Over a period of approximately one month, the OB Main Control Room ( MCR) Heating, Ventilating and Air Conditioning ( HVAC) system experienced four failures. Troubleshooting was completed for each of the failures and for three of the failures the cause was determined to be an intermittent dropout or chattering of the Loss of Offsite Power ( LOOP) start relay for two fans ( 0B-V116 MCR Supply and OB-V121 MCR Return Fans). The fourth failure was due to a contactor in the Motor Control Center ( MCC) for the OB-V116 MCR Supply Fan. On 11/29/16 the second failure occurred on the LOOP start relay for the OB-V116 MCR Supply fan. The investigation identified a manufacturing defect of the Agastat/Tyco ETR Relays in the lot of relays used for the recent preventative maintenance ( PM) relay replacements. The relays were determined to be unreliable since the initial PM replacement on 10/19/16 until 12/5/16, when the quality issue was identified and relays from a different lot were installed. The B train of MCR HVAC was determined to be inoperable due to the relay issue for a period of 47 days, which is greater than the allowable Limiting Condition for Operation (LCO) action window of 7 days (per TS 3.7.2.a.1) for an inoperable Control Room Emergency Fresh Air System ( CREFAS) train.
Therefore, this was a condition prohibited by Technical Specifications (TS). |
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Category:Letter
MONTHYEARIR 05000352/20243012024-02-0202 February 2024 Initial Operator Licensing Examination Report 05000352/2024301 and 05000353/2024301 IR 05000352/20230042024-01-31031 January 2024 Integrated Inspection Report 05000352/2023004 and 05000353/2023004 IR 05000352/20240112024-01-31031 January 2024 Information Request to Support Post-Approval Site Inspection for License Renewal; Inspection Report 05000352/2024011 ML24026A2962024-01-26026 January 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS)- Syrs, . ML24004A0342024-01-17017 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0026 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000352/20230102024-01-11011 January 2024 Age-Related Degradation Report 05000352/2023010 and 05000353/2023010 IR 05000352/20234012023-12-21021 December 2023 Cybersecurity Inspection Report 05000352/2023401 and 05000353/2023401 ML23321A2362023-12-14014 December 2023 Issuance of Amendment Nos. 262 and 224 Adoption of TSTF-477, Revision 3 and Associated Technical Specification Changes ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23333A2182023-11-29029 November 2023 Operator Licensing Examination Approval ML23325A2062023-11-21021 November 2023 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML23313A0432023-11-13013 November 2023 Summary of Regulatory Audit in Support of Amendment Request for Control Room Air Conditioning Technical Specifications ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums IR 05000352/20230032023-10-27027 October 2023 Integrated Inspection Report 05000352/2023003 and 05000353/2023003 and Independent Spent Fuel Storage Installation Inspection 07200065/2023001 ML23297A1722023-10-24024 October 2023 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000352/2024010 and 05000353/2024010 IR 05000352/20235012023-10-17017 October 2023 Emergency Preparedness Biennial Exercise Inspection Report 05000352/2023501 and 05000353/2023501 RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans ML23279A0612023-10-0505 October 2023 Paragon Energy Solutions LLC, Part 21 Final Report Re Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23276A5162023-10-0303 October 2023 Federal Emergency Management Agency Level 1 Finding from 2023 Evaluated Emergency Preparedness Exercise ML23275A1082023-09-29029 September 2023 FEMA Level 1 Findings Limerick NPP- Boyertown/Colebrookdale ML23241A9452023-09-27027 September 2023 Generation Station, Units 1 and 2 Regulatory Audit Plan Supporting Review of the Equipment Qualification Portion of Limerick Digital Instrumentation and Controls License Amendment Request ML23269A0522023-09-26026 September 2023 Request for Information and Notification of Conduct of IP 71111.21.N.04, Age-Related Degradation, Reference Inspection Report 05000352/2023010 and 05000353/2023010 ML23255A0952023-09-12012 September 2023 Resubmittal of License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) to Address ML23254A0242023-09-0606 September 2023 Paragon Energy Solutions LLC, Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23249A1002023-09-0606 September 2023 Requalification Program Inspection IR 05000352/20230052023-08-31031 August 2023 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2023005 and 05000353/2023005) ML23248A2082023-08-31031 August 2023 UFSAR Cover Page ML23242A2172023-08-30030 August 2023 Response to Request for Additional Information for Application to Adopt TSTF-477, Revision 3, Add Action for Two Inoperable Control Room AC Subsystems and Associated Technical Specification Changes NMP2L2851, Relief Request Associated with Successive Inspections for Generic Letter 88-01 / BWRVIP-75-A Augmented Examinations2023-08-25025 August 2023 Relief Request Associated with Successive Inspections for Generic Letter 88-01 / BWRVIP-75-A Augmented Examinations ML23228A0942023-08-16016 August 2023 Response to Request for Additional Information for Supplemental License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the . IR 05000352/20230022023-08-14014 August 2023 Integrated Inspection Report 05000352/2023002 and 05000353/2023002 ML23220A0182023-08-0808 August 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000352/2023401 and 05000353/2023401 RS-23-087, Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor2023-08-0404 August 2023 Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor ML23212B2362023-07-31031 July 2023 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System - WEC Documents ML23212B1052023-07-31031 July 2023 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation - Revise ML23202A2192023-07-21021 July 2023 Response to Request for Additional Information for Supplemental License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the . ML23193B0122023-07-20020 July 2023 Audit Plan in Support of Review of License Amendment Request and Exemption Request for Digital Instrumentation and Controls Installation Support (Epids L-2023-LLA-0025 and L-2023-LLE-0005) ML23187A0962023-07-19019 July 2023 Generation Station, Unit Nos. 1 and 2 - Revised Estimated Review Completion Date Concerning License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML23208A1522023-07-0606 July 2023 PEMA Letter Dated 7-6-23 Re Limerick Exercise 9-26-23 ML23177A2242023-06-26026 June 2023 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection . ML23145A1972023-06-23023 June 2023 Correction to the Renewed Facility Operating License Pages in Amendment Nos. 255, 256, 257, 258, 259, and 260 2024-02-02
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000352/LER-2017-0012017-01-27027 January 2017 Condition Prohibited by TS due to Parts Quality Issue, LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue 05000353/LER-2016-0012016-07-27027 July 2016 Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error, LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 05000352/LER-2016-0032016-05-18018 May 2016 Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak, LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak 05000352/LER-2016-0022016-04-11011 April 2016 Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements, LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements 05000352/LER-2016-0012016-03-23023 March 2016 Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock, LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function 2017-01-27
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Limerick Generating Station, Units 1 and 2 05000352 & 05000353
3. LER NUMBER
2017 - 00 001 I. Unit Conditions Prior to the Event Limerick Generating Station (LGS) Units 1 and 2 were both operating in Operational Condition (OPCON) 1 at 100 percent power at the time of the event. There were no other structures, systems, or components inoperable at the time of the event that contributed to the event.
