05000316/LER-1980-022-03, /03L-0:on 800503,radiation Monitor R-11 Alarmed During Normal Operation.Sample Pump for R-11 & R-12 Would Not Remain Running.Caused by Wear of Pump.Pump Replaced & Air Sampler Tested.Entire Sys Will Be Replaced

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/03L-0:on 800503,radiation Monitor R-11 Alarmed During Normal Operation.Sample Pump for R-11 & R-12 Would Not Remain Running.Caused by Wear of Pump.Pump Replaced & Air Sampler Tested.Entire Sys Will Be Replaced
ML17331A179
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 06/02/1980
From: Wizner D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A177 List:
References
LER-80-022-03L, LER-80-22-3L, NUDOCS 8006050312
Download: ML17331A179 (2)


LER-1980-022, /03L-0:on 800503,radiation Monitor R-11 Alarmed During Normal Operation.Sample Pump for R-11 & R-12 Would Not Remain Running.Caused by Wear of Pump.Pump Replaced & Air Sampler Tested.Entire Sys Will Be Replaced
Event date:
Report date:
3161980022R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION I7.77) l LICENSEE EVENT REPORT CONTROL BLOCK:

Qi (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)

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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T gQQ SDURcf ~LQB 0

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60 61'OCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10

~02 DURING NORMAL OPERATION RADIATION MONITOR R-11 ALARMED.

THE SAMPLE

~03 4

PUMP FOR R-11 AND R-12 WOULD NOT REMAIN RUNNING'HE SAMPLE PUMP WAS REMOVED FROM SERVICE CONSTITUTING AN INOPERABLE RAD MONITOR SYSTEM PER

~OS 0:

6 T.S. 3.3.3,1 AND TABLE 3.3-6.

THE ACTION REQUIREMENTS WERE MET, THIS EVENT H0ID NO EFFECT ON PUBLIC HEALTH AND SAFETY.

SIMILAR EVENTS

INCLUDE

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RO 79 034/03L Oi 80 013/03L Op 80 018/03L 0 AND FOR DOCKET 050 315'O 79 012/03L-0 AND 79-48/03L-O.

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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT R EV IS I ON LF RIIRO EVENTYEAR REPORT NO.

CODE TYPE NO.

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UC 2'I 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER 022 ~P022

~2022

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~ 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 FAILURE WAS DUE,TO WEAR OF THE PUMP.

THE COMPLETE PUMP WAS REPLACED AND v ~II THE AIR SAMPLER TESTED.

PLANS ARE TO REPLACE THE ENTIRE SYSTEM AS PART OF MODIFICATION RFC DC 12-2448.

4 CU ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ3

~16 Z

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10 44 PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

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11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 2

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11 12 LOSS OF OR DAMAGE,TOFACILITY 43 TYPE

DESCRIPTION

2 Z

042 NA 7

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10 PUBLICITY ISSUED DESCRIPTION Qs O

~NQ44 NA 7

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10 80 LOCATIONOF RELEASE QB 45 80 80 80 p>ohio So ~i~~Jup

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80 NRC USE ONLY DAVID G.

WIZNER 68 69, 80 p4oNE 6 1 6 46 5 5 9 0 1 p EXT 1 3 98 NAME OF PREPARER 7

8 9

FACILITY

~30 METHOD OF STATUS

% POWER OTHER STATUS ~

DISCOVERY DISCOVERY DESCRIPTION

~E022 ~10 0 022 NA

~A022 OPERATOR OBSERVATION 7

8 9

10

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