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ENS 534371 June 2018 13:05:00On 5/30/2018 a physicist for Christiana Care Home Services discovered that 50 Iodine-125 seeds were missing from the Hot Lab. The licensee began investigating to determine what happened to the seeds. The licensee determined that the seeds had been initially brought into the Hot Lab on 2/6/2018. The licensee believes that on 3/16/2018 an employee from Occupational Safety picked up empty trays from the Hot Lab to recycle them as part of their recycling program and that the Iodine-125 seeds may have been on two of the trays picked up. The trays were taken to a trailer where normal scrap metal is placed and were later picked up by the recycling company. The licensee believes, but could not confirm that the recycling company picked up the trays along with the seeds which were then taken to universal waste disposal. The licensee interviewed the occupational safety individual and the individual could not confirm that he saw any Iodine-125 seeds in the trays he placed into the recycling box. The licensee has also contacted the recycling company to determine if the boxes can be retrieved, however, the recycling company stated that the box of scrap metal could not be retrieved at this point. The licensee contacted the Iodine-125 vendor to confirm that the inventory that they have in their possession was correct. The quantity of seeds missing consisted of 50 Iodine-125 seeds with a total activity of 6 millicuries. THIS MATERIAL EVENT CONTAINS A "CATEGORY 3" LEVEL OF RADIOACTIVE MATERIAL Category 3 sources, if not safely managed or securely protected, could cause permanent injury to a person who handled them, or were otherwise in contact with them, for some hours. It could possibly - although it is unlikely - be fatal to be close to this amount of unshielded radioactive material for a period of days to weeks. These sources are typically used in practices such as fixed industrial gauges involving high activity sources (for example: level gauges, dredger gauges, conveyor gauges and spinning pipe gauges) and well logging. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 534401 June 2018 15:21:00The following report was received from the Ohio Bureau of Environmental Health and Radiation Protection via email: The Licensee had a truck with a CPN Model MC1DR gauge in it, stolen at approximately (1330 EDT) on 5/31/18 from a convenience store in southeast Columbus. The gauge contains 10 mCi of Cs-137 and 50 mCi of Am-241 sealed sources. The truck and gauge were recovered by police several hours later. The Licensee got the truck and gauge back about (2100 EDT) that evening. The gauge case had been opened, but the gauge did not appear to be damaged. The Licensee is taking the gauge to Cline Technical Services (a licensed service provider) to have it checked out as a precautionary measure. An ODH (Ohio Department of Health) inspector (will be visiting the) licensee location on Monday, 6/4/18. Ohio Item Number: OH180004 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 544634 January 2020 15:00:00At 1109 (EST) on 01/04/2020, it was determined that the primary containment leakage rate did not meet value La, defined in 10 CFR 50, Appendix J, 'Primary Reactor Containment Leakage Testing for Water-Cooled Power Reactors'. An additional, tested valve has been closed to maintain leakage below maximum allowable leakage, La. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5444616 December 2019 09:12:00

At 0358 EST, on 12/16/2019, with Unit 1 in Mode 1 at 100 (percent) power and Unit 2 in Mode 1 at 47 (percent) power, a valid actuation of the Emergency Diesel Generators (EDG) occurred. The reason for the emergency diesel generator auto start was that the normal feeder breaker from the 1C 6.9KV Unit Board to the 1B-B 6.9KV Shutdown Board (SDBD) tripped due to the breaker's 51G relay actuating causing an under-voltage signal on the 1B-B 6.9KV Shutdown Board. All 4 Emergency Diesel Generators automatically started as designed when the 6.9KV Shutdown Board under-voltage signal was received.

The 1B-B 6.9KV Shutdown Board was automatically energized from the 1B-B 6.9KV Diesel Generator. All required 6.9KV loads were sequenced back on to the 1B-B 6.9KV Shutdown Board as designed after the board was energized from its emergency diesel generator. The remainder of the electrical system is in normal alignment.

This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the Emergency Diesel Generators. There was no impact to the health and safety of the public or plant personnel. The NRC Senior Resident has been notified.

ENS 5443812 December 2019 08:14:00

EN Revision Imported Date : 3/4/2020 MANUAL REACTOR TRIP DUE TO A LOSS OF HEATER DRAIN TANK PUMP FLOW At 0432 EST, on 12/12/19, Sequoyah Unit 2 experienced a manual reactor trip. The trip was initiated due to a loss all number 3 Feedwater Heater Drain Tank pump flow; plant procedures directed a manual reactor trip if power is greater than 80 percent. The Auxiliary Feedwater System (AFW) automatically actuated as required when the expected post trip feedwater isolation actuation actuated. Reactor Coolant System (RCS) temperature is being maintained by the steam dump system with all 4 Reactor Coolant Pumps (RCPs) in service. All control and shutdown rods fully inserted. All safety systems responded as designed. No primary or secondary safety valves actuated during or after the transient. Unit 2 is currently stable at normal operating temperature and normal operating pressure in Mode 3. The electrical system is in a normal alignment. There was no impact on U1. There was no impact to the health and safety of the public or plant personnel. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four hour, non-emergency notification per 10CFR50.72(b)(2)(iv)(B) and an 8 hour non-emergency notification accordance with 10CFR50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. The NRC Resident Inspector was notified.

  • * * UPDATE ON 03/03/2020 AT 1320 FROM JAKE OLIVIER TO OSSY FONT * * *

The following update to the EN submitted on 12/12/19 is being made to provide clarification on reporting criteria originally described in paragraph five of EN 54438: This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector was notified. Notifed R2DO (Davis).

ENS 5441526 November 2019 16:28:00The following report was received from the North Carolina Department of Health and Human Services via email: RMB (North Carolina Radioactive Materials Branch) received a report of a portable nuclear gauge that was run over at a job site. The gauge was cordoned off and is away from any pedestrian areas. At the time of this report, based on on-site photos provided by the licensee; the source rod is retracted and is undamaged and initial surveys show no leakage. Gauge outer housing appears damaged but intact. Intertek will be arriving to take possession of the gauge to transport for repair. Inspector has been dispatched to conduct an on-site investigation. Additional information will be provided to update, complete & close this report. Our (North Carolina Department of Health and Human Services) investigation is ongoing. The gauge is a Troxler model number 3430. NC Event Report ID. NO.: 190041
ENS 5441326 November 2019 15:00:00

