05-04-2016 | On March 5, 2016, at 1512 Eastern Standard Time (EST), Watts Bar Nuclear Plant ( WBN) Unit 1 entered Technical Specification (TS) 3.6.3, Containment Isolation Valves, Condition A for a containment isolation valve being inoperable.
During a containment walkdown, leakage was found on valve 1-FCV-61-122, Glycol Cooled Floor Return Header Isolation and the valve was declared inoperable. TS 3.6.3 Condition A requires that a penetration flow path with one containment isolation valve inoperable to be isolated by use of at least one closed and de-activated automatic valve, closed manual valve, blind flange, or check valve with flow through the valve within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The penetration associated with this containment isolation valve was not isolated until 2113 EST on March 5, 2016. The cause of this event was operations staff misunderstanding the applicability of the Note associated with TS 3.6.3, which allows administrative controls under certain conditions.
Because the action specified by TS 3.6.3 was not completed within four hours, this condition is reportable as an operation or condition prohibited by TS per 10 CFR 50.73(a)(2)(i)(B). |
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Category:Legal-Affidavit
MONTHYEARCNL-24-016, Supplement to Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14)2024-01-10010 January 2024 Supplement to Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14) CNL-23-044, Transmittal of Revision 3 to WCAP-18774-P and WCAP-18774-NP, Addendum to the Rotterdam Dockyard Company Final Stress Report for 173 P.W.R. Vessels TVA III & IV (Report No. 30749-B-030, Rev. 3) - Evaluation of One Closure Stud Out2023-06-0101 June 2023 Transmittal of Revision 3 to WCAP-18774-P and WCAP-18774-NP, Addendum to the Rotterdam Dockyard Company Final Stress Report for 173 P.W.R. Vessels TVA III & IV (Report No. 30749-B-030, Rev. 3) - Evaluation of One Closure Stud Out CNL-23-043, Emergency License Amendment Request to Relax the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Studs in Technical Specification Table 1.1-1, Modes (WBN-TS-23-09)2023-05-0404 May 2023 Emergency License Amendment Request to Relax the Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Studs in Technical Specification Table 1.1-1, Modes (WBN-TS-23-09) CNL-21-098, Supplement to Response to Request for Additional Information Regarding Application to Modify Technical Specifications Steam Generator Inspection/Repair Program Provisions and Operating License Condition 2.C.(4)2022-01-0505 January 2022 Supplement to Response to Request for Additional Information Regarding Application to Modify Technical Specifications Steam Generator Inspection/Repair Program Provisions and Operating License Condition 2.C.(4) ML21246A1172021-09-0202 September 2021 Affidavit Dated September 2, 2021, Executed by Anthony J. Schoedel ML21223A2592021-08-11011 August 2021 Affidavit - Prop Slides - Partially Closed Meeting with TVA Potential Watts Bar, Unit 2 Tube Locking LAR CNL-21-011, Expedited Application for Approval to Use a Growth Rate Temperature Adjustment When Implementing the Generic Letter 95-05 Analysis for the (WBN TS-391-21-002)2021-02-25025 February 2021 Expedited Application for Approval to Use a Growth Rate Temperature Adjustment When Implementing the Generic Letter 95-05 Analysis for the (WBN TS-391-21-002) CNL-20-063, Supplement to License Amendment Request for Measurement Uncertainty Recapture Power Uprate (WBN-TS-19-06)2020-07-27027 July 2020 Supplement to License Amendment Request for Measurement Uncertainty Recapture Power Uprate (WBN-TS-19-06) CNL-19-082, License Amendment Request for Measurement Uncertainty Recapture Power Uprate (WBN-TS-19-06)2019-10-10010 October 2019 License Amendment Request for Measurement Uncertainty Recapture Power Uprate (WBN-TS-19-06) CNL-18-116, Response to Request for Additional Information Regarding the Application to Revise Watts Bar Nuclear Plant Unit 2 - License Condition 2.C(4) PAD4TCD (391-WBN-TS-18-03)2018-10-11011 October 2018 Response to Request for Additional Information Regarding the Application to Revise Watts Bar Nuclear Plant Unit 2 - License Condition 2.C(4) PAD4TCD (391-WBN-TS-18-03) CNL-18-103, Topical Report TVA-NPG-AWA16, TVA Overall Basin Probable Maximum Precipitation and Local Intense Precipitation Analysis, Calculation CDQ0000002016000041,.2018-09-0606 September 2018 Topical Report TVA-NPG-AWA16, TVA Overall Basin Probable Maximum Precipitation and Local Intense Precipitation Analysis, Calculation CDQ0000002016000041,. CNL-18-081, Request for Review and Approval of Topical Report TVA-NPG-AWA16, TVA Overall Basin Probable Maximum Precipitation and Local Intense Precipitation Analysis, Calculation CDQ0000002016000041, Revision 12018-06-22022 June 2018 Request for Review and Approval of Topical Report TVA-NPG-AWA16, TVA Overall Basin Probable Maximum Precipitation and Local Intense Precipitation Analysis, Calculation CDQ0000002016000041, Revision 1 05000390/LER-2016-0022016-05-0404 May 2016 Technical Specification Action