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Category:Letter
MONTHYEARML24038A0222024-02-0505 February 2024 Achp Letter on Section 106 Programmatic Agreement Participation IR 05000289/20230062024-01-29029 January 2024 Constellation Energy Generation, LLC, Three Mile Island Nuclear Station, Unit 1 - NRC Inspection Report No. 05000289/2023006 ML23342A1242024-01-0909 January 2024 Independent Spent Fuel Storage Installation Security Inspection Plan ML23325A1092024-01-0505 January 2024 Review of the Management Plan for Three Mile Island Station, Unit No. 2, Debris Material ML23354A2062023-12-20020 December 2023 (TMI-2), Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23354A2112023-12-20020 December 2023 Response to Request for Additional Information for the TMI-2 Post-Shutdown Decommissioning Activities Report, Rev. 5 IR 05000320/20230032023-11-28028 November 2023 TMI-2 Solutions, LLC, Three Mile Island Nuclear Station, Unit 2, NRC Inspection Report No. 05000320/2023003 ML23243A9082023-08-29029 August 2023 Shpo Letter to TMI-2 Regarding Section 106 Activities IR 05000320/20230022023-08-17017 August 2023 TMI-2 Solutions, LLC, Three Mile Island Nuclear Station, Unit 2 - NRC Inspection Report 05000320/2023002 ML23216A1742023-08-14014 August 2023 Consultation Letter to David Morrison for TMI-2 ML23216A1772023-08-14014 August 2023 Consultation Letter to Rebecca Countess for TMI-2 ML23216A1752023-08-14014 August 2023 Consultation Letter to Joanna Cain for TMI-2 ML23216A1732023-08-14014 August 2023 Consultation Letter to Christine Turner for TMI-2 IR 05000289/20230052023-08-14014 August 2023 Constellation Energy Generation, LLC, Three Mile Island Nuclear Station, Unit 1 - NRC Inspection Report 05000289/2023005 ML23216A1782023-08-14014 August 2023 Consultation Letter to Steve Letavic for TMI-2 ML23221A1402023-08-0808 August 2023 (TMI-2), Response to Requests for Additional Information for the TMI-2 Post-Shutdown Decommissioning Activities Report, Rev. 5 ML23200A1882023-07-31031 July 2023 TMI-2 Correction Letter Amendment 67 ML23209A7632023-07-28028 July 2023 Letter from PA Shpo to TMI-2 Solutions on Cultural and Historic Impacts of Decommissioning ML23192A8272023-07-10010 July 2023 TMI-2 Solutions, LLC - Response to Shpo Request for Additional Information for Er Project 2021PR03278.006, TMI-2 Decommissioning Project ML23167A4642023-07-0505 July 2023 Letter - TMI-2- Exemption 10 CFR Part 20 Append G Issuance ML23167A0312023-06-28028 June 2023 Acceptance Review and Schedule for the Request for Exemption from a Requirement from 10 CFR 20, Appendix G, Section Iii.E, EPID L-2023-LLE-0016 ML23171B0222023-06-19019 June 2023 (TMI-2) - Notification Pursuant to 10 CFR 72.140(d) Regarding Application of Previously Approved TMI-2 Quality Assurance Program to Independent Spent Fuel Storage Installation Activities ML23137A2822023-05-17017 May 2023 (TMI-2), Request for Exemption from 10 CFR 20, Appendix G, Section Iii.E ML23138A0662023-05-17017 May 2023 TMI-2 NHPA Section 106 Shpo Letter to NRC 5-17-23 ML23026A3132023-05-0202 May 2023 Issuance of Exemption from 10 CFR 70.24 (EPID-L-2023-LLE-0003) ML23122A1842023-05-0101 May 2023 Shpo_Er_Summary_Letter ML23121A2492023-05-0101 May 2023 License Amendment Request, Historic and Cultural Resources Review, Response to Request for Additional Information ML23117A0012023-04-26026 April 2023 Commitment Revision Summary Report ML23027A0832023-04-24024 April 2023 Environmental Assessment/Finding of No Significant Impact - Request for Exemption from 10 CFR 70.24 ML23108A0802023-04-18018 April 2023 Annual Radiological Effluent Release Report ML23108A0822023-04-18018 April 2023 Annual Radiological Environmental Operating Report IR 05000320/20230012023-04-12012 April 2023 TMI-2 Solutions, LLC, Three Mile Island Nuclear Station, Unit 2 - NRC Inspection Report No. 05000320/2023001 ML23102A0382023-04-10010 April 2023 Occupational Radiation Exposure Annual Report ML23108A2002023-04-10010 April 2023 CFR 20.2206(b) Personnel Radiation Exposure Report for 2022 ML23094A2582023-04-0606 April 2023 Letter to Sidney Hill, Chief, Onondaga Nation, Re., Initiation of Consultation Under Section 106 of the NHPA for the Proposed License Amendment Request for TMI 2 ML23093A0572023-04-0606 April 2023 Letter to Joanna Cain, President, Re., Ongoing Activities Related to the Proposed License Amendment Request for Three Mile Island Nuclear Station, Unit 2 ML23094A2362023-04-0606 April 2023 Letter to Carissa Speck, Re., Initiation of Consultation Under Section 106 of the NHPA for the Proposed License Amendment Request for Three Mile Island Nuclear Station, Unit 2 ML23094A2542023-04-0606 April 2023 Ltr J Bendremer Thpo Stockbridge-Munsee Community Band of Mohican Indians Re Initiation of Consultation Under Section 106 of the NHPA for Proposed License Amendment Request for TMI 2 ML23086C0652023-04-0606 April 2023 Ltr Larry Heady, Thpo, De. Tribe of Indian; Re., Initiation of Consultation Under Section 106 of the NHPA for the Proposed License Amendment Request for TMI Nuclear Station, Unit 2 ML23093A0562023-04-0606 