EN Revision Text: AGREEMENT STATE REPORT - LOSS OF A NUCLEAR DENSITY GAUGE The following report was received from the Pennsylvania Bureau of Radiation Protection via email: On November 26, 2019 a lawyer representing the licensee reported the event via telephone. The licensee is Larson Design Group, USNRC Radioactive Material License No. 47-35062-01, PA reciprocity license PA-R0218. Details are sparse at this time. The lawyer stated an employee wrecked a vehicle carrying a nuclear gauge (with Cesium 137 and Americium 241) in a ditch late Friday night. He had a friend pick him up, leaving the vehicle and gauge unattended. At some point police found the vehicle and impounded it. The police recognized the radioactive material shipping case in the vehicle. They allowed the employee to claim the vehicle only after producing documentation indicating he was authorized to possess it. It is believed the gauge never left the vehicle and it is back in possession of the licensee. The DEP (Department of Environmental Protection) will update this event as soon as more information is provided. PA Event Report ID No.: 190028

  • * * UPDATE FROM JOHN CHIPPO TO KARL DIEDERICH AT 1004 EST ON 12/11/19 * * *

The following update was received from the Pennsylvania Bureau of Radiation Protection via fax: The nuclear gauge was a Troxler 3440 (S/N: 33739) containing 8.1 mCi of Cs-137 and 40 mCi of Am-241/Be. The gauge was impounded by police and was out of the licensee's control for approximately 60 hours. The employee responsible has had his employment terminated. As part of corrective actions, the licensee will review its training practices and update as necessary." Notified R1DO (Lally) and (via e-mail) NMSS Events group, ILTAB, and CNSC. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5441125 November 2019 22:16:00At approximately 1500 EST, on 11/25/2019, a technician departed a job site when they realized that they left the tailgate opened and the density gauge was no longer in the back of the truck. The technician turned around to look for the gauge, however, the gauge could not be found. The licensee searched for the gauge for approximately 4 hours and then contacted local law enforcement. The gauge was reported by local law enforcement to have been picked up at approximately 1630 EST. The licensee went to the police department to examine the gauge and it was reported not to be leaking. The gauge information is a Humboldt model 5001C, Serial Number 2301 containing 10 milliCuries of Cs-137 and 40 milliCuries of Am-241. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5440925 November 2019 18:20:00

EN Revision Text: TEMPORARY PROCESS RADIATION MONITORING SAMPLE CART NON FUNCTIONAL At 1245 PST, on November 23, 2019, the Turbine Building Process Radiation Monitoring Sample Rack (TEA-SR-26) was declared non-functional and taken out of service to perform planned preventive maintenance per procedure. The temporary sample cart was placed in service as an alternate method per plant procedures. At 0854 PST, on November 25, 2019, it was discovered that the temporary sample cart had a broken belt. At that time neither the Turbine Building Process Radiation Monitoring Sample Rack nor the temporary sample cart could be returned to service. At 1300 PST, on November 25, 2019, the temporary sample cart was returned to service following repairs. This restored the required compensatory measures for TEA-SR-26. This event is being reported as a major loss of assessment capability in accordance with 10 CFR 50.72(b)(3)(xiii). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 11/27/2019 AT 0655 EST FROM SEAN KEEHN TO BRIAN LIN * * *

At 2057 PST, on November 26, 2019, it was discovered that the temporary sample cart had lost power and was not in service. At this time, neither TEA-SR-26 nor the temporary sample cart were in service, this was a subsequent failure of the temporary sample cart, and at the time the station had been unsuccessful at restoring a reliable alternate sampling method following the failure that occurred at 0854 PST, on November 25, 2019. At 2350 PST, on November 26, 2019, the temporary sample cart was returned to service following repairs. This restored the required compensatory measures for TEA-SR-26. The NRC Resident Inspector will be notified. Notified the R4DO (Pick) via email.

ENS 5441426 November 2019 15:04:00

The following report was received from the Virginia Department of Health via email: On November 25, 2019 a licensee reported that the shutter of a fixed gauge used to measure the level of material inside a process vessel might have failed to close during the semi-annual radiological testing. The gauge is a Ronan Engineering, Model SA1-F37, serial number M7407, containing 40 mCi of Cs-137. The shutter arm is actuating, but the radiation reading at approximately 3 inches below the source remained the same (0.8 mR/hr) when the shutter was opened and closed. The source is located approximately 10 feet from the ground level and is only accessible by a stepladder. There are no routine activities that bring employees in close proximity to the source. There was no public exposure or environmental release from this event. The licensee has contacted the manufacturer for further investigation. The Virginia Office of Radiological Health will review the licensee's written report and determine additional actions to be taken. Event Report ID No.: VA-19-006

  • * * RETRACTION ON 12/2/19 AT 1255 EST FROM ASFAW FENTA TO KERBY SCALES * * *

The following was received from the Virginia Department of Health via email: Please retract the incident report that was submitted on November 26, 2019. The licensee was advised by Ronan Engineering to take measurements directly from the detector side by closing and opening the shutter instead of taking a reading at approximately 3 inches below the source. On November 27, 2019, the licensee retested the shutter by measuring directly to the detector side and found 0.4 mR/hr when the shutter was opened and 0.2 mR/hr when the shutter was closed. The licensee reported to the agency that the gauge was working properly. There was no problem on the gauge; rather, it was an error on the measurement technique.

ENS 5441025 November 2019 20:00:00

The following report was received from the Arizona Department of Health Services (Department) via email: On November 25, 2019, the Department was notified of a lost I-125 seed. The licensee believes that the seed was most likely lost in pathology on November 21, 2019. The Department is continuing to investigate the event. Arizona Incident: 19-028.

  • * * UPDATE SENT BY BRAIN GORETZKI RECEIVED BY RICHARD SMITH ON NOVEMBER 26, 2019 AT 9:45 EST * * *

The following was received via email from the state of Arizona: Vender for the I-125 seed was Isoaid, description of the seed was 5 cm stranded seed, Lot Number 63917-5, and activity was 0.197mCi I-125. Notified: R4DO (Pick). THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5440820 November 2019 15:48:00