Not Met for Inoperable Containment Isolation Valve, LER 16-002-00 for Watts Bar, Unit 1, Regarding Technical Specification Action Not Met for Inoperable Containment Isolation Valve CNL-15-263, Application to Revise Technical Specification 4.2.1, Fuel Assemblies (WBN-TS-15-03) - Supplemental Information Related to the Onsite Regulatory Audit at Pacific Northwest National Laboratory2015-12-29029 December 2015 Application to Revise Technical Specification 4.2.1, Fuel Assemblies (WBN-TS-15-03) - Supplemental Information Related to the Onsite Regulatory Audit at Pacific Northwest National Laboratory CNL-15-204, Response to NRC Question Regarding the Revised Containment Analysis, Including Enclosure 3, WCAP-17834-NP, Revision 2, Wcobra/Trac Long Term LOCA M&E and Containment Integrity Analysis and Enclosure 4, Affidavit2015-09-21021 September 2015 Response to NRC Question Regarding the Revised Containment Analysis, Including Enclosure 3, WCAP-17834-NP, Revision 2, Wcobra/Trac Long Term LOCA M&E and Containment Integrity Analysis and Enclosure 4, Affidavit ML15265A0452015-09-18018 September 2015 Holtec International - Request for Additional Documentation for Watts Bar Dry Storage Project ML13225A0242013-08-0606 August 2013 Fuel Thermal Conductivity Degradation, Response to Supplemental Safety Evaluation Report Open Item 61 ML11341A0342011-11-30030 November 2011 Attachment 32, General Atomics-Electronics Systems Inc. Letter GA-ESI 4493, Request by General Atomics Electronic Systems, Inc. to Withhold Certain Information from Public Disclosure Under 10CFR2.390 Dated October 14, 2011.. ML1109502762011-04-0101 April 2011 Response to Large Break Loss of Coolant Accident (LBLOCA) and Over-Pressurization Request for Additional Information ML0325803962003-05-29029 May 2003 Enclosure 3 - Watts Bar, Withholding from Public Disclosure, Responses to the NRC Request for Additional Information on the RFA-2 Licensing Submittal (WBN-TS-02-13) for the Watts Bar Nuclear Plant (Proprietary) ML0222102552002-08-0707 August 2002 Letter from Brent R. Marquand to Charles Bechhoefer Requesting That Licensing Board Sign and Issue Subpoena for Sam L. Harvey, Based on Description of Intended Testimony Set Forth in Tva'S 03/29/2002 Witness List 2024-01-10
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000391/LER-2017-0052018-01-25025 January 2018 Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error, LER 17-005-00 for Watts Bar, Unit 2, Regarding Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error 05000390/LER-2017-0152018-01-0808 January 2018 Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications, LER 17-015-00 for Watts Bar, Units 1 and 2, Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications 05000390/LER-2017-0142017-12-20020 December 2017 Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function, LER 17-014-00 for Watts Bar, Unit 1, Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function 05000390/LER-2017-0122017-10-23023 October 2017 Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications, LER 17-012-00 for Watts Bar, Unit 1, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0112017-10-23023 October 2017 Failure to Enter Technical Specification 3.6.3 for Containment Isolation Valve, LER 17-011-00 for Watts Bar, Unit 1, Regarding Failure to Enter Technical Specification 3.6.3 for Containment lsolation Valve 05000390/LER-2017-0102017-10-10010 October 2017 Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board, LER 17-010-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board 05000391/LER-2017-0042017-09-25025 September 2017 Manual Reactor Trip Due to Inoperable Rod Position Indication, LER 17-004-00 for Watts Bar Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication 05000390/LER-2017-0042017-08-31031 August 2017 Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup, LER 17-004-01 for Watts Bar, Unit 1, Regarding Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup 05000390/LER-2017-0082017-08-14014 August 2017 Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation, LER 17-008-00 for Watts Bar, Unit 1, Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation 05000390/LER-2017-0072017-08-0808 August 2017 Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance, LER 17-007-00 for Watts Bar, Unit 1, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance 05000390/LER-2017-0062017-07-31031 July 2017 Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications, LER 17-006-00 for Watts Bar, Unit 1, Regarding Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications 05000390/LER-2017-0052017-07-10010 July 2017 Isolation of the 1 B-B Safety Injection Pump Leads to Condition Prohibited by Technical Specifications, LER 17-005-00 for Watts Bar re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications 05000391/LER-2017-0032017-05-22022 May 2017 Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure, LER 17-003-00 for Watts Bar, Unit 2, Regarding Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure 05000391/LER-2017-0022017-05-12012 May 2017 Manual Reactor Trip