05000265/LER-2003-003

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LER-2003-003,
Quad Cities Nuclear Power Station Unit 2
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2652003003R00 - NRC Website

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE Say Quad Cities Nuclear Power Station Unit 2 05400265 (if more space Fs reqdred, use additional ociples of NRC Forth 356AX1T)

PLANT AND SYSTEM IDENTIFICATION

General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].

EVENT IDENTIFICATION

Low Pressure Coolant Injection Differential Pressure Instrument Inoperable due to Misposition of Instrument Valve A. � CONDITION PRIOR TO EVENT Unit: 2 � Event Date: March 24, 2003 � Event Time: 2013 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.659465e-4 months <br /> Reactor Mode: 1 � Mode Name: Power Operation � Power Level: 100% Power Operation (I) - Mode switch in the RUN position with average reactor coolant temperature at any temperature.

E. � DESCRIPTION OF EVERT On June 20, 2003, during performance of a functional test on the Low Pressure Coolant Injection (LPCI) (B0] recirculation riser differential pressure switches [63], it was discovered that the high-side isolation valve (ISV) for one of the differential pressure switches was closed, rendering the instrument inoperable.

There are four of these differential pressure switches, and they provide a one-out- of-two-twice logic for the LPCI Loop Select System. This system directs the LPCI system to inject to the intact reactor recirculation pipe during a loss of coolant event.

The positions of the manifold valves on the other three switches were inspected, and the valves were found to be in their proper positions. Also, it was determined that no work was performed on these switches between March 24, 2003 and June 20, 2003.

Therefore, with the other three switches operable, the function was not lost.

The surveillance in progress was completed, the switch was tested satisfactorily and the manifold valves were returned to the in-service position.

A work history review identified that the last work performed that would have affected the mispositioned valve was completed on March 24, 2003; therefore, this event in reportable as a condition prohibited by Technical Specifications, since the instrument was inoperable longer than the allowed outage time.

A review of the March 24, 2003 surveillance test found that the steps for restoration and verification of proper restoration were signed. The two individuals who performed the surveillance on March 24, 2003, could not be interviewed, as they were no longer employed with Exelon Generation Company, LLC. A search of the work history involving these two individuals for any safety related work where they acted alone in the field or together with no other support was conducted. This review went back one year. No discrepancies were identified.

Immediate Actions

and Unit 2 were verified to be in the correct position.

All Instrument Maintenance crews were briefed on this issue as they came on shift.

Corrective Actions to be Completed Instrument Maintenance Department UMW Management will review and revise the IMD Human Performance Training Program and Dynamic Learning Activities to include more stringent guidelines and more stringent pass/fail criteria.

IMD Management will conduct paired field observations and provide remediation to personnel upon discovery of inadequate performance in use of the human performance tools.

IMD Management will develop a Human Performance improvement plan to include IND first-line supervisor performance.

F. PREVIOUS OCCURRENCES

No reportable events were identified during the last two years that involved a failure in the IMD to utilize human performance tools.

G. COMPONENT FAILURE DATA

There were no component failures associated with this event.

BAC FORM 366A 17-2001)