The following report was received from the Vermont Department of Health via email: Medical Event: Y90 resin Sir-Spheres treatment infusion aborted due to kinked microcatheter. 99.5 (percent) of the drawn dose was not delivered to the treatment site. Contamination of IR (interventional radiology) suite floor detected. Contamination of infusion paraphernalia (gloves, shoe covers, gauze, towels) detected. Contaminated items were contained and floor was decontaminated to acceptable levels by RSO (Radiation Safety Officer). Date of Event: 11/18/2019 11/18/19 AU (Authorized User) notified referring physician and patient of the medical event 11/19/19 RSO contacted State of Vermont 11/19/19 NRC contacted for clarification of event 11/20/19 RSO contacted Sirtex Incident Details: Terumo Progreat, I.D. 0.027(inches) (0.7mm), 130cm length, was used initially to access treatment site. Boston Scientific, I.D. 0.021(inches) (0.5mm), 130cm length, was used to access treatment site after unsuccessful attempt with Progreat. IR (Interventional Radiologist) Fellow assembled the delivery device. The original dose measurement was 2.2 mR/hr at 1230 (EST). The Nalgene with undelivered dose vial and the second Nalgene with delivery catheter were measured in exactly the same setup as original dose measurement. The total residual in the 2 Nalgene containers were 1.9 mR/hr + 0.25 mR/hr = 2.15 mR/hr at 1430. With 2 hours decay correction, the Nalgene containers reading should be 2.15 x 1.02 = 2.19 mR/hr. 2.19 / 2.2 = 0.995 or 99.5 (percent) for Vial + Catheter. Therefore, about 0.5 (percent) of the drawn dose (44.3 mCi) was lost. 0.5 (percent) of 44.3 mCi is 0.2 mCi (This is the calculated amount of Y90 lost) The DAVYR (Dosimetry and Activity Visualizer for Y-90 Radioembolization) application provides the following liver dose calculation based on the partition model: Liver = 27.5 Gy for a 1.5 GBq (or 40.5 mCi) dose delivery. This is based on 100 (percent) of prescribed dose being delivered. In the worst-case scenario where all the lost activity (0.2 mCi) was delivered to the patient, the liver dose calculation is: Liver = 27.5 Gy x (0.2 mCi / 40.5 mCi) = 0.14 Gy (or 14 rem) The only way to properly measure the bags of contaminated paraphernalia (towels, gloves, gauze, shoe covers) in the same setup as the original dose measurement would involve transferring the contents into several Nalgene containers. This can be done next day to properly account for lost Y90 activity. Medical event criteria - the byproduct material administration has to meet the following (10 CFR 35.3045): 1. The dose differs from a dose that would have resulted from the prescribed dosage by more than 50 rem to an organ or tissue. The unintended dose to any organ or tissue from the lost 0.2 mCi Y90 would be similar to the Liver dose calculated above (14 rem) and does not exceed 50 rem difference. Note: The highest delivered dose to Liver from the lost Y90 is calculated to be 14 rem. This is below the target dose of 110 Gy (or 11,000 rem) and does exceed the 50 rem difference; however, this was a medical safety decision resulting from unforeseen microcatheter kinking due to patient anatomy. 2. The total dose delivered differs from the prescribed dose by 20 (percent) or more. Yes, the total dose delivered is calculated to be about 0.2 mCi and is much below the prescribed dose of 40.5 mCi. A medical safety decision to abort the infusion was due to an unforeseen device event (kinked microcatheter) that prevented the safe delivery of Y90 microspheres.

  • * * UPDATE ON 11/26/19 AT 0738 EST FROM FRANCIS ONEILL TO OSSY FONT * * *

The following update was received from the Vermont Department of Health via email: As a follow up to Event Number 54408, Y-90 Sirsphere event, the calculated dose to the unintended organ, the pancreas, is 14 Rem or 0.14 Gray. Notified R1DO (Henrion) and NMSS Events Notification via email. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

ENS 5438715 November 2019 13:30:00The following report was received from the Arizona Department of Health Services via email: The Department received notification that one (1) tritium exit sign has been lost/stolen. The Department has requested additional information and continues to investigate the event. Arizona Incident Number: 19-027 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5438915 November 2019 19:17:00The following report was received from the Kansas Department of Health and Environmental Services via email: The gauge operator stepped approximately 15 feet away from the gauge to observe fill material being placed and a bulldozer backed over the gauge, clipping the corner of it. The gauge was not in use at the time and the source was not out. The only damage is to the yellow housing and a crack in the grey battery housing. The RSO (Radiation Safety Officer) conducted radiological surveys using a SE International Radiation Alert Monitor 4 and obtained background readings only. The gauge will be returned to the office and put into secure storage until it can be returned to the manufacturer for repair. Follow-up information will be provided to NRC. The density gauge was a Troxler model 3430, serial number 25943, containing 333 MBq of Cs-137 and 1,628 GBq of Am-241/Be.
ENS 5439216 November 2019 21:06:00The following summary report was received from the North Carolina Radioactive Materials Branch via email: This happened 11/15/19 and (the Nucor Environmental Manager) was made aware of the incident around (1400 EST), yesterday. Nucor Steel has a 2015 fixed nuclear gauge in a c-frame that was due for maintenance. The gauge was deemed offline and they rolled the c-frame to a locked location where they were to perform scheduled maintenance. It was at this time that they discovered the shutter was stuck open. They tried to close the shutter (with air) but it would not close. (The Nucor Environmental Manager) explained that they roll the gauge by motor, and that during this time the shutter was opened. No employee was exposed to radiation. This gauge is exposed to the elements and (the Nucor Environmental Manager) believes there is dirt inhibiting the shutter from closing. Since they could not get it to close, they rolled the gauge back to its normal online position where it can be open and not at risk to employees. (The Nucor Environmental Manager) stated there is no damage to the source and there (are) not any leaks. (The Nucor Environmental Manager) called the manufacturer to come perform maintenance yesterday. They arrived at his facility around (1400) today and are currently working on the gauge.
ENS 543694 November 2019 09:06:00At 0535 (EST) on November 4, 2019, with Unit 1 in mode 1 at 15 (percent) power, the reactor was manually tripped due to the lifting of an 'A' Main Steamline Safety Valve following a Condenser Steam Dump transient. The trip response was not complex, with all systems responding normally post-trip, and all control rods fully inserted into the core. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the Main Condenser by using the Condenser Steam Dump Valves. Offsite power is available and is currently supplying Normal and Emergency busses. The plant is currently stable in mode 3. Unit 2 is unaffected by this event and remains at 100 (percent) power in mode 1. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5435125 October 2019 03:24:00On October 24, 2019, at 2051 Central Time, while performing Train C Sequencer maintenance, a valid undervoltage actuation signal was sent to Unit 2 Emergency Diesel Generator (EDG) 23. The ESF Train C bus loads were shed but EDG 23 did not automatically start because it had been placed in Pull-To-Stop to support the sequencer maintenance activities. EDG 23 was taken out of Pull-To-Stop by Control Room staff to allow it to auto start and load the bus. As a result of the bus strip signal, the in service Spent Fuel Pool Cooling Pump secured. Spent Fuel Pool Cooling was restored with no measurable increase in pool temperature. The reactor was not critical and reactor decay heat removal was not challenged throughout the event. This actuation is reportable per 10 CFR 50.72(b)(3)(iv)(A) due to the automatic actuation of a system listed in 10 CFR 50.72(b)(3)(iv)(B). The NRC Resident Inspector has been notified.
ENS 5435225 October 2019 10:19:00The following report was received from the Alabama Department of Public Health via email: Representative reported that personnel found a gauge to have a failed shutter. Representative reported that the shutter is failed in the closed position. Representative reported that (the) gauge was discovered in the reported condition during some maintenance operations. Representative stated that the gauge was discovered in its reported condition on 10/24/2019. Representative reported this to (the) Agency (Alabama Department of Public Health) on 10/25/2019 at 0813 (CDT). Gauge contains source s/n 8829GK, a 500 mCi Cs-137 source. Gauge is reported as an Ohmart model SH-2. No known device issues that could have caused a failed shutter. Licensee is in the process of ordering parts for repair. Representative stated that ABB will repair the gauge." Alabama Incident number 19-29.
ENS 5433316 October 2019 14:28:00On October 16, 2019, at 0829 (EDT), an individual was transported for treatment to an offsite facility to address a personal medical issue. Due to the nature of the medical condition, only a partial survey could be completed prior to transport. Follow-up surveys performed by radiation protection technicians identified no radiological contamination of the worker or of the ambulance and response personnel. This event is being reported per 10 CFR 50.72(b)(3)(xii), 'Any event requiring the transport of a radioactively contaminated person to an offsite medical facility for treatment.' The NRC Resident Inspectors have been notified.
ENS 5433416 October 2019 17:20:00