as a Result of a Secondary Plant Transient, LER 17-002-00 for Watts Bar, Unit 2, Regarding Manual Reactor Trip as a Result of a Secondary Plant Transient 05000391/LER-2017-0012017-05-0303 May 2017 Containment Airlock Function Lost Due to Equalizing Valve Not Closing, LER 17-001-00 for Watts Bar, Unit 2, Regarding Containment Airlock Function Lost Due to Equalizing Valve Not Closing 05000390/LER-2017-0032017-03-0303 March 2017 Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications, LER 17-003-00 for Watts Bar, Unit 1, Regarding Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0022017-02-22022 February 2017 Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications, LER 17-002-00 for Watts Bar Nuclear Plant, Unit 1, Regarding: Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2016-0112016-12-0909 December 2016 Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler, LER 16-011-01 for Watts Bar Nuclear Plant, Unit 1 Regarding Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler 05000391/LER-2016-0082016-10-28028 October 2016 Reactor Trip Resulting from Failure of 2B Main Bank Transformer, LER 16-008-00 for Watts Bar, Unit 2, Regarding Reactor Trip Resulting from Failure of 2B Main Bank Transformer 05000391/LER-2016-0052016-08-19019 August 2016 Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip, LER 16-005-00 for Watts Bar, Unit 2, Regarding Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip 05000390/LER-2016-0102016-08-0808 August 2016 Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado, LER-16-010-00 for Watts Bar Nuclear Plant, Units 1 and 2 Regarding Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado 05000391/LER-2016-0042016-08-0404 August 2016 Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure, LER 16-004-00 for Watts Bar, Unit 2, Regarding Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure 05000391/LER-2016-0032016-07-27027 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Governor Valve Spring Over-Tensioning, LER 16-003-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump lnoperable for Longer Than Allowable Outage Time Due to Governor Valve Spring Over-Tensioning 05000390/LER-2016-0082016-07-15015 July 2016 Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B, LER 16-008-00 for Watts Bar, Unit 1, Regarding Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B 05000390/LER-2016-0092016-07-15015 July 2016 Failure to Complete Surveillance Requirements Causes a Condition Prohibited by the Technical Specifications, LER 16-009-00 for Watts Bar, Unit 1, Regarding Failure to Complete Surveillance Requirements Causes Conditions Prohibited by the Technical Specifications 05000391/LER-2016-0022016-07-11011 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Turbine Speed Control Failure, LER 16-002-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer Than Allowable Outage Time Due to Turbine Speed Control Failure 05000390/LER-2016-0062016-06-30030 June 2016 Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump, LER 16-006-00 for Watts Bar, Unit 1, Regarding Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump 05000390/LER-2016-0072016-06-20020 June 2016 Technical Specification Action Not Met for Rod Position Indication, LER 16-007-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Technical Specification Action Not Met for Rod Position Indication 05000391/LER-2016-0012016-06-13013 June 2016 Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines, LER 16-001-00 for Watts Bar, Unit 2, Regarding Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines 05000390/LER-2016-0042016-05-23023 May 2016 Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables, LER 16-004-00 for Watts Bar, Unit 1, Regarding Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables 05000390/LER-2016-0052016-05-13013 May 2016 Both Trains of Unit 1 Emergency Gas Treatment System Inoperable During Unit 2 Testing, LER 16-005-00 for Watts Bar, Unit 1, Regarding Both Trains of Unit 1, Emergency Gas Treatment System Inoperable During Unit 2, Testing 05000390/LER-2016-0032016-05-10010 May 2016 Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting, LER 16-003-00 for Watts Bar, Unit 1, Regarding Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting 05000390/LER-2016-0022016-05-0404 May 2016 Technical Specification Action Not Met for Inoperable Containment Isolation Valve, LER 16-002-00 for Watts Bar, Unit 1, Regarding Technical Specification Action Not Met for Inoperable Containment Isolation Valve 05000390/LER-2016-0012016-03-0909 March 2016 Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable, LER 16-001-00 for Watts Bar, Unit 1, Regarding Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable ML1134703432011-12-13013 December 2011 Withdrawal of License Event Report 390/2011-003, Mode Change Without Meeting Limiting Condition for Operation (LCO) 3.7.5 2018-01-08
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002
I. PLANT OPERATING CONDITIONS BEFORE THE EVENT
Watts Bar Nuclear Plant (WBN) Unit 1 was in Mode 1 at 100 percent rated thermal power (RTP).
