LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2671982014R00 - NRC Website |
|
text
__
r public Servlee Company fOdsudD 16805 Road 19 1/2, Platteville, Colorado 80651-9298 May 17, 1982 Fort St. Vrain Unit No. 1 P-82149
- [N
--IhI_N kM[$.
r.
U$
p il MAY 701982 Mr. John T. Collins, Regional Administrator dN Region IV Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Reference:
Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Collins:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/82-014, Final, submitted per the requirement. of Technical Specification AC 7.5.2(b)2 and AC 7.5.2(b)4.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/82-014
//
Very truly yours, 16W r
Don Warembourg Manager, Nuclear Production DW/cis Enclosure cc: Director, MIPC
'@a 8205260028 8
~ -
REPORT DATE:
May 17, 1922 REPORTABLE OCCURRENCE 82-014 ISSUE O OCCURRENCE DATE:
Aoril 17, 1982 Page 1 of 5 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE CONPANY OF COLORADO 16805 WELO COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT NO. 50-267/82-014/03-L-0 Final IDENTIFICATICN OF 3
OCCURRENCE:
During the period from April 17, 1982, to April 26, 1982, the reactor was operated at power with only one complete prestressed concrete reactor vessel (PCRV) liner cooling loop operating. This condition occurred on several separate occasions, each of which was terminated within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.
These occurrences were necessary to determine a.
primary coolant to liner cooling system leakage path.
Since it was necessary to maintain the reactor at power operation with only one complete operating prestressed concrete reactor vessel liner cooling i
loop, these events constituted degraded modes of LCO 4.2.13.
This 4
occurrence is reportable per AC 7.5.2(b)2 and AC 7.5.2(b)4 of the Technical Specifications.
i EVENT CESCRIPTION:
On April 13, 1982, while commencing a normal reactor and plant startup, an alarm was received indicating high pressure within the prestressed concrete reactor vessel liner cooling system, System 46, Loop 1, subheader outlet plenum.
Upon investigation, the outlet pressure of the liner cooling pumps was higher than normal. A sample for radioisotopes was taken from the System 46, Loop 1 cooling system.
The results indicated the presence of several radioactive isotopes, the longest-lived being Xenon-133, with the probable source being primary coolant.
All concentrations were below the maximum permissible concentration (MPC), and the surge tank was ventea via the gas waste release system to relieve pressure. The System 46, i
Loop 1 was sampled daily with the radioactive contamination reaching a maximum on April 16, 1982.
It was determined that a primary coolant leak into the prestressed concrete reactor vessel liner
+
cooling system, Loop 1, existed.
The contamination level was dependent on reactor power, temperature, and pressure conditions. Therefore, it was neces sa ry to keep the reactor at power operation, while isolating, draining, and sampling each subheader of Loop 1 to locate the leak.
Although the cooling capability and flow was never totally interrupted in Loop 1, since the subheaders were removed from the system and drained one at a
.<m.,,
mm--
.~.. -
m_.
. u.J 6
i j
i i
REPORTABLE OCCURRENCE 82-014 ISSUE 0 Page 2 of 5 l
l i
1
- time, it was concluded that Loop I was not considered a " complete" operating loop per LCO 4.2.13.
i
~
Commencing at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br /> on April 17, 1982, the process of isolating one subheader at a time of Loop 1 at various reactor power levels (all below 20%) began.
Upon isolating, draining, and sampling 4
f subheader No. 46237, radioactivity above background was detected.
l This subheader was the only one which showed a significant increase above background contamination. Subheader No. 46237 supplies cooling' water to the reactor core support floor within the prestressed 4
concrete reactor vessel. A su vey of individual tubes within the subheader isolated the leakage to within tube #F4T21. After locating this specific tube, the reactor was manually shutdown in order to facilitate repairs.
A repair and modification procedure was developed to isolate the affected tube from the liner cooling system and allow for future detection of possible primary coolant leakage i
from it.
This occurrence is reportable per AC 7.5.2(b)2 of the Technical Specifications as a degraded mode of LCO 4.2.13 due to having only one complete operating loop of the prestressed concrete reactor.
vessel liner cooling system during reactor power operation.
It is also reportable per AC 7.5.2(b)4 due to the abnormal leakage path through the core support floor liner into the prestressed concrete reactor vessel liner cooling system via a defective cooling tube.
l
CAUSE
DESCRIPTION:
The cause of the occurrence was leakage of primary coolant into the j
prestressed concrete reactor vessel liner cooling tube (F4T21) within subheader No. 46237 which supplies cooling water to the core support floor.
