981-005-01, /01T-0:on 810318,four Closure Studs on Reactor Coolant Pump 2A2 Had Corrosion Wastage in Pump Closure Area. Caused by Leakage from Pump Closure Gaskets.Stud 20 Replaced.Studs 1,2 & 3 Left in Place | /01T-0:on 810318,four Closure Studs on Reactor Coolant Pump 2A2 Had Corrosion Wastage in Pump Closure Area. Caused by Leakage from Pump Closure Gaskets.Stud 20 Replaced.Studs 1,2 & 3 Left in Place | | | 05000270/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-006-03, /03L-0:on 810409,valve 2PR-8 Failed to Open During on-line Insp.Caused by Faulty Valve Operator Diaphragm.Valve Repaired & Verified Operable | /03L-0:on 810409,valve 2PR-8 Failed to Open During on-line Insp.Caused by Faulty Valve Operator Diaphragm.Valve Repaired & Verified Operable | | | 05000287/LER-1981-006, Forwards LER 81-006/03X-1.Detailed Event Analysis Encl | Forwards LER 81-006/03X-1.Detailed Event Analysis Encl | | | 05000287/LER-1981-006-03, /03X-1:on 810324,reactor Protection Sys Channel a High Pressure Trip Found Out of Calibr.Caused by Transmitter Drift.Pressure Transmitter Recalibr | /03X-1:on 810324,reactor Protection Sys Channel a High Pressure Trip Found Out of Calibr.Caused by Transmitter Drift.Pressure Transmitter Recalibr | | | 05000269/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-006-03, /03L-0:on 810328,RCS Subcooling Margin Monitors Were Discovered Inoperable When Computer Alarm Printer & Rider in Control Room Indicated All Analog Points in Alarm Condition.Caused by Failed Low Level Amplifier | /03L-0:on 810328,RCS Subcooling Margin Monitors Were Discovered Inoperable When Computer Alarm Printer & Rider in Control Room Indicated All Analog Points in Alarm Condition.Caused by Failed Low Level Amplifier | | | 05000269/LER-1981-007-01, /01T-0:on 810410,fire Barrier Door for West Penetration Room Was Inoperable W/O Proper Fire Watches Maintained.Caused by Personnel Error.Individual Involved Counseled Re Importance of Communication | /01T-0:on 810410,fire Barrier Door for West Penetration Room Was Inoperable W/O Proper Fire Watches Maintained.Caused by Personnel Error.Individual Involved Counseled Re Importance of Communication | | | 05000269/LER-1981-007, Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-007, Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | Forwards LER 81-007/01T-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-007-03, /03L-0:on 810329,inner Door Seal of Reactor Bldg Personnel Lock Found to Leak at Rate Greater than That Allowed by Procedure.Caused by Faulty Installation of Strong Backs.Gasket Shinned & Strong Backs Reinstalled | /03L-0:on 810329,inner Door Seal of Reactor Bldg Personnel Lock Found to Leak at Rate Greater than That Allowed by Procedure.Caused by Faulty Installation of Strong Backs.Gasket Shinned & Strong Backs Reinstalled | | | 05000270/LER-1981-007-01, /01T-0:on 810326,during Periodic Test,Auto/Manual Transfer Switches for B1T-8 & B2T-5 Incorrectly Placed in Manual Position & Not Returned After Test Completion.Caused by Personnel Error.Switches Restored to Auto Position | /01T-0:on 810326,during Periodic Test,Auto/Manual Transfer Switches for B1T-8 & B2T-5 Incorrectly Placed in Manual Position & Not Returned After Test Completion.Caused by Personnel Error.Switches Restored to Auto Position | | | 05000287/LER-1981-008-03, /03L-0:on 810422,during Seismic Block Wall Insp, Discovered Breach of Fire Barrier in Penetration 3-T-T-1. Caused by Pulling of Electrical Cables Through Barrier. Breach Repaired Using RTV Foam | /03L-0:on 810422,during Seismic Block Wall Insp, Discovered Breach of Fire Barrier in Penetration 3-T-T-1. Caused by Pulling of Electrical Cables Through Barrier. Breach