II. DESCRIPTION OF EVENT
A. Event
entered Technical Specification (TS) 3.6.3, Containment Isolation Valves, Condition A for a containment isolation valve associated with the ice condenser glycol system {El IS:BC} being inoperable. During a containment walkdown, leakage was found on valve 1-FCV-61-122, Glycol Cooled Floor Return Header Isolation {EIIS:FCV} and the valve was declared inoperable. TS 3.6.3 Condition A requires that a penetration flow path with one containment isolation valve inoperable to be isolated by use of at least one closed and de-activated automatic valve, closed manual valve, blind flange, or check valve with flow through the valve within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The penetration associated with this containment isolation valve was not isolated until 2113 EST on March 5, 2016.
Because the action specified by TS 3.6.3 was not completed within four hours, this condition is reportable as an operation or condition prohibited by TS per 10 CFR 50.73(a)(2)(i)(B).
B. Inoperable Structures, Components, or Systems that Contributed to the Event No inoperable structures, components, or systems contributed to this event.
C. Dates and Approximate Times of Occurrences Date Time Event 3/05/16 1512 EST 1-FCV-61-122, Glycol Cooled Floor Return Header Isolation declared inoperable.
3/05/16 1935 EST Licensing requested to verify invoking the TS LCO 3.6.3 note allowing the CIV path to remain open with administrative controls in place and determine acceptable time frame for "intermittent.
3/05/16 2113 EST 1-FCV-61-110 was closed and deactivated, isolating the penetration flowpath.
3/05/16 2142 EST Licensing formal interpretation of TS 3.6.3 compliance entered into operating logs.
D. Manufacturer and Model Number of Components that Failed While a leak on valve 1-FCV-61-122 caused the plant to enter TS 3.6.3 Condition A, it was not the cause of personnel failing to comply with the requirements of the Technical Specifications.
E. Other Systems or Secondary Functions Affected
There were no systems or secondary functions affected by this event.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002 F. Method of discovery of each Component or System Failure or Procedural Error While a component issue was involved in this report, it did not cause the condition prohibited by Technical Specifications G. Failure Mode and Effect of Each Failed Component While a leak on valve 1-FCV-61-122 caused the plant to enter TS 3.6.3 Condition A, it was not the cause of personnel failing to comply with the requirements of the Technical Specifications.
H. Operator Actions
Upon receiving clarification of the expectations associated with the TS 3.6.3 Note, operations properly isolated the impacted penetration.
I. Automatically and Manually Initiated Safety System Responses There were no automatic or manual system responses associated with this event.
III. CAUSE OF THE EVENT
A. The cause of each component or system failure or personnel error, if known.
This event was the result of an incorrect understanding of how to comply with the Note associated with TS 3.6.3.
B. The cause(s) and circumstances for each human performance related root cause.
The cause of this event was an incorrect understanding of how to comply with the Note associated with TS 3.6.3.