April 2023 Letter to Steve Minnick, Site Decommissioning Director, Re., Ongoing Activities Related to the Proposed License Amendment Request for Three Mile Island Nuclear Station, Unit 2 ML23094A2602023-04-0606 April 2023 Letter to William Tarrant, Seneca-Cayuga Nation, Re., Initiation of Consultation Under Section 106 of the NHPA for the Proposed License Amendment Request for TMI 2 ML23094A2392023-04-0606 April 2023 Letter to Courtney Gerzetich, Thpo, Onedia Nation of Wisconsin, Re., Initiation of Consultation Under Section 106 of the NHPA for the Proposed License Amendment Request for TMI 2 ML23093A0592023-04-0606 April 2023 Letter to Rebecca Countess, Chair, Re., Ongoing Activities Related to the Proposed License Amendment Request for Three Mile Island Nuclear Station, Unit 2 2024-02-05
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lhree Mile l:stiW!d Nu<:fear Stalioo Roote 441 Sooth Post Office Bax 4B0 MZddJetown. PA 17051*0480 Tel 717-948-8461 June 5, 2019 TMl-19-053 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 THREE MILE ISLAND NUCLEAR STATION, UNIT 2 (TMl-2)
POSSESSION ONLY LICENSE NO. DPR-73 DOCKET NO. 50-320
Subject:
TMl-2 Unfiltered Leak Rate from Containment with RB Breather Closed This special report is being submitted pursuant to the requirements of Three Mile Island Nuclear Generating Station, Unit 2, Technical Specifications 3.1.1.2.d, specifically:
T.S. 3.1.1.2 The unfiltered leak rate from Containment with the RB Breather closed shall be less than 1/100 of the rate through the RB Breather.
Action: If the unfiltered leak rate from Containment with the RB Breather closed is greater than 1/100 of the rate through the RB Breather or if the trend indicates that the 1/t00 value will be exceeded within one year, then:
- a. Identify the excessive leakage path;
- b. Make necessary repairs and/or adjustments;
- c. Perform an additional unfiltered leak rate test; and
- d. Prepare and submit a special report to the Commission pursuant to Specification 6.8.2 within the next 30 days.
On 05/09/19 the TMl-2 T.S. 3.1.1.2 Unfiltered Leak Rate Test was performed using Surveillance Procedure 2303-6.1 with the results indicating leakage (1.3%) above the acceptance criteria of <1%. This condition was documented in the TMI site corrective action program under Issue Report (IR)# 04247808.
A troubleshooting team was assembled, and a troubleshooting plan developed. Details of the troubleshooting are documented in IR 04247808. The purpose of troubleshooting was to address the action of T.S. 3.1.1.2.a to "identify the excessive leakage path."
There were 6 potential causes identified and 4 of them were refuted by the troubleshooting. The 2 potential causes that were not refuted were:
Airlock leakage - door seals were visually inspected; equalizing valves were found to be fully closing; and equalizing valve seats (as visible) were found acceptable. The airlock Page lof 2
TMl-19-053 doors were cycled to permit entry into the Containment for inspection. All components of the airlock functioned correctly.
Purge Valve(s) leakage- (outside) purge valves were found to be fully seated when closed. The Inner Purge valves are permanently blocked open (a condition of Post-Defueling Monitored Storage - PDMS); the outside purge valves were cycled per procedure, open and then closed.
The instrumentation used to complete the surveillance was checked for leakage and calibrated. A calibrated alternate instrument was installed at an alternate containment penetration as part of the troubleshooting plan. The conclusion of the troubleshooting effort satisfied T.S. 3.1.1.2.b, although, there were no necessary repairs and/or adjustments required. Per T.S. 3.1.1.2.c, the test was conducted again with satisfactory results (0.9%). A review of results from previous test performances [2013=0.1%,
2007=0.5%, 2002=0.2%) did not indicate an adverse trend or any outstanding issues that may affect the conduct of the test. It is noted that the most recent test result is higher than previously measured. This will be factored into the testing preparations and evaluation at the next testing interval per TS 4.1.1.2. Based on*an initial failed test, the next test interval shall be 1 year per TS 4.1.1.2.
The most probable cause for the initial test failure was leakage through the purge valve( s) and/or the Reactor Bui.lding Airlock( s) since they are infrequently cycled components which may have achieved improved seating after being cycled. A contributing cause was the steady lowering local atmospheric (barometric) pressure during the entire initial (failed) test duration.
There are no regulatory commitments contained in this letter.
If you have any questions, please contact Gil Wright at (717) 948-8225.
Respectfully, Gregory H. Halnon President and Chief Nuclear Officer, GPUN cc: USNRC TMl-2 Region I Inspector USNRC TMl-2 Project Manager USNRC Senior Resident Inspector - Three Mile Island NRC Regional Administrator, Region *I Director, Bureau of Radiation Protection - Pennsylvania Department of Environmental Protection Page2of 2