EN Revision Text: CONTAMINATINON OF HOT LAB DUE TO BREAKING CAPSULE The following report was received from the Georgia Radioactive Materials Program via email: A patient diagnosed with hyperthyroidism was scheduled to receive 30 mCi of Iodine-131 on Oct 15, 2019. The patient informed the AU (authorized user) that they could not swallow the capsule, so the AU proceeded to break the capsule in half and pour the contents in water to easily administer to the patient. The patient and AU were in the treatment room when the AU began to break the capsule. The AU then went to the hot lab where he successfully broke the capsule using a syringe needle. The nuclear technician inquired as to what was happening in the hot lab and realized that there may be a potential contamination issue and contacted the RSO (Radiation Safety Officer). The areas were surveyed and determined to be contaminated with Iodine-131 was the hot lab, hallway in front of the hot lab, counter of the treatment room, scrub pants, shoes and socks. The RSO took the scrub pants and sock and shoes and placed them in an area for DIS (decay in storage). He proceeded to clean the area from least contaminated, the hallway and treatment room, but could not get it completely clean. The treatment room is a less used room and isolated so that room could be sealed off and secured. The hallway is posted and cordon off. Currently, the RSO is uncertain as to how much contamination is in the hot lab and has the room sealed and secured until he can further assess the area. The staff who were working in the area consisted of the RSO, Assistant RSO, nuclear technician, and AU were monitored for thyroid uptake. Results were negative. The patient was not monitored for thyroid uptake since the patient was sitting at the opposite side of the treatment room opposite of where the contamination occurred. The floor of the room and adjacent hallway was free of contamination. In addition, the patient had a Iodine-123 uptake one week prior. So they would have had some residual Iodine-123 still in the body. The patient was never administered the Iodine-131 in water. The RSO will prepare a full report discussing the incident, root cause and correction plan within 15 days. An associate will be assigned to the event.

  • * * UPDATE AT 1733 EST ON 11/26/2019 FROM IRENE BENNETT TO JEFF HERRERA * * *

The following is a synopsis of a report received from the Georgia Radioactive Materials Program via email: On October 30, 2019 a reactive inspection was performed by the Georgia Radioactive Materials Program. The areas of contamination were verified to have a physical barrier to prevent inadvertent entry and signs posted to warn individuals of the contaminated areas. The Grady Memorial Hospital Radiation Safety officer (RSO) stated that the lab will not re-open until the contamination level reaches background, approximately 80 days from the time of the incident. The RSO temporarily removed the authorized user from administrating any therapeutic doses indefinitely. The RSO reported that there will be proper training for authorized users, technologists and residents who are involved in administering radioactive materials. A technologist will be required to be present in the room where I-131 is administered. Instructions will be added about not opening or breaking capsules containing radioactive materials to hospital procedures and refresher training will encompass the procedures. The physician did not think a bioassay was necessary for the patient as they were not exposed. Notified the R1DO (Henrion) and NMSS via email.

ENS 5432915 October 2019 19:10:00At time 0911 (CDT), Main Steamline Radiation Monitor 2-RUK-2325/2327 (MAIN STEAM LINE 2-01/2-03 RADIATION MONITOR) was removed from service for planned maintenance. Compensatory measures were in place prior to removing the monitor from service to assure adequate monitoring capability available to implement the CPNPP emergency plan in the unlikely event of challenges to the steam generator or fuel cladding. The N16 radiation monitor serves as a backup with alarm function and Radiation Protection technicians have been briefed on taking local readings with a Geiger-Mueller tube on MSL (Main Steam Line) 2-01 and MSL 2-03. With this radiation monitor non-functional, with compensatory measures in place, and the monitor NOT expected to be returned to service within 72 hours, the condition is reportable as a loss of assessment capability per 10CFR50.72(b)(3)(xiii). Comanche Peak Nuclear Power Plant (CPNPP) has assurance of steam generator integrity and fuel cladding integrity and there is negligible safety significance to the current condition with respect to the public health and safety perspective. Corrective actions are being pursued to complete maintenance and restore 2-RUK-2325/2327 to functional status. The NRC Resident Inspector has been notified.
ENS 543146 October 2019 19:21:00

The following report is a summary of the information received via phone call: On 10/6/19, the radiation safety officer (RSO) noticed that one of the company vehicles appeared to have been broken into and the windows were smashed. The RSO conducted an inventory of the density gauges and determined that one of them was missing. The RSO then contacted local law enforcement (LLEA) and reported the incident. LLEA arrived on site at approximately 1640 EDT to obtain the incident information. The incident is still under investigation. The gauge information is as follows: Manufacturer: Humboldt Model: 5001 Serial Number: 2529 Source Quantity/Activity: Am-241/Be - 50 milliCuries Cs-137 - 10 milliCuries.

