LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl |
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>s public Service Company Cf OcEcIreldo Yn 16805 Road 19 1/2, Platteville, Colorado 80651-9298 July 22, 1982 Fort St. Vrain Unit No. 1 P-82264
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All 2 61982 Mr. John T. Collins, Regional Administrator
- N Region IV Nuclear Dagulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Reference:
Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Collins:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/82-027, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)1 and AC 7.5.2(b)3..
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/82-027.
Very truly yours, hn kwl*
Don Warembourg Manager, Nuclear Production DW/cis Enclosure A
cc:
Director, MIPC h%
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8207290196 820722 PDRADOCK05000g s
REPORT DATE:
July 22, 1982 REPORTABLE OCCURRENCE 82-027 ISSUE O CCCURRENCE DATE:
June 28, 1982 Page 1 of 5
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FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT NO. 50-267/82-027/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
While performing a regularly scheduled Surveillance Test on primary coolant moisture monitor instrumentation sample flow alarm setpoints, an Instrument < Technician found 11 of the flow alarms were out of
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tolerance as specified by LCO 4.4.1, Table 4.4-1, note (t).
This event is reportable per Fort St.
Vrain Technical Specification AC 7.5.2(b)1 and AC 7.5.2(b)3.
EVENT j
DESCRIPTION
With the plant operating at 70% thermal power and 215 MW(e), plant Instrument Technicians performed the Primary Coolant Instrumentation Sample Flow Alarm Functional Test, SR 5.4.1.1.6e-M.
This test determines if the sample flow low and sample flow high alarm setpoints are correct and will alarm in the main Control Room.
Limiting Conditions of Operation 4.4.1, Table 4.4-1, note (t),
specifies that a dewpoint moisture monitor will not be considered operable unless the following conditions are met:
a) The fixed low-low sample flow alarms are set at 1 standard cubic centimeter per second.
b) The fixed high sample flow alarms are set at 75 standard cubic centimeters per second.
c) The variable low sample flow alarms are set at 1 to 50 standard cubic centimeters per second, depending on reactor power level.
i While performing the above mentioned Surveillance Test, one of the fixed low-low sample flow alarm setpoints was found below the 1 standard cubic centimeter per second limit, five of the fixed high sample flow alarm setpoints were found above the 75 standard cubic centimeters per second limit, and five of the variable low sample flow alarm setpoints were found below the 50 standard cubic centimeters per second limit as was specified for the reactor power level at the time the Surveillance Test was performed. The setpoints found for these flow alarms are listed in the attached tables, one through three.
REPORTABLE OCCURRENCE 82-027 ISSUE O Page 2 of 5 In reference to the attached tables, the fixed " low-low" sample flow alarm and the variable " low" sample flow alarms are actuated on decreasing voltage, and the fixed "high" sample flow alarms are actuated on increasing voltage.
Although the flow alarm setpoints were found out of tolerance, this did not prevent the fulfillment of the functional requirements of the dewpoint moisture monitors. The actual sample flows were verified to be above the minimum flow rates specified for 75% to 100% reactor power operation.
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e REPORTABLE OCCURRENCE 82-027 ISSUE 0 Page 3 of 5 TABLE 1 Low-Low Flow (1 sec/sec) i l Moisture l Monitor l Acceptance l
As l
As l
l Monitor I Loop 1
Criteria l
Found I Left l I
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1 l MM-1117 i Loop 1 1 0.08V - 0.13V I 0.006V l 0.108V l TABLE 2 High Flow (75 sec/sec) l Moisture l Monitor i Acceptance l
As l
As l
l Monitor i Loop i
Criteria l
Found i Left [
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l MM-1115 i High Level 1 4.06V - 4.16V l 5.11V I 4.15V l l
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1 l MM-1116 i Looo 1 1 4.09V - 4.19V l 4.28V l 4.15V l l
1 I
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i l MM-1119 i High Level i 4.06V - 4.16V I 4.34V I 4.11V [
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l I
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l MM-1120 i Loop 2 1 4.05V - 4.15V I 4.23V I 4.07V l l
l l
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l l MM-1122 l Loop 2 1 4.06V - 4.16V I 4.30V I 4.07V l TABLE 3 Low Flow (50 sec/sec) l Moisture l Mur. tor l Acceptance l
As l
As l
l Monitor I Loop 1
C9tteria l
Found l Left l 1
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l l MM-1115 i High Level i 2.99V - 3.09V I 2.02 V I 3.06V l l
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l 1
l l MM-1116 i Loco 1 l 2.93V - 3.03V I 0.897V l 3.01V l l
1 1
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i l MM-1119 I Hioh Level i 2.96V - 3.06V I 0.805V l 3.03V l l
l 1
1 I
I l MM-1120 i Loop 2 1 2.92V - 3.02V I 0.87 V I 3.00V l l
l 1
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l l MM-1122 l Loco 2 1 2.86V - 2.96V l 0.98 V l 2.90V l 1
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REPORTABLE OCCURRENCE 82-027 ISSUE 0 Page 4 of 5
CAUSE
DESCRIPTION:
The cause of this event, as far as the "high alarm setpoints are
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concerned, was instrument drift due to ambient conditions in that area of the Reactor Building.
