05000313/LER-2010-003, Regarding Manual Reactor Scram Conservatively Initiated After Multiple Abnormal Events Occurred During Plant Startup from Refueling Outage

From kanterella
Revision as of 04:36, 14 January 2025 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Regarding Manual Reactor Scram Conservatively Initiated After Multiple Abnormal Events Occurred During Plant Startup from Refueling Outage
ML101600698
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 06/09/2010
From: David Bice
Entergy Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
1CAN061001 LER 10-003-00
Download: ML101600698 (6)


LER-2010-003, Regarding Manual Reactor Scram Conservatively Initiated After Multiple Abnormal Events Occurred During Plant Startup from Refueling Outage
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3132010003R00 - NRC Website

text

1CAN061001 June 09, 2010 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001

Subject:

Licensee Event Report 50-313/2010-003-00 Manual Reactor Scram Arkansas Nuclear One - Unit 1 Docket No. 50-313 License No. DPR-51

Dear Sir or Madam:

Pursuant to the requirements of 10 CFR 50.73(a)(2)(iv)(A), enclosed is the subject Licensee Event Report concerning a manual Reactor scram on April 18, 2010.

There are no new commitments contained in this submittal.

Sincerely, DBB/slc Enclosure Entergy Operations, Inc.

1448 S.R. 333 Russellville, AR 72802 Tel 479-858-5338 David B. Bice Acting Manager, Licensing Arkansas Nuclear One

1CAN061001 Page 2 of 2 cc:

Mr. Elmo Collins Regional Administrator U. S. Nuclear Regulatory Commission Region IV 612 E. Lamar Blvd., Suite 400 Arlington, TX 76011-4125 NRC Senior Resident Inspector Arkansas Nuclear One P.O. Box 310 London, AR 72847 Institute of Nuclear Power Operations 700 Galleria Parkway Atlanta, GA 30339-5957 LEREvents@inpo.org

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (9-2007)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB NO. 3150-0104 EXPIRES 8/31/2010 the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Arkansas Nuclear One, Unit 1 05000313 1

OF 4

4. TITLE Manual Reactor Scram Conservatively Initiated After Multiple Abnormal Events Occurred During Plant Startup From a Refueling Outage
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 04 18 2010 2010 003 00 06 09 2010 FACILITY NAME DOCKET NUMBER
9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 1 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A)
10. POWER LEVEL 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER-Specify in Abstract below or in NRC Form 366A 011 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)

12. LICENSEE CONTACT FOR THIS LER NAME TELEPHONE NUMBER (Include Area Code)

David B. Bice, Acting Manager, Licensing 479-858-5338 CAUSE SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX

CAUSE

SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX B

AB SEAL B580 Y

14. SUPPLEMENTAL REPORT EXPECTED
15. EXPECTED SUBMISSION DATE MONTH DAY YEAR YES (If yes, complete 15. EXPECTED SUBMISSION DATE)

NO ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)

On April 18, 2010, Arkansas Nuclear One-Unit 1 (ANO-1) was operating at approximately 11 percent Reactor power, nearing the completion of the twenty-second refueling outage, and preparing to connect the Main Generator to the Electrical Grid (Grid). The ANO-1 Operating Staff entered the Reactor Coolant Pump Abnormal Operating Procedure at 1346 Central Daylight Time (CDT) due to indications of a degraded third stage seal on a Reactor Coolant Pump (P-32C). The cause of the P-32C seal failure was later determined to be an inadequate tolerance between the pump coupling slinger ring and stand pipe splash shield. At 1356 CDT, an Operator stationed at the Main Turbine reported smoke and small flames at Main Turbine Governor Valve 3 (GV3). An electro-hydraulic control (EHC) fluid leak that had previously been repaired during the outage resulted in EHC fluid entrainment in the calcium silicate piping insulation at GV3, promoting an exothermic reaction between the EHC fluid and the insulation when exposed to operating temperatures. The Operating Staff manually tripped the Main Turbine and conservatively performed a manual Reactor scram at 1357 CDT. A local CO2 fire extinguisher was used to extinguish the small flames at GV3 immediately following detection by the Operator stationed at the valve. MODE 5 conditions were established, and after repairs to the Main Turbine insulation and P-32C seal replacement, ANO-1 was connected to the Grid at 1918 CDT on April 25, 2010.

NRC FORM 366 (9-2007)

A. Plant Status At the time of the event, Arkansas Nuclear One - Unit 1 (ANO-1) was nearing the completion of the twenty-second refueling outage (1R22), operating at approximately 11 percent Reactor power, and preparing to connect the Main Generator [TB][GEN] to the Electrical Grid (Grid). The Main Generator was at rated speed with the Generator Output Breakers [TB][BKR] open, and Main Generator Exciter voltage regulator [TL][RG] testing was in progress. All structures, systems, and components that were used, or could have been used to mitigate, reduce the consequences of, or limit the safety implications of the event were available.

B. Event Description

On April 18, 2010 at 1346 Central Daylight Time (CDT), the ANO-1 Operating Staff entered the Reactor Coolant Pump [AB][P] Abnormal Operating Procedure due to Control Room indications of a degraded third stage seal [SEAL] on a Reactor Coolant Pump (P-32C).