  • * * UPDATED ON 10/7/19 AT 1404 EDT FROM CHRIS GENDUSO TO KERBY SCALES * * *

The Pavement Inspection Technologies RSO reported that the gauge was recovered intact. Notified R1DO (Dentel), ILTAB and NMSS Events (email). THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 543125 October 2019 16:29:00At 0850 CDT, on 10/5/2019, the control room was notified of a personnel injury in the Unit 1 containment building. The individual was considered potentially contaminated since a complete frisk could not be performed prior to transport to a local hospital. At 1234 CDT, a radiological survey determined that the individual and their clothing had trace amounts of activity that was easily removed. The employee did not sustain any life threatening injuries. This is reportable under 10 CFR 50.72(b)(3)(xii). Additionally, at 1135 CDT contact was made with the Arkansas Department of Health about transport of the potentially contaminated individual. This is reportable under 10 CFR 50.72(b)(2)(xi) due to notification of an offsite agency. The NRC Resident Inspector has been notified.
ENS 543114 October 2019 17:54:00The following is a summary from a part 21 report received via facsimile: Susquehanna identified a deviation with a phase to phase to ground short that was caused by misalignment of the cubicle stabs when racking in the cubicle. The cubicle was racked into the cell and 2 of the 3 phase stab fingers engaged properly with the bus. The A phase stab fingers missed the center of the bus, however an electrical connection was maintained. This condition was estimated to be present for 3 years before the failure occurred. The deviation was originally evaluated as an installation issue, however after further evaluation, the deviation has been determined to be a failure to comply with the specification requirements. The specification requirements were reviewed and it was determined that the design of the connection stabs did not fully comply with the requirements. The reported deviation will complete an electrical connection between the stab finger assembly and the bus, but at a possible reduced current carrying ability as only 1 side of the stab finger assembly is touching the bus. This causes less surface area contact between the stab finger and the bus, which causes less current carrying ability. The cubicle will likely function, however over time, if left uncorrected, it is possible that the connection could overheat, depending on the load of the cubicle, since the connection has a reduced surface area and/or has a higher resistance than what would be typical if the stab finger assembly was properly engaged. The issue could extend to all F10 series MCC cubicles supplied by NLI (Nuclear Logistics Inc.) with the current design of stab assembly P/N: 5600-SA3-1. This design has been provided to Susquehanna Station, Limerick Generating Station, and Perry Nuclear. Please contact me with any questions or comments: Tracy Bolt, Director of Quality Assurance AZZ Nuclear 7410 Pebble Drive Ft. Worth, TX 76118
ENS 5428721 September 2019 10:28:00At 0800 (CDT), with Unit 2 in Mode 1 at 100 percent (power), the reactor was manually tripped due to elevated vibration indication on the 2C reactor coolant pump exceeding annunciator response procedure trip criteria. The trip was not complex, with all systems responding normally post trip. Auxiliary Feedwater (AFW) auto actuated as expected following the manual reactor trip. Operations responded and stabilized the plant. Decay heat is being removed via the use of AFW and subsequent steaming of the steam generators to the main condenser. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b(2)(iv)(B). In addition, this event report is being reported as an eight-hour non-emergency notification per 10 CFR50.72(B)(3)(iv)(A) for a specified system actuation. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. Farley reported that there was no increase in containment unidentified leakage or fluctuations with RCP seal flow during this event.
ENS 5427212 September 2019 03:25:00The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. Radiation monitor RU-140 (#2 Steam Generator Main Steam Line radiation monitor) experienced a communication failure on both ports A and B. The RU-140 monitor is off line and non-functional at this time. At least one channel of RU-140 is required to perform a Steam Generator Tube Rupture (SGTR) dose assessment. This represents an unplanned loss of radiological assessment capability for the inability to perform dose assessments that require the radiation monitor. The ability to make emergency classifications from other radiological data collection methods such as field sampling remains available. Actions have been initiated to restore the radiation monitor. The NRC Resident Inspector has been informed.
ENS 5427112 September 2019 00:49:00On September 11, 2019 at 1719 CDT, plant personnel identified a condition in which the 208 foot elevation inner primary containment airlock door was not in its fully seated and latched position while the 208 foot elevation outer primary containment airlock door was opened. The 208 foot elevation outer containment airlock door was subsequently closed by the individual exiting the area. The time that both 208 foot elevation containment airlock doors were not in their fully seated and latched positions was less than 1 minute. Following this occurrence, maintenance personnel inspected the 208 foot elevation inner containment airlock door and re-positioned this door to its fully seated and latched position. There was no radioactive release as a result of this event. This condition requires an 8-hour non-emergency notification in accordance with 10CFR50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector has been notified.
ENS 543178 October 2019 17:08:00The following report was received from the Arizona Department of Health Services via email: The Department (Arizona Department of Health Services) received notification on October 8, 2019, that a Humboldt 5001 series, SN#5820, portable gauge was stolen from a work site in San Luis, Arizona, on September 5, 2019. The portable gauge contains 44 milliCuries of americium-241 and 11 milliCuries of cesium-137. The Arizona Department of Public Safety and the San Luis Police Department were notified of the event by the licensee on September 5th and a police report was filed. The Department (Arizona Department of Health Services) has requested additional information and continues to investigate the event." Arizona Incident Number: 19-023 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5421111 August 2019 11:40:00At 0814 EDT on 8/11/19, with Unit 2 at 83 percent power during a planned load reduction, the reactor was manually tripped due to degraded feedwater flow control to the 23 Steam Generator caused by a malfunction of the associated Feedwater Regulating Valve, 23BF19. The trip was not complex, with all systems responding normally post trip. An actuation of the Auxiliary Feedwater system occurred following the manual reactor trip as expected due to low level in the steam generators. The unit is stable in Mode 3. Decay heat is being removed by the Main Steam Dumps and Auxiliary Feedwater System. Due to the actuation of the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee notified the State of New Jersey. Unit 1 remains at 100 percent power.
ENS 542098 August 2019 11:11:00The following was report was received from the Ohio Department of Health via email: The licensee discovered a leaking Eckert & Ziegler Cs-137 vial source. The leak test result, performed on August 6, 2019, identified 0.016 microCuries of removable activity. Notification to the Ohio Department of Health was made on August 8, 2019. The licensee will dispose of the source through a licensed waste broker. Device model number: RV-137-250U Serial number: 171069 Ohio item number: OH190014
ENS 5416416 July 2019 12:48:00The following report was received from the Ohio Bureau of Environmental Health and Radiation Protection via email: The licensee (Professional Service Industries, Inc.) experienced a vehicle fire today (7/15/19) involving a Troxler 3430P gauge, S/N 70185, containing a double-encapsulated sealed source of Cs-137 (8 mCi (0.30 GBq)) plus a double-encapsulated sealed source of Am-241 (40 mCi (1.48 GBq)). The vehicle driver pulled over on the shoulder of the interstate when he noticed smoke (coming) from the bed of the truck. The licensee believes that the cause of the fire may have been as a result of vandalism that ruptured the fuel tank. The licensee reported that such activities have occurred in the past. No one was injured. After the fire was extinguished, the device was surveyed using a calibrated NDS Model ND-500A survey meter. The measured radiation levels of the device were 20 mR/hr at the surface, and 0.9 mR/hr at 1 meter, without the transport case. The device has been leak tested pending results and Troxler has been contacted for disposal. Item Number: OH190011
ENS 5415811 July 2019 15:02:00The following report was received from the Illinois Emergency Management Agency (Agency) via email: During Agency efforts to pursue an annual self-inspection report from a general licensee (Weber Packaging Solutions, aka Weber Marking Systems), it was discovered (3) NDC model 103 fixed gauges, containing 150 mCi of Am-241 each could not be accounted for. The company provided a sales order, dated 3/9/17, showing the sale of the gauges (incorporated into machinery) to Margot Machinery in Scotia, New York. On July 11, 2019, the Agency determined through communications with State of New York program staff and Margot Machinery that the transfer of the devices out of Illinois was not to a licensed broker or another general licensee. Margot Machinery was unaware the machinery contained any radioactive sources. Weber indicated on the sale bill (NDC Model 5400 TC gauge) but did not verify the transfer was to another general licensee or someone specifically licensed and authorized to receive the sources. Margot Machinery states they were unaware sources were present and had never taken possession of the machinery. Margot Machinery had contracted a broker (Buckeye Business in Ohio) to rig and remove the equipment. Agency efforts are ongoing to contact Buckeye Business and determine the fate of the machinery and sources. Correspondence is ongoing with State of Ohio officials. This matter remains open and the report will be updated as details become available. Illinois Item Number: IL190021 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5416012 July 2019 14:35:00The following report was received from the Pennsylvania Bureau of Radiation Protection (PA DEP) via facsimile: On July 10, 2019, a Troxler gauge was hit by a roller while on a job site at the Philadelphia Airport. The area was secured, and the PA DEP responded to the site. The gauge was not found to be leaking and was secured for shipment back to the operators' office in New Jersey. Preliminary investigation indicates the gauge operator is licensed in New Jersey, but not licensed to operate within Pennsylvania. There was no exposure to workers or the public. Gauge is a Troxler model 4640-B, Serial number: 72103 containing 8 milliCuries of Cs-137. Event Report ID No.: PA190016
ENS 541391 July 2019 05:55:00