IV. ANALYSIS OF THE EVENT
TS LCO 3.6.3 Condition A, Containment Isolation valves, required the penetration associated with valve 1-FCV-61-122 to be isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Note 1 associated with TS 3.6.3 allows for a penetration flow path to be unisolated intermittently under administrative controls, such as to perform testing after maintenance. Operations stationed a dedicated operator in accordance with TS LCO 3.6.3 Note 1, but did not isolate the valve. This was based on an understanding that by invoking Note 1 with a dedicated operator stationed to isolate the flowpath that this met the intent of shutting the valve for the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time requirement for the action statement of the LCO. Upon being informed by site licensing that this reading of the TS Note was incorrect, the valve was isolated.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 002
V. ASSESSMENT OF SAFETY CONSEQUENCES
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event There were no safety system failures associated during this event. In the event a Loss of Coolant Accident (LOCA) had occurred during the inoperability of valve 1-FCV-61-122, the remaining containment isolation valve (1-FCV-61-110) for this penetration was capable of closing and isolating this penetration.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident Not applicable.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from the discovery of the failure until the train was returned to service Not applicable.
VI. CORRECTIVE ACTIONS
This event was entered into the Tennessee Valley Authority Corrective Action Program and is being tracked under condition report 1146157.
A. Immediate Corrective Actions
Upon identifying the correct requirements to implement TS 3.6.3 Condition A, the impacted penetration was properly isolated.
B. Corrective Actions to Prevent Recurrence
A shift order defining the correct response when entering TS 3.6.3 Condition A was provided to the operating staff. This issue will be a topic of future operations training.
VII. ADDITIONAL INFORMATION
A. Previous similar events at the same plant
This LER involves an incorrect understanding by operations personnel in how to apply Technical Specification requirements. No similar event was identified with the same causal basis.
B. Additional Information
None.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
C. Safety System Functional Failure Consideration
This condition did not result in a safety system functional failure.
D. Scrams with Complications Consideration There was no scram associated with this report.
VIII. COMMITMENTS
None.
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05000390/LER-2016-010 | Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado LER-16-010-00 for Watts Bar Nuclear Plant, Units 1 and 2 Regarding Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000390/LER-2016-001 | Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable LER 16-001-00 for Watts Bar, Unit 1, Regarding Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000390/LER-2016-011 | Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler LER 16-011-01 for Watts Bar Nuclear Plant, Unit 1 Regarding Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000391/LER-2016-001 | Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines LER 16-001-00 for Watts Bar, Unit 2, Regarding Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000391/LER-2016-002 | Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Turbine Speed Control Failure LER 16-002-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer Than Allowable Outage Time Due to Turbine Speed Control Failure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000390/LER-2016-002 | Technical Specification Action Not Met for Inoperable Containment Isolation Valve LER 16-002-00 for Watts Bar, Unit 1, Regarding Technical Specification Action Not Met for Inoperable Containment Isolation Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000391/LER-2016-003 | Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Governor Valve Spring Over-Tensioning LER 16-003-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump lnoperable for Longer Than Allowable Outage Time Due to Governor Valve Spring Over-Tensioning | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000390/LER-2016-003 | Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting LER 16-003-00 for Watts Bar, Unit 1, Regarding Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000391/LER-2016-004 | Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure LER 16-004-00 for Watts Bar, Unit 2, Regarding Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2016-004 | Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables LER 16-004-00 for Watts Bar, Unit 1, Regarding Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000391/LER-2016-005 | Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip LER 16-005-00 for Watts Bar, Unit 2, Regarding Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2016-005 | Both Trains of Unit 1 Emergency Gas Treatment System Inoperable During Unit 2 Testing LER 16-005-00 for Watts Bar, Unit 1, Regarding Both Trains of Unit 1, Emergency Gas Treatment System Inoperable During Unit 2, Testing | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000391/LER-2016-006 | Turbine Driven Auxiliary Feedwater Pump Auto Start on Lo-Lo Steam Generator Level Following Planned Unit Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2016-006 | Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump LER 16-006-00 for Watts Bar, Unit 1, Regarding Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000391/LER-2016-007 | Manual Reactor Trip Due to Loss of Main Feedwater | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2016-007 | Technical Specification Action Not Met for Rod Position Indication LER 16-007-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Technical Specification Action Not Met for Rod Position Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000390/LER-2016-008 | Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B LER 16-008-00 for Watts Bar, Unit 1, Regarding Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000391/LER-2016-008 | Reactor Trip Resulting from Failure of 2B Main Bank Transformer LER 16-008-00 for Watts Bar, Unit 2, Regarding Reactor Trip Resulting from Failure of 2B Main Bank Transformer | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2016-009 | Failure to Complete Surveillance Requirements Causes a Condition Prohibited by the Technical Specifications LER 16-009-00 for Watts Bar, Unit 1, Regarding Failure to Complete Surveillance Requirements Causes Conditions Prohibited by the Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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