LER-1982-043, Forwards LER 82-043/03L-0.Detailed Event Analysis Encl |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2671982043R00 - NRC Website |
|
text
.
ptIniie service conipaniy e cenetniosa 16S05 Road 19 1/2, Platteville, Colorado 80651-9298 November 24, 1982 Fort St. Vrain Unit No. 1 P-82531 i
Mr. John T. Collins, Regional Administrator Region IV Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Reference:
Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Collins:
Enclosed please find a copy e'
Reportable Occurrence Report No. 50-267/82-043, Final, submitted par the requirements of Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/82-043.
V y truly yours, l
1D Don Warembourg Manager, Nuclear Production DW/cis Enclosure ce Director, MIPC h
QCobNhp f
O 8212200123 821124 PDR ADOCK 05000267 S
PDR
x k
F REPORTABLE OCCURRENG DISTRIBUTIM mmbe r o f Coo t es Dep ar tmen t o f Ene r gy - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Letter)
San Francisco operations Of fice Attn: California Patent Group 1333 3 roadway Oakland, California 96612 De p a r t:e n t o f En e r gy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Letter)
Mr. Glen A. Newby, Chie f HTR 3 ranch Division of Nuclear Pcwer Development Mail Station 5-107 Washin gton, D.C.
20545 De p a r t :ne n t o f En e r gy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - a (P latter)
Attn : Project Manager P. O. Box S1608 San Diego, California 92138
!!r. John T. Collins, Regional Administrator 1 Original of P latter)
P4sien IV Nuclear Pegulatory Cornission 611 Ryan Plaza Drive S uite 1000 Arlin gt on, Te xas 76011 M r. Ge o r ge K uz:rr e z - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P tatter)
Nuclear Regulatorv Co-.is sion 7920 Norf olk Avenue Be thesda, Maryland 20034 Di r e c t o r - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Le t te r)
Of fice of Management Information sad Program Control Nuclear Regulatory Comission Washington, D.C.
20555 INPO Records Center 1 (P Letter)
Suite 1500 1100 circle 75 Parkvay Atlanta, GL 30339 Mr. Richa rd Phe lp s FS7, CA. S i te Rep re sen t ative - - - - - - - - - - - - - - - -
1 (P Letter)
General Atomic Cocoany 16864 Weld County Road 191/2 Platteville, Colorado 80651 NRC Resident Site Inspector 1 (P Letter)
)
1 l
O
=
~
REPORT DRTE:
Noven6er 24,1982 REPORTABLE OCCURRENCE 82-043 ISSUE 0 OCCURRENCE DATE:
October 28, 1982 Page 1 of 3 FORT ST. VRAIN NUCLEAR GENERATING STATION i
PUBLIC SERVICE COMPANY OF COLORADO l
16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT NO. 50-267/82-043/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
On October 27, 1982, and October 28, 1982, with the reactor shutdown, the average of the prestressed concrete reactor vessel cooling water system (System 46) inlet and outlet temperatures in both loops fell below 100 degrees fahrenheit. This constitutes a degraded mode of LCO 4.2.15(e) and is being reported per Fort St. Vrain Technical Speci fication AC 7.5.2(L,'2.
EVENT
DESCRIPTION
On October 25, 1982, with auxiliary boiler #2 already out of service, auxiliary boiler #1 was also taken out of service for maintenance.
Since a portion of the steam supply from these boilers is used to control water temperatures in the PCRV cooling water system (System 46) during shutdown conditions when reactor heat is insufficient to do so, the loss of the boilers caused the average of the System 46 inlet and outlet water temperatures to trend toward the 100 degrees fahrenheit minimum allowed by LCO 4.2.15(e).
This downward trend continued until Loop 2 of System 46 was manually shutdown at 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br /> on October 26, 1982. The reduced heat removal rate that resulted from this action was sufficient to stabilize the Loop 1 average temperature at a value slightly above the 100 degrees fahrenheit limit.