At approximately 1400 EDT, on 6/30/19, a company technician discovered that his personal vehicle was stolen from his residence driveway in Tolland, CT. The vehicle contained a Troxler density gauge locked in the trunk of the vehicle. The technician contacted the Connecticut State Police and reported the stolen vehicle and the stolen density gauge. The state police are still investigating the issue. The nuclear density gauge is a Troxler model 3440, serial number 69523, containing 10 mCi of Cs-137 and 40 mCi of Am-241.

  • * * UPDATE ON JULY 9, 2019 AT 1008 EDT FROM HABIB CHAUDHARY TO BETHANY CECERE * * *

On July 8, 2019, a State Trooper found the gauge in a portable restroom in Highland Park in Hartford, CT. Connecticut Department of Energy and Environmental Protection determined the gauge was intact. The licensee's radiation safety officer is sending the gauge for leak testing. Notified R1DO (Dimitriadis), and ILTAB and NMSS Events Notification (via email).

  • * * UPDATE ON JULY 9, 2019 AT 1652 EDT FROM SHAWN CHAUDHARY TO CATY NOLAN * * *

The Connecticut Department of Energy & Environmental Protection representative stated that he surveyed the gauge and cleared it since no damage was done. Tri State has also visually inspected and surveyed the gauge and found it to be intact and not tampered with. For extra precautions, a leak test of the gauge was taken and sent to a certified lab. The gauge will not be used until we have received the results from the lab. Moving forward, all technicians have been instructed to make every attempt to drop off their gauge at Tri State Materials Testing Lab's designated gauge room every day at the end of their field work. If they cannot make it back due to weekend and night work, they must store the gauge at their home securely to prevent this type of incident recurrence. Notified R1DO (Dimitriadis), and ILTAB and NMSS Events Notification (via email). THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5411412 June 2019 13:11:00

EN Revision Text: AGREEMENT STATE REPORT - LOST AMERICIUM/BERYLLIUM SOURCE The following report was received from the Texas Department of State Health Services (the Agency) via email: On June 12, 2019, the licensee's Radiation Safety Officer (RSO) notified the Agency that while performing an in-depth audit, he became aware that a 250 millicurie americium-241/beryllium source (SN: T-128) they had been licensed for was not present at their main site. Records for the source indicate the last leak test was performed in September 2017, but the source was not recorded on quarterly inventories in 2018. The RSO has been unable to find any records of transfer or disposal. The RSO is continuing record searches and interviews as well as physical searches of the licensee's facilities. More information will be provided as it is obtained in accordance with SA-300. Texas Incident #: 9686

  • * * UPDATE ON 06/21/2019 AT 1605 EDT FROM KAREN BLANCHARD TO THOMAS KENDZIA * * *

The following was received from the Texas Department of State Health Services via email: On 6/21/2019, licensee notified the Agency that it located the missing source at one of its facilities. Notified the R4DO (O'KEEFE), and the NMSS Events Notification, ILTAB, and CNSNS (Mexico Nuclear Safety Commission) via email. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5410911 June 2019 17:03:00At 1324 CDT, on 6/11/19, Coffey County Emergency Management issued the following alert: The Civil Authorities have issued a Nuclear Power Plant Warning for Coffey, KS beginning at 1323 CDT and ending at 1423 CDT (WIBW radio AM/FM). Coffey County Emergency Management Required Weekly Test. A press release is planned to notify residents that the warning was only a test. There was no impact to the health and safety of the public as a result of this event as the offsite response capabilities remain functional. The site is operating with no emergency conditions present. This event is being reported under 10 CFR 50.72(b)(2)(xi), as an inadvertent notification of the IPAWS (Integrated Public Alert Warning System) system. A press release is planned. The NRC Resident Inspector has been notified.
ENS 5410811 June 2019 16:57:00A non-licensed contract employee supervisor had a confirmed positive for a controlled substance during a pre-access fitness for duty test. The individual's unescorted access to the plant has been terminated and the badge removed.
ENS 5411011 June 2019 18:07:00

