05000266/FIN-2018003-02
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Finding | |
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Title | Licensee-Identified Violation |
Description | Violation: Point Beach Nuclear Plant, Units 1 and 2, Renewed Operating License Condition 4.F, requires the licensee to implement and maintain in effect all provisions of the approved fire protection program that comply with 10 CFR 50.48(a) and 10 CFR 50.48(c), National Fire Protection Association Standard NFPA 805, as specified in the license amendment requests and as approved in the safety evaluation report dated September 8, 2016.Section 1.5.1, Nuclear Safety Performance Criteria, of NFPA 805, stated in part, that fire protection features shall be capable of providing reasonable assurance that, in the event of a fire, the plant is not placed in an unrecoverable condition. To demonstrate this, the following performance criteria shall be met: (a) Reactivity Control; (b) Inventory and Pressure Control; (c) Decay Heat Removal; (d) Vital Auxiliaries; and (e) Process Monitoring.Section 1.5.1 (d), Vital Auxiliaries, of NFPA 805, stated that vital auxiliaries shall be capable of providing the necessary auxiliary support equipment and systems to assure that the systems required under (a), (b), (c), and (e) are capable of performing their required nuclear safety function. Contrary to the above, from March 16, 2018 through April 11, 2018, the licensee failed to ensure that vital auxiliaries were capable of providing the necessary auxiliary support equipment and systems to assure that the systems required under (a), (b), (c), and (e) are capable of performing their required nuclear safety function. Specifically, select 120 VAC instrument buses, needed as a vital auxiliary, would not have been energized during certain fire scenarios and compensatory measures were not implemented. Significance/Severity Level: The inspectors determined the performance deficiency was more than minor because it adversely affected the Mitigating Systems cornerstone attribute of Protection Against External Factors (Fire) and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process. The finding did not screen to green using questions 1.5.1A and 1.5.1B and thus required a detailed risk evaluation. The Senior Reactor Analyst performed walkdowns of dominant fire sequences and conducted an onsite review of the licensee's fire calculation which confirmed that the increase in risk due to the finding was less than 1E6/year (Green). |
Site: | Point Beach |
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Report | IR 05000266/2018003 Section 1R18 |
Date counted | Sep 30, 2018 (2018Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | IP 71111.18 |
Inspectors (proximate) | T Hartman K Barclay V Myers G Edwards N Fields J Rutkowski R Baker J Cameron |
Violation of: | 10 CFR 50.48 License Condition - Fire Protection |
INPO aspect | |
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Finding - Point Beach - IR 05000266/2018003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Point Beach) @ 2018Q3
Self-Identified List (Point Beach)
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