Leakage via this path requires that a slight defect must exist in both the support floor liner and the cooling tube.
Since the leakage was dependent on reactor power, temperature,- and pressure, it was necessary to isolate the subheaders during reactor power operation to identify the leak.
CORRECTIVE ACTION:
Each subheader of System 46, Loop 1, was isolated, drained, and 1
sampled to identify the leakage path. Each subheader was returned to 1
normal operation well within the 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> grace period of LCO 4.2.13.
At 0602 hours0.00697 days <br />0.167 hours <br />9.953704e-4 weeks <br />2.29061e-4 months <br /> on April 26, 1982, the reactor was manually shutdown, 3'
making LCO 4.2.13 no longer applicable.
4 4.--->.---,--w---
- - w m--
--.,,w-v
,e
..-.mer
., ~.., --.,,
.,,-c.
REPORTABLE CCCURRENCE 82-014 ISSUE 0 i
Page 3 of 5 The repair procedure which invnived capping both the inlet and outlet ends of tube FAT 21, was completed at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on May 2, 1982.
The associated modification provided an interspace on each end of the caoped tube and the acility to determine any possible future leakage within these interspacts.
(See Figure 1)
No further corrective action is anticipated or required.
m-
_ _ _ ~ _. - _
Figure lo Repair and modification to PCRV liner cool;ng tube /ff4T21 Public Service Conpany of Colorado Change flotice
- 1496
/
/
ls N
\\
s Tube F4T21 Tube F4T21
\\
\\
Outlet Inlet
.x 6
A L JN
\\
h
\\
x 3
s s
N s
IftflER SEAL CAPS
\\
\\
K N
s
\\
IrlTERSPACES FORMED W/ / / / / / /
/ / / / / / /1 4
~ DY T10DI FICATI0fl
\\
\\
\\
\\\\\\\\'
i\\\\
kN\\\\\\ ~\\\\\\\\
/I V
/I OUTER SEAL CAPS
/
/
/
/
/
/
/
/
/
/
/
/
/
/
/
f 9
P
~
2'C;A mmu
--[
IllDIVIDUAL IllTERSPACE ISOLATI0ft VALVES [o$
E m
o R
E 58 rT1 IllTERSPACE PPESSURIZATI0ft co7 ISOLATI0ft YALVE S
- flot drawn to scale - OJC From: Purifled Helium System
. -- _-. -.. ~ -
REPORTABLE CCCURRENCE 82-014 l
ISSUE O Page 5 of 5 4
i i
l i
(
Prepared By:
u% k,
r i
Owen J. Q)yton G i
Technical Services Technician i
I Reviewed By:
/M'
/[
i Charles Fuller Technical Servica ngi er..g Supervisor i
/
i i
/
i i
Reviewed By:
[./
Edwin O(/W 11 7"
Station Manager 4
y Approved By:
YN MM/
~ ' ' '
Don Wareihacurg l
Manager, Nuclear reduction i
4 1
'I a
1 w--..-
,-r,--
7
.,,..,-,mw.,-,,,ne,
.,-,,--~4
,.-.-m,-,--,,--,-y.-
'm&
---a-'mw-e* -
+-a-----+w
- - w-
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000267/LER-1982-001-03, /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | | | 05000267/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002-03, /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-003-03, /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | | | 05000267/LER-1982-004-01, /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | | | 05000267/LER-1982-004, Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005-03, /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | | | 05000267/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-006-03, /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | | | 05000267/LER-1982-007, Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-007-01, /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | | | 05000267/LER-1982-008-03, /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | | | 05000267/LER-1982-009-03, /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | | | 05000267/LER-1982-010-03, /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | | | 05000267/LER-1982-011-03, /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | | | 05000267/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-012-03, /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | | | 05000267/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013-03, /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | | | 05000267/LER-1982-014-03, /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | | | 05000267/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-015-03, /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | | | 05000267/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-016-03, /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | | | 05000267/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-017-03, /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to S | /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to Svc | | | 05000267/LER-1982-018-03, /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | | | 05000267/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-019-03, /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-020-03, /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | | | 05000267/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-021-03, /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | | | 05000267/LER-1982-022-03, /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | | | 05000267/LER-1982-023-03, /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | | | 05000267/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-024, Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | | | 05000267/LER-1982-024-03, /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | | | 05000267/LER-1982-025, Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | | | 05000267/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-026-03, /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | | | 05000267/LER-1982-027-03, /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | | | 05000267/LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028, Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028-03, /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | | | 05000267/LER-1982-029-03, /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | |
|