05000244/LER-1979-014-03, /03L-0 on 790709:during RCS Cooldown,Operator Noted Channel P-452 Overpressurization Alarm Not in Correct State.Caused by Bistable Setpoint Drift.Alarm Unit Replaced

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/03L-0 on 790709:during RCS Cooldown,Operator Noted Channel P-452 Overpressurization Alarm Not in Correct State.Caused by Bistable Setpoint Drift.Alarm Unit Replaced
ML17261A135
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/08/1979
From: Edgar E
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17244A754 List:
References
LER-79-014-03L, LER-79-14-3L, NUDOCS 7908140800
Download: ML17261A135 (2)


LER-1979-014, /03L-0 on 790709:during RCS Cooldown,Operator Noted Channel P-452 Overpressurization Alarm Not in Correct State.Caused by Bistable Setpoint Drift.Alarm Unit Replaced
Event date:
Report date:
2441979014R03 - NRC Website

text

<<NRC FORM 366 79-014/03L-0 U. S. NUCLEAR REGULATORY COMMISS

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investigation showed power operator relief valve actuation bistable setpoint 8 psi above T.S. value.

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Bistable setpoint drift. Alarm unit was replaced with qualified spare, alarm setpoint was adjusted, and unit was tested successfully.

Unit was rechecked successfull on 7/16/79.

The alarm unit is a Foxboro model 63/U-AT-OHAA.

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