ENS 53054
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ENS Event | |
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18:40 Nov 5, 2017 | |
Title | Loss of Secondary Containment Pressure Due to Voltage Transient |
Event Description | At approximately 1240 CST on 11/05/17, the Main Control Room received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR [volt-ampere reactive] Compensator (SVC) caused by a voltage transient on the 138 kV feed due to thunderstorms in the area. As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge at 1241. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a Condition that Could Have Prevented Fulfillment of a Safety Function under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 1242 by starting the Standby Gas Treatment HVAC (VG) system.
The NRC Resident Inspector has been notified. |
Where | |
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Clinton Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material | |
Time - Person (Reporting Time:+-1.48 h-0.0617 days <br />-0.00881 weeks <br />-0.00203 months <br />) | |
Opened: | Seth Strope 17:11 Nov 5, 2017 |
NRC Officer: | Jeff Herrera |
Last Updated: | Nov 5, 2017 |
53054 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (98 %) |
After | Power Operation (98 %) |
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