The following report was received from the Georgia Department of Natural Resources via email: A TheraSphere Y-90 patient did not receive the full dose to the target organ that was prescribed. The administered dose differed from the prescribed dose by more than 20 (percent). The prescribed activity to be delivered to the patient was 2.15 GBq (58 mCi). The calculated delivered activity to the patient was 1.01 GBq (27.3 mCi). The delivered activity was determined by comparing pre-and post-administration survey meter measurements of the administration equipment, as per standard TheraSphere procedure. Radiological Analysis: Prescribed dose to target volume (liver): 127 Gy Administered dose to target volume (liver): 59.8 Gy Discussion and Outcome: On May 28, 2019, it was brought to the radiation safety officer's attention that a Y-90 TheraSphere administration had not delivered the full prescribed activity to the patient as intended. Upon further discussion it was noted that the performing physician noticed after connection of the line between the micro-catheter and the delivery vial that multiple air bubbles had become trapped in the line. He then created a closed system manifold using a three-way stopcock and syringes to effectively bleed out air bubbles and flush back as much of the dose as possible to the patient. The closed system prevented any spillage or contamination, and residual dose was retained in the syringes and stopcocks. Despite these actions taken by the physician, a post-administration assay of the waste container showed that the full desired activity had not made it out of the delivery equipment and into the patient. The procedure was a segmentectomy, and (the) patient will be re-evaluated in one month's time to determine if an additional therapeutic administration will be needed. Root Cause: Human error: Air was likely trapped somewhere in the system during the initial setup of the equipment. Operator technique failed to completely purge the lines of this air. Air bubbles in the line were not visible or not noticed prior to the connection of the line. Efforts to eliminate the air and deliver the full dose to the patient were then not successful. Corrective Actions and Actions to Prevent Further Occurrences: The nature of this event and the likely cause has been discussed with all staff involved in these procedures. A refresher training session has been scheduled for staff involved in these procedures. This training will be provided by a representative from BTG/TheraSphere starting on June 10, 2019. An additional step will be added to the procedure to visually and verbally confirm that there is no detectable air in the line between the micro-catheter and the dose vial prior to connection.

  • * * UPDATE FROM IRENE BENNETT TO HOWIE CROUCH (VIA EMAIL) ON 4/30/20 AT 1323 * * *

The NMED report number from the original report was removed. The new NMED report number was not obtained. NRC Event number 54684 was also created for this event and was deleted from the database. Notified R1DO (Schroeder) and NMSS Event Notification (email). A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

ENS 5411512 June 2019 15:45:00The following report was received from the State of Florida Bureau of Radiation Control via email: This morning, HRMC Inc. (Holmes Regional Medical Center) called to report a misadministration of Y-90 TheraSpheres to a patient, 77 y/o female. Prescribed activity was 0.304 GBq, prescribed dose was 120 grey. Administered activity was 3.0 GBq, awaiting confirmation of administered dose, BRC (Bureau of Radiation Control) assumes administered dose will be 10 times prescribed dose based on 10 times administered activity. Lot # 1999265. An authorized physician discussed this incident with the patient and a few family members. This was intended to be a one time treatment. This appears to meet the criteria for an abnormal occurrence. Florida Incident Number: FL19-078 A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 540971 June 2019 17:58:00On June 1,2019, at 1618 (CDT), a notification under 10 CFR 50.72(b)(2) is being made due to notification to offsite agencies as a result of gasoline leakage to the site drainage system in the owner controlled area at South Texas Project. During a routine tour, the facilities department notified the site environmental group about a gasoline leak on fuel tank sight glass at the fuel island on site. The site environmental (group) has determined the leak amount requires notification to the Texas Commission of Environmental Quality and the Environmental Protection Agency National Response Center. The Texas Commission of Environmental Quality was notified at 1618 on June 1, 2019, and the Environmental Protection Agency National Response Center at 1626 on June 1, 2019. The NRC Resident Inspector has been notified. The licensee stated that approximately 1,384 gallons of gasoline leaked over a period of time. The spill is located at an equipment warehouse area at a distance from the plant. The leak has been isolated and the cleanup is expected to be completed by tomorrow.
ENS 5409329 May 2019 16:22:00The following report was received from the Texas Department of State Health Services via email: On May 29, 2019, the agency (Texas Department of State Health Services) was notified by the licensee's radiation safety officer (RSO) that one of their crews had suffered a source disconnect at a field site location. The exposure device being used was a QSA 880D device containing a 58.8 Curie Iridium - 192 source. The RSO stated two individuals approved for source retrieval, retrieved the source, and that no over exposures occurred due to the event. The RSO stated that during the retrieval it was found that the drive cable broke near the connector. The crank out device has been taken out of service and will be sent to the manufacturer for inspection. Additional information will be provided as it is received in accordance with SA-300. Texas Incident #: 9683
ENS 5407320 May 2019 00:02:00On May 19, 2019, at 1809 CDT, the Safety Parameter Display System (SPDS) was lost to both Arkansas Nuclear One Units 1 and 2 due to the SPDS Inverter (2Y-26) failure. The SPDS Inverter is the power supply to both units' SPDS. The Unit 2 Control Room dispatched operators in response to a smoke alarm received from the 2Y-26 Inverter room. Upon arrival, smoke was reported emanating from 2Y-26. There was no report of fire at any time. Field operators de-energized 2Y-26 and the smoke ceased. The loss of SPDS also caused the Power Operating Limits (POL) function of the Unit 2 Core Operating Limits Supervisory System (COLSS) to be lost, so Unit 2 reduced power to 91 (percent) in accordance with Technical Specifications. Both units are at power and stable. The NRC Resident has been notified. This is reportable per 10 CFR 50.72(b)(3)(xiii).
ENS 5407118 May 2019 02:09:00

On Friday, May 17, 2019 at 2303 (EDT), with the reactor at 70 (percent) core thermal power, Pilgrim Nuclear Power Station initiated a manual reactor scram due to degrading condenser vacuum as a result of the trip of Seawater Pump B. All control rods inserted as designed. The plant is in hot shutdown. Plant safety systems responded as designed. Pressure is being controlled using the Mechanical Hydraulic Control System and Main Condenser. Reactor water level is being maintained with the feedwater and condensate system. During the manual reactor scram, the plant experienced the following isolation signals as designed:

"Group 2 Isolation: Miscellaneous containment isolation valves
Group 6 Isolation: Reactor Water Clean-up
Reactor Building Isolation Actuation

Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'any event that results in actuation of the reactor protection system (RPS) when the reactor is critical...' This notification is also being made in accordance with 10 CFR 50.72(b)(3)(iv)(A), 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section...' (B)(2) 'General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs).' This event has no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee will notify the Massachusetts Emergency Management Agency.