II. Description of the Event
Over a period of approximately one month, the Main Control Room (MCR) Heating, Ventilating and Air Conditioning (HVAC) system experienced four failures. Three of the failures were caused by an intermittent dropout, or chattering of the LOOP start relay for two fans (0B-V116 MCR Supply and OB-V121 MCR Return Fans). The fourth failure was due to a contactor in the MCC for the OB-V116 MCR Supply Fan. Each of these events caused an unplanned Limiting Condition for Operation (LCO) entry and inoperability of the Control Room Emergency Fresh Air Supply (CREFAS) system. A timeline of events is as follows:
10/19/16 - KS-078-326B and KS-078-359B relays replaced for Preventative Maintenance (PM).
Post Maintenance Testing (PMT) was performed by running the OB MCR HVAC train.
11/13/2016 - To support chiller swaps the OA MCR HVAC train was secured and Operations attempted to start the OB train. This was the first start attempt since the PMT performance on 10/19/16. When the supply fan handswitch was placed in RUN, the fan did not start. Relay replacements were performed for KS-078-026B, which was found failed, and KS-078-326B, which was found chattering. Following replacements, the supply fan was started successfully.
When Operations attempted to start the OB return fan by placing the handswitch in RUN, it did not start. The KS-078-359B relay was found chattering, thereby preventing the return fan from starting.
11/20/16 - After running the OB train of MCR HVAC for a period of one week, the supply fan tripped. The contactor was observed to be chattering. Breaker maintenance was performed and the contactors were replaced. Additionally, new wiring was installed internal to the breaker cubicle. During troubleshooting, the KS-078-326B and KS-078-026B relays were removed from the field and bench tested satisfactorily.
11/29/16 - To support a MCR chiller swap, the OA MCR fans were secured and Operations attempted to start the OB train. When the supply fan handswitch was placed in RUN, the fan did not start. The cause was determined to be a failed KS-078-326B relay.
12/5/16 - The 'B' MCR Return fan tripped and the 'A' MCR return fan auto-started.
Troubleshooting efforts identified a chattering KS-078-359B relay in the field.
On 11/29/16, the site believed that the relay failure was not an infantile failure and that there may be a common condition that was causing these failures. The relay was sent for testing and evaluation, and on 12/15/16, the station received the analysis which identified a manufacturing issue had caused the relay failures.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Limerick Generating Station, Units 1 and 2 05000352 & 05000353
3. LER NUMBER
2017 - 00 001
III. Analysis of the Event
The identified relay failures were all determined to be attributed to intermittent drop out, or chattering of the installed Agastat/Tyco model ETR1413D004 (ETR TDPU series) relay coil.
These relays were all installed as normally energized, power monitoring/ Loss of Offsite Power (LOOP) start relays. They are installed to allow a 35-second time delay before the fan restarts on re-energization of the associated load center during a LOOP.
The testing determined that the relays were not reliable and failure of the relays could not be predicted. The OB MCR HVAC train was determined to be unreliable since the initial relay replacement on 10/19/16 until when the relays were replaced with relays from a different lot on 12/05/16. The B train of MCR HVAC was conservatively determined to be inoperable for a period of 47 days, which is greater than the allowable LCO action window of 7 days (per TS 3.7.2.a.1) for an inoperable CREFAS train, and therefore was deemed to be a condition prohibited by TS.
IV. Cause of the Event
Bench tests were performed on-site on the removed relays in addition to failure analysis by an offsite testing facility. This testing determined the cause of the relay chattering to be an incorrectly installed capacitor on the internal timing circuit board.
V. Corrective Actions Completed/Planned Extent of condition actions were taken to replace all of the Agastat 2016 ETR relays installed at Limerick. A total of two additional relays, from the same lot, were identified to be installed in the plant and both these relays were proactively replaced.
A Part 21 was generated by TE Connectivity for the manufacturing issue. (ML17006A011) VI. Previous Similar Occurrences There were no previous similar occurrences in the last five years of MCR Supply fan and Return fan trips due to defective relays.
VII. Component data:
System: V Central Control Complex Env. Ctrl. Sys.
Component: RLY Relay, Time- Delay Starting or Closing Component number: KS-078-326B & KS-078-359B Manufacturer: T351 Tyco Instrument DIV Model number: ETR1413D004
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05000352/LER-2017-001 | Condition Prohibited by TS due to Parts Quality Issue LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue | |
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