Repaired Using RTV Foam | | | 05000269/LER-1981-008-01, /01T-0:on 810513,loss of Valve Position Noticed. Valve CCW-8 Determined to Be Electrically Inoperable.Caused by Open Circuit in Several Conductors in Control Cable. Control Cable Replaced & Valve Electrically Cycled | /01T-0:on 810513,loss of Valve Position Noticed. Valve CCW-8 Determined to Be Electrically Inoperable.Caused by Open Circuit in Several Conductors in Control Cable. Control Cable Replaced & Valve Electrically Cycled | | | 05000270/LER-1981-008-03, /03L-0:on 810508,solenoid Valve for 2FDW-316 Stuck in Manual Position,Disabling Automatic Level Control of B Steam Generator from Emergency Feedwater Sys.Valve Replaced Per Procedure | /03L-0:on 810508,solenoid Valve for 2FDW-316 Stuck in Manual Position,Disabling Automatic Level Control of B Steam Generator from Emergency Feedwater Sys.Valve Replaced Per Procedure | | | 05000287/LER-1981-008, Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | | | 05000270/LER-1981-008, Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-008, Forwards LER 81-008/01T-0.Detailed Event Analysis Encl | Forwards LER 81-008/01T-0.Detailed Event Analysis Encl | | | 05000269/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Analysis Encl | Forwards LER 81-009/03L-0.Detailed Analysis Encl | | | 05000287/LER-1981-009-03, /03L-0:on 810507,containment Isolation Valve 3CS-6 Was Discovered in Intermediate Position,Resulting in Loss of Containment Integrity.Cause Undetermined.Valve 3CS-6 Verified Operable | /03L-0:on 810507,containment Isolation Valve 3CS-6 Was Discovered in Intermediate Position,Resulting in Loss of Containment Integrity.Cause Undetermined.Valve 3CS-6 Verified Operable | | | 05000269/LER-1981-009-03, /03L-0:on 810622,during Normal Operations,Startup Transformer CT-1 Locked Out.Cause Not stated.CT-1 Transformer & Bus Work Checked & Protective Relaying Checked for Malfunction Prior to Return to Svc | /03L-0:on 810622,during Normal Operations,Startup Transformer CT-1 Locked Out.Cause Not stated.CT-1 Transformer & Bus Work Checked & Protective Relaying Checked for Malfunction Prior to Return to Svc | | | 05000270/LER-1981-009-03, /03L-0:on 810415,during Low Pressure Svc Water Pump Periodic Test,Valves 2LPSW-19 & 2LPSW-21 Were Closed Resulting in RB Rbcu Being Out of Svc.Caused by Personnel Error.Valve 2LPSW-19 Opened & Personnel Counseled | /03L-0:on 810415,during Low Pressure Svc Water Pump Periodic Test,Valves 2LPSW-19 & 2LPSW-21 Were Closed Resulting in RB Rbcu Being Out of Svc.Caused by Personnel Error.Valve 2LPSW-19 Opened & Personnel Counseled | | | 05000287/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | | | 05000287/LER-1981-010-03, /03L-0:on 810517,broken Airline to Valve 3LPSW-525 Was Discovered.Caused by Breakage of Brass Nipple Between Air Supply Isolation Valve & Accumulator Tank.Brass Nipple Replaced | /03L-0:on 810517,broken Airline to Valve 3LPSW-525 Was Discovered.Caused by Breakage of Brass Nipple Between Air Supply Isolation Valve & Accumulator Tank.Brass Nipple Replaced | | | 05000269/LER-1981-010-03, /03L-0:on 810602,turbine Driven Emergency Feedwater Pump Declared Inoperable.Caused by Governor Valve Sticking in Open Position Due to Sys Contamination.Linkage Pin Removed,Governor Valve Freed & Stem Cleaned | /03L-0:on 810602,turbine Driven Emergency Feedwater Pump Declared Inoperable.Caused by Governor Valve Sticking in Open Position Due to Sys Contamination.Linkage Pin Removed,Governor Valve Freed & Stem Cleaned | | | 05000269/LER-1981-010, Forwards LER 81-010/03L-0.Detailed Event Analysis Encl | Forwards LER 81-010/03L-0.Detailed Event Analysis Encl | |
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