ENS 5406716 May 2019 10:29:00At 1030 MDT, on 5/15/2019, a Troxler gauge was damaged by a vehicle driving at a high rate of speed through a job site in Middleton, ID. The gauge was damaged and the source and rod disconnected from the gauge base. The on site technician contacted the radiation safety officer who arrived on-site to investigate the incident. The gauge area was quarantined, the area surveyed and the damaged equipment was placed into a container and shipped back to the office while it awaits leak testing prior to returning the gauge to the vendor. The area surveyed after the gauge was removed indicated that there was no surface contamination. The licensee filed a police report and documented the issue. The gauge was a Troxler model 3444 Serial Number: 35061 Isotopes: Cs-137, 8 milliCuries; Am-241, 40 milliCuries The licensee contacted the Region IV office (VonEhr).
ENS 5406415 May 2019 02:21:00At 2151 CDT, on 14 May 2019, Comanche Peak Nuclear Power Plant (CPNPP) experienced a voltage transient within the onsite 138kV switchyard due to the loss of one of the offsite switchyards supplying power to the CPNPP 138kV switchyard. The reduction in safeguards bus voltage due to the transient caused the Unit 2 safeguard busses to load shed and perform a slow transfer to power supplied from 345kV transformer XST2A. Unit 2 was subjected to actuation of both blackout sequencers causing an automatic start of both motor driven Auxiliary Feedwater (AFW) pumps as well as the turbine-driven AFW pump. No emergency diesel generators started by design. All AFW pumps have been returned to standby status. All other safety systems functioned as designed. Unit 1 is currently defueled, and was unaffected by this event. The licensee has notified the NRC resident inspector.
ENS 540549 May 2019 07:01:00On May 9, 2019 at 0348 CDT, an automatic scram was received on Unit 2 following a turbine trip. All rods inserted to their full-in positions. All Group 2 and Group 3 automatic isolations actuated as expected. Systems operated as expected. Reactor vessel inventory and pressure are being maintained in normal control bands. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B), any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical. The NRC Resident Inspector has been notified. Decay heat is being removed using the steam bypass valves to the condenser and the safety relief valves did not lift as a result of the trip.
ENS 540401 May 2019 21:03:00

EN Revision Text: MANUAL REACTOR TRIP DUE TO MISALIGNED CONTROL ROD At 1643 (CDT), with Unit 2 in Mode 2 during low power physics testing, the reactor was manually tripped per procedure due to a misaligned control rod. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the atmosphere using the atmospheric relief valves. Unit 1 is not affected. Due to the Reactor Protection System actuation, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 05/08/2019 AT 1212 EDT FROM MIKE CONNER TO JEFFREY WHITED * * *

This Event Notification is being updated to clarify that the reactor was not critical when this event occurred. Therefore, the reporting requirement is changed from 10 CFR 50.72(b)(2)(iv)(B) to 10 CFR 50.72 (b)(3)(iv)(A). The reactor was tripped during low power physics testing. The misaligned rod was encountered during rod group insertion and the affected bank had been inserted to the extent that the reactor was subcritical when the operators tripped the reactor. The licensee notified the NRC Resident Inspector. Notified R2DO (Lopez)

ENS 5410711 June 2019 13:25:00The following report was received from the Kentucky Department for Public Health and Safety via email: Kentucky Radiation Health Branch (KYRHB) was notified by email, June 10, 2019, of an apparent fixed gauge device On/Off shutter equipment failure. KY Licensee Arkema, Inc. reports that on May 1, 2019, during a required 6-month check, instrument techs discovered the shutter was not closing. Verified by survey meter, the readings did not 'go down' as expected. Survey numbers are not recorded. Licensee RSO (radiation safety officer) notified plant operations department and the safety department that entry into that vessel is not permitted until the shutter mechanism has been repaired. This vessel is sealed and can contain hazardous chemicals. The only openings into the vessel are through bolted flanges or a bolted manway. The operations department controls who and when entry is allowed into any vessel. Entry into any vessel cannot be done unless the proper permits are completed, the tank is cleared, verified as clear, the source shutter is closed and verified as closed. If any of these things (are) not done then entry into the vessel is not permitted. The licensee will have a tag installed on the bolted manway stating that entry is not permitted. Ronan Engineering is scheduled to be onsite to evaluate repair or replace options. There has been no entry into this vessel in the past 6 months. The licensee will provide timely updates to KYRHB. The licensee will reinstruct employees of event reporting criteria. Kentucky Event ID: KY19006 .
ENS 5403629 April 2019 22:50:00On 4/29/19, at approximately 2029 EDT, the Operations Shift Manager was made aware that the Berrien County Sheriff's Department (BCSD) had been notified of an Emergency Siren that had spuriously actuated. BCSD was notified by local residents. The affected siren has been disabled and it has been verified that all associated local areas still have coverage from other functional emergency sirens. The cause of the actuation is under investigation at this time. This notification is being made under 10 CFR 50.72(b)(2)(xi), Offsite Notification, as a four (4) hour report." The licensee has notified the NRC Resident Inspector.
ENS 5403529 April 2019 20:01:00During power ascension on April 29, 2019, at 1630 (EDT), Nine Mile Point Unit 1 power and pressure oscillations were observed with reactor power at approximately 82 (percent). At time 1633 (EDT), the reactor was manually scrammed when the scram criteria of greater than 4 (percent) APRM power oscillations were observed in accordance with special operating procedures. All control rods fully inserted and all plant systems responded per design following the scram. Following the manual scram, the High Pressure Coolant Injection (HPCI) System automatically initiated as expected. At Nine Mile Point Unit 1, a HPCI system actuation signal on low Reactor Pressure Vessel (RPV) level is normally received following a reactor scram, due to level shrink. HPCI is a flow control mode of the normal feedwater systems, and is not an Emergency Core Cooling System. At 1633 (50 seconds after the reactor scram), RPV level was restored above the HPCI System low level actuation setpoint and the HPCI System initiation signal was reset. Pressure control was established on the Turbine Bypass Valves, the preferred system. No Electromatic Relief Valves actuated due to this scram. Nine Mile Point Unit 1 is currently in Hot Shutdown, with reactor water level and pressure maintained within normal bands. The offsite grid is stable with no grid restrictions or warnings in effect. The cause of the power oscillations is currently under investigation. The NRC Resident Inspector was notified. The New York State public service commission was notified.