Similar Documents at Ginna |
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LER-2076-016, Rod Position Deviation Channel Was Found to Be Inoperable |
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| 2442076016R00 - NRC Website |
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text
CONTROL BLOCK:
LER 76-16/3L LICENSEE EVENT REPQPy t
(PLEASE PRINT ALLREQUIRED lMFORIVlATIOlIl),
1 s
6 LICENSEE NAME LCENSE NUMBER Q~g N
Y R
6 G Jl' 0 0 0
0 0
P p 7
89 14 15 LICENSE EVENT TYPE TYPE 0
4 1
1 1
1
~03 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE OOCI'ET NUMBER EVENT DATE REPORT DATE Ion~]com~
L
~L 0
5 0 0 2
4 4
0 5
2 0
7 6
0 6
0 4
7 6
7 8
57 58 59 60 61 68 69 74 75 80
EVENT DESCRIPTION
Q~g uring check of computer rod position program, rod position deviation channel was found 7
8 9 80 COD~]
to be inoperable.
A hand log was started as specified by Tech. Spec.
Table 3.5-1, Item 7
89 80 Qp~]
16a; Item 16b was still in service.
Computer technician re-initialized program and rod 7
8 9 80 Ioas]
position program check was completed satisfactorily.
The channel was deemed o~erahie 7
8 9 Qpg and the hand log terminated.
(Reportable Occurrence 50-244/76-16, 30-day).
80 80 7
89 SYSTEM
CAUSE
CODE CODE COMPONENT CODE [oar]~tF 6
I Ns T
R U
7 8 9 10 11 12 17 CAUSE DESCRIPTION [008]
he event was caused by a failure FAME COMPONENT SUPPUEA COMPONENT MANUFACTURER W
1 2
0 N
44 47 43 48 in. the computer to correctl monitor rod osition 80 7
8 9 [oOs) eviation.
Upon re-initializing, the computer pro ram was a ain found o erable.
7 89 80
~10 0 erator verification of Tech.S ec.-related ro rams in the cont'd. on attached sheet)
OTHER STATUS NA AMOUNT OF ACTIVITY OFFSITE CONSEQUENCES 7
89 FACiLITY STATUS POWER [gg E
~10 0
7 8
9 10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE Ittsj H
F NA 7
8 9
10 11 PERSONNEL EXPOSURES NUMBER TYPE
DESCRIPTION
~as ~00 0
Pi NA 7
8 9 11 12 13 PERSONNEL INJURIES NUMBER
DESCRIPTION
~to ~00 o
NA 7
89 11 12 METHOD OF DISCOVERY b
44 45 46 44, 45 DISCOVERY DESCRIPTION NA LOCATION OF RELEASE NA 80 80 80 80 80 Q~g 7
8 9 LOSS OR DAMAGE TO FACILITY TYPE OESCAIPTION Q~g
~H 7
89 10 PUBLICITY 89 NA 80 80 80 ADDITIONAL FACTORS Q~g Corrective Action Report 1080 has been initiated for this event.
7 89 7
89 Thomas A. Me er 80 PHDNE,7 1 6/546 2 700 ext.
29 1-206 GFO 80 I 6 GT
4(
II
Licensee Event Report Reportable Occurrence 50-244/76-16 Cause Descri tion (cont'd.)
computer willbe continued, and a Tech. Spec.
change willbe considered to eliminate further reports of this event when a suitable alternative is in effect.
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