The P-32C seal and rotating assembly had recently been replaced during 1R22. At 1356 CDT, an unrelated small fire was identified at Governor Valve 3 (GV3) [TA][V] in the High Pressure Main Turbine enclosure. Smoke and short flames were noted coming from an approximately 2-inch wide gap in the insulation surrounding GV3, and was immediately reported to the Control Room by an Operator stationed at that location. The Operating Staff manually tripped the Main Turbine and conservatively performed a manual Reactor scram at 1357 CDT. A local CO2 fire extinguisher was used to extinguish the small flames at GV3 immediately following detection. MODE 5 conditions were established, and after repairs to the Main Turbine insulation and P-32C seal replacement, ANO-1 was connected to the Electrical Grid at 1918 CDT on April 25, 2010.

C. Apparent Causes The manual Reactor scram was conservatively performed by the ANO-1 Operating Staff due to the occurrence of multiple abnormal events. This conservative decision was considered appropriate by Arkansas Nuclear One (ANO) Plant Management.

During 1R22, major work was completed on P-32C. Upon reassembly of the pump and seal components, all identified dimensions were verified to be correct per vendor procedures. The clearance between the pump coupling slinger ring and the stand pipe splash shield was not measured and was not recognized by the vendor to be a critical dimension. After the pump was placed in service and pump shaft axial growth occurred due to normal thermal, mechanical, and deflection growth, the pump coupling slinger ring came into contact with the stand pipe splash shield, resulting in metal erosion from the stand pipe splash shield. The interaction between the slinger ring and splash shield created debris that ultimately entered the third stage of the P-32C pump seal, causing the third stage seal failure. U.S. NUCLEAR REGULATORY COMMISSION (9-2007) LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKET
6. LER NUMBER
3. PAGE YEAR SEQUENTIAL NUMBER REVISION NUMBER Arkansas Nuclear One - Unit 1 05000313 2010 003 00 3

OF 4

Apparent Causes - continued The root cause of the P-32C seal failure was determined to be a lack of recognition that the gap between the pump coupling slinger ring and stand pipe splash shield was a critical dimension, and the lack of any documentation specifying the critical dimension value.

The small fire at GV3 resulted from a previously repaired electro-hydraulic control (EHC) [TG]

fluid leak causing EHC fluid entrainment in the pipe insulation. The EHC contained in the calcium silicate insulation experienced an exothermic catalytic reaction. The fire hazard associated with EHC-soaked calcium silicate insulation was determined to be applicable to locations where an EHC leak could saturate calcium silicate insulation while at cold conditions, then be subjected to high temperatures above 450 degrees Fahrenheit, with a path for the low molecular weight volatile vapors to escape into open air. The small flames issuing from the insulation at GV3 were coming from a patched area of the pipe insulation where an air gap existed for this specific condition to occur.

D. Corrective Actions

The manual Reactor scram was a result of conservative decision-making on the part of the ANO-1 Operating Staff. No corrective actions were warranted as a result of that action.

The P-32C Flowserve (previously Byron-Jackson) N-9000 seal was removed and replaced with a rebuilt N-9000 seal. The pump coupling slinger ring to stand pipe splash shield gap tolerance was identified and corrected during the seal replacement.

The EHC-contaminated insulation was removed from GV3 and replaced. Additionally, an ANO-1 plant walk down was performed by Fire Protection Engineering and Operations to identify potential areas for lube oil [LL] or EHC leaks, where such a leak could come into contact with hot pipes or equipment. The walk down focused on the High Pressure Turbine governor and throttle valves (and gland steam deck below), the Low Pressure and High Pressure Turbine bearings and associated lube oil piping [TD], the Main Feed Water [SJ]

Pumps [P], and the Main Feed Water Pump Lube Oil Reservoirs [SL]. Any identified issues were documented in the ANO Corrective Action Process. External Industry Operating Experience Report OE31287 was developed and issued.

E. Safety Significance Evaluation Systems and components required to shutdown the Reactor, maintain safe shutdown conditions, remove residual heat, and control the release of radioactive material were available and performed as required. Following the manual Reactor scram initiation, all Control Rods [AA] fully inserted. No Primary or Secondary Safeties lifted and no safety limits were exceeded. The small flames at Main Turbine GV3 were immediately extinguished by an Operator stationed at the GV3 location, and did not pose a safety concern. U.S. NUCLEAR REGULATORY COMMISSION (9-2007) LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKET
6. LER NUMBER
3. PAGE YEAR SEQUENTIAL NUMBER REVISION NUMBER Arkansas Nuclear One - Unit 1 05000313 2010 003 00 4

OF 4

Safety Significance Evaluation - continued ANO-1 operating procedures require a Reactor Coolant Pump to be secured if two of the pump seal stages were to fail. The condition that caused the failure of the third stage of the P-32C pump seal did not impact the ability of the first two stages of the seal to function properly. The remaining intact seal stages on the Flowserve (previously Byron-Jackson) N-9000 Reactor Coolant Pump Seal are designed to maintain Reactor Coolant System (RCS) integrity for this event. There is no significant safety concern associated with the failure of one stage of the P-32C mechanical pump seal.

F. Basis for Reportability A 4-hour Non-Emergency notification was performed in accordance with 10CFR 50.72(b)(2)(iv)(B) Reactor Protection System [JC] Actuation.

Follow up reporting is required by 10CFR 50.73(a)(2)(iv)(A) Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B).

G. Additional Information

A review of the last five years of reportable events did not reveal any events that would be considered similar.

Energy Industry Identification System (EIIS) codes and component codes are identified in the text as [XX].