Concerning the " low-low" and the variable " low" alarm setpoints, it has been determined there is a procedural inadequacy in the Overall Plant Operating Procedures, III and IV. The Reactor Operator was required only to verify correct moisture monitor sample flow without any verification of actual alarm setpoints.
CORRECTIVE ACTION:
The alarm set' points were re-adjusted to the correct values, and the Surveillance Test was completed satisfactorily.
The frequency of this test will be increased for a period of time until enough data can be gathered to verify a higher level of reliability.
Also, a change will be ini+* ted to the Overall Plant Operating Procedures, Sections III and IV.
Vs change will require that not only the actual sample flows be verified, but also the alarm setpoints have been reset by plant Instrument Technicians in accordance with reactor power level at that time.
As a precaution, the digital volt ~ meter used for the previous Surveillance Test of June 28, 1982, has been sent out for a
calibration recheck. When results of this check have been received, action will be taken as required.
No further carrective action is anticipated or required.
v.
w y,
REPORTABLE OCCURRENCE 82-027 ISSUE O Page 5 of 5
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Prepared By:
//ent.
Quane C.~Frye 47 Technical Services Technician Reviewed By:
hAldr,L id Charles Fuller TechnicalServicsEngine 'ing Supervisor
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Reviewed By:
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StatibnMana}gerEdwin/DL(H14 A" Approved By:
FwM Don Waremcourg
(/
Manager, Nuclear Production
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| 05000267/LER-1982-001-03, /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | /03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired | | | 05000267/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-002-03, /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-003-03, /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | /03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr | | | 05000267/LER-1982-004-01, /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | /01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators | | | 05000267/LER-1982-004, Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | Forwards LER 82-004/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-005-03, /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | /03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened | | | 05000267/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-006-03, /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | /03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels | | | 05000267/LER-1982-007, Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | Forwards LER 82-007/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-007-01, /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | /01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking | | | 05000267/LER-1982-008-03, /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | /03L-0:on 820228,nine Class 1 Snubbers Found Inoperable During Surveillance Testing of Hydraulic Shock Suppressors.Caused by Thermal Contraction &/Or External Seal Leakage.Snubbers Repaired as Required | | | 05000267/LER-1982-009-03, /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | /03L-0:on 820306,during Valve Lineup for Authorized Gas Waste Release,Some Gas Released Through Vacuum Tank.Caused by Valve Left Open During Preparations. Unsampled Release Terminated & Valve Lineup Corrected | | | 05000267/LER-1982-010-03, /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | /03L-0:on 820407 & 11,pure Helium Leakage in Steam Generator Interspace Found in Excess of Limits.Caused by Faulty Seal.Sys Modified | | | 05000267/LER-1982-011-03, /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | /03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage | | | 05000267/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-012-03, /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | /03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs | | | 05000267/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-013-03, /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | /03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned | | | 05000267/LER-1982-014-03, /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | /03L-0:between 820417 & 26,only One Complete Pcrv Liner Cooling Loop Was Operable.Caused by Isolating Loop 1 Subheaders to Locate Primary Coolant to Pcrv Liner Cooling Sys Leak.Extent & Cause of Tube Failure Unknown | | | 05000267/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-015-03, /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | /03L-0:on 820418 & 19,w/plant Operating at Power, Emergency Feedwater to Loop 2 Circulator Water Turbine Drives Were Isolated to Repair PV-21244 & PV-21244-1.Caused by Normal Wear,Resulting in Excessive Flow | | | 05000267/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-016-03, /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | /03L-0:on 820427,during Surveillance Testing,Class I Hydraulic Check & Sway Suppressor Snubber CRS-144 Found Inoperable.Caused by Seal & Gasket Leakage Allowing Loss of Hydraulic Oil.Snubber Rebuilt | | | 05000267/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-017-03, /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to S | /03L-0:on 820512,total Primary Coolant Oxidants Exceeded Tech Spec.Caused by Prolonged Maint Outage Allowing Power Operated Relief Valve Depressurization.Offgassing of Core Moisture/Oxidants Resulted When Plant Returned to Svc | | | 05000267/LER-1982-018-03, /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | /03L-0:on 820501,essential 480-volt Buses Tie Breaker Would Not Close During Surveillance Test Simulating Loss of Outside Power & Turbine Trip.Caused by Breaker Spring Charging Motor Switch in Off Position | | | 05000267/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-019-03, /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | /03L-0:on 820518,during Feedwater Flow Surveillance Test,Circulator 1A Speed Program Switch & Two Feedwater Flow Switches Were Out of Calibr.Caused by Instrument Drift.Switches Recalibr | | | 05000267/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | Forwards LER 82-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-020-03, /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | /03L-0:on 820517,w/reactor Operating at 40% Power & Pcrv Pressurized to Greater than 100 Psia,Primary & Secondary Interspace Penetration Pressure Decreased Below Allowable Limits.Caused by Impurities in Low Temp Absorber | | | 05000267/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | Forwards LER 82-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-021-03, /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | /03L-0:on 820517,plant Protective Sys Circulator Speed Module Found Reading Too Low.Caused by Loose Speed Switch Module Pin Connector,Which Made Poor Connection. Connector Reseated & Tightened in Place | | | 05000267/LER-1982-022-03, /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | /03L-0:on 820521,unplanned Radiological Releases from Reactor Bldg Exhaust Stack Occurred.Caused by Isolation Valve Closure Due to Personnel Error & Airborne Activity Entering Containment Tank Through Water Traps | | | 05000267/LER-1982-023-03, /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | /03L-0:on 820527,primary Coolant Oxidants Exceeded Tech Specs AC 7.5.2(b)2 on Three Separate Occasions.Caused by Gradual Ingress of Moisture & Oxidants.Moisture & Oxidant Offgassed from Core.Power & Temp Reduced | | | 05000267/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-024, Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | Forwards LER 82-024/03X-2.Detailed Event Analysis Encl | | | 05000267/LER-1982-024-03, /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | /03L-0:on 820605,all Three 480-volt Essential Buses Were Lost.Caused by Improperly Calibr Undervoltage Relays Due to Inadequate Relay Calibr Procedure.Procedure Updated | | | 05000267/LER-1982-025, Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | Forwards LER 82-025/03L-1.Detailed Event Analysis Encl | | | 05000267/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | Forwards LER 82-026/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-026-03, /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | /03L-0:on 820615,total Primary Coolant Oxidants Exceeded Limiting Conditions for Operation on Two Occasions. Caused by Water in Core Due to Sudden Pressure Surge from Loss of 480-volt Essential Busses.Concentrations Reduced | | | 05000267/LER-1982-027-03, /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | /03L-0:on 820628,11 Flow Alarms Found Out of Tolerance During Primary Coolant Moisture Instrumentation Sample Flow Alarm Function Test.Caused by Instrument Drift & Procedural Inadequacy.Setpoints Readjusted | | | 05000267/LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028, Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | Forwards LER 82-028/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1982-028-03, /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | /03L-0:on 820707,excessive Water Leakage Through PV-21244 Necessitated Isolation of Emergency Feedwater Supply Header.Caused by Water Cut in Valve Seat & Plug. Valve Ring Seat,Plug Assembly,Body & Seat Gaskets Replaced | | | 05000267/LER-1982-029-03, /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | /03X-1:on 820712,20 & 21,emergency Feedwater Headers to Helium Circulator Pelton Wheel Drives Isolated to Perform Maint on Leaking Header Safety Valves.Cause of Leakage Not Stated | |
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