Cooling water flow through Loop 2 of System 46 was re-established on October 27, 1982, at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> with the idea that auxiliary boiler
- 1 was being returned to service. Due to the fact that the boiler was not returned to service until 1455 hours0.0168 days <br />0.404 hours <br />0.00241 weeks <br />5.536275e-4 months <br /> the same day, the average of the inlet and outlet water temperatures in Loop 2 of System 46 remained less than the 100 degrees fahrenheit minimum from the time that flow had been re-established. The presence of water in the line from the boiler to the System 46 surge tank further inhibited the supply of steam to the System 46 surge tanks. As a result, the average temperature in Loop 1 of System 46 also fell
(
below the 100 degrees fahrenheit limit at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.
Additional problems were experienced in the early morning hours of October 28, 1982, with malfunctioning auxiliary boiler feedpumps, and
~
REPORTABLE OCCURRENCE 82-043 ISSUE O Page 2 of 3 consequently, heating of the System 46 surge tanks was not observed until approximately 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />.
Loop 1 of System 46 returned to full compliance with LCO 4.2.15(e) at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />, and Loop 2 at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on October 28, 1982.
The reactor remained in a cold shutdown condition throughout the event.
CAUSE
DESCRIPTION:
Equipment malfunction.
Operator error.
The residual decay heat production rate from the reactor was, by itself, insufficient to maintain the loop averages of the PCRV cooling water system inlet and outlet temperatures above the 100 degrees fahrenheit minimum specified in LCO 4.2.15(e) when both of the loops were in service. To maintain the loop averages above 100 degrees fahrenheit with more than one loop in service, auxiliary heat was required but was not immediately available due to equipment malfunctions. As a result of these malfunctions and the failure of the operating personnel to remove a System 46 loop from service, when it was apparent insufficient heat was available, the loop averages fell below the 100 degrees fahrenheit minimum.
CORRECTIVE ACTION:
Auxiliary boiler #2 was put in service to increase the heat input to the PCRV cooling water system.
Correct operation of the PCRV cooling water system during all conditions will be reviewed with all Licensed Operators by the Training De-e*-ent.
No further corrective action is anticipated or required.
i, i
~~
\\
REPORTABLE OCCURRENCE 82-043 ISSUE O Page 3 of 3 i
i Q
f f
%E l
1
_6 t--
Prepared By:
v.u Pau? A/ Tramp Techafcal Services Technician Reviewed By:
<//[m C?iaries Fuller Technical Services Engineering Supervisor
/
Reviewed By:
Edwin 0. Hill Station Manager Approved By:
>*/f/
////
a9t < ~
Do~n Wafembourg
/~
Manager, Nuclear *9roduction
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000267/LER-1982-001-03, /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | | | 05000267/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002-03, /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-003-03, /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | | | 05000267/LER-1982-004-01, /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | | | 05000267/LER-1982-004, Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005-03, /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | | | 05000267/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-006-03, /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | | | 05000267/LER-1982-007, Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-007-01, /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | | | 05000267/LER-1982-008-03, /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | | | 05000267/LER-1982-009-03, /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | | | 05000267/LER-1982-010-03, /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | | | 05000267/LER-1982-011-03, /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | | | 05000267/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-012-03, /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | | | 05000267/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013-03, /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | | | 05000267/LER-1982-014-03, /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | | | 05000267/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-015-03, /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | | | 05000267/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-016-03, /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | | | 05000267/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-017-03, /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to S | /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to Svc | | | 05000267/LER-1982-018-03, /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | | | 05000267/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-019-03, /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-020-03, /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | | | 05000267/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-021-03, /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | | | 05000267/LER-1982-022-03, /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | | | 05000267/LER-1982-023-03, /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | | | 05000267/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-024, Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | | | 05000267/LER-1982-024-03, /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | | | 05000267/LER-1982-025, Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | | | 05000267/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-026-03, /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | | | 05000267/LER-1982-027-03, /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | | | 05000267/LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028, Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028-03, /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | | | 05000267/LER-1982-029-03, /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | |
|