LER-1979-021, Supplemental LER 79-021/01T-1:on 791208,following Return to Svc After Refueling Outage,Primary Containment Pressure Would Not Stabilize.Caused by Leaking Due to Unevenly Tightened Bolts.New Controls & Hatch Lock to Be Used |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2961979021R00 - NRC Website |
|
text
UPDATE REPORT PREVTOU~PORT DATE 3.2-21;79 A
LlCENSEE EVENT REPORT v. o. gvut ncqsqgg.ge 4 wan 4 g,t4444444gvvgvgv 0
0 Qg 4
1 1
1 1 Q4~
Qg 25 26 LICENSE TYPE 30 S7 CAT 58 CONTROL BLOCK:
Q'PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 1 6
A L
B R
F 02 0
0 0
0 0
0 0
9 LICENSEE CODE 14 15 LICENSE NUMBER 7
8
~02 soURcE ~LOB 0
5 0
0 0
2 9
6 7
1 2
0 8
7 9
OB 0
2 0
5 8
0 O~
60 61 DOCKET NUMBER EVENT DATE 74
. 75 REPORT DATE 80 FVENT DESCRIPTION AND PROBABLE CONSEQUENCES 010 With unit 3 at 200 MWe followi the
~03, primary containment pressure would not stabi 1ize per Technical Specification
- 3. 7. a. 2 ~
u7m
~'"""'0 5
safety of the public; no previous similar occurrences.
~OS
~07
~DS 80 7
8 7
8 9
SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE g
~@A Q77
~AQ72
~CQT3 2
Z Z
Z 2
Z Q74
~ZQPg
~Z Qls 9
10 11 12 13 18
'19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.
CODS TYPE NO.
QI7 ggpoaT
~79
~
~02 1
~~
~01
~ ~
1 21 22 23 24 26 27 28 29, 30 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORMhUB.
SUPPLIER MANUFACTURER QIB ~GQI9
~BQ20 PJQ2' 023 ~8 ~ Q2S 9
Q20 33 34 35 36 37 40 41 42 43
, 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o
East drywall equipment hatch door was leakin due to two or ossibl three of twel~ve
- unevenly tightened bolts.
Bolts were reti htened and hatch assed LLRT.
A tive controls are being developed to incorporate additional verifications and the use 3
of a 1ock to insure that the hatch is not moved without ro er a rove 1 4
80 METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32
~A Q31 Maintenance personnel observed 45 46 LOCATIONOf RELEASE Q NA 80 80 44 45 80 9'
ll 12 LOSS OF OR DAMAGE TO FACILITYQ43 TYPE 'ESCRIPTION
~ZQ42 NA 9 'o PUBLICITY ISSUED DESCRIPTION~
~NQ44 NA 7
8 80 80 NRC USE ONLY
~4 Te 80 Ta 0
2 0
68 69 8 9'0 PHONEME NAME OF PREPARER Boogoso IEg+
7 8
9 FACILITY STATUS
% POWER OTHER STATUS Q 0
Qgg ~02 0 Qgg NA 8
9 10 '
12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ
~IB
~Z Q33 2 Q34 NA 7
8 9'o
.11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39
~oo o Q77~2Qgs NA 7
8 9
11 12 13 PERSONNEI. INJURIES NUMBER OESCRIPTIONQ41
~00 0 Qgo, 'NA
P
~ g I
~t je L
~:~, 7ennesse Valley Author ity Broivns Ferry Nuclear Plant Form BF-
- 'lv I.ER SUPPLEMENTAL lNFORNA'I1ON BFRO-5G-296 /
7921 Technical Specification Involve('.
4 ~ 7 A.2 ~ g Reported Under Technical SpecZication
- 6. 7. 2.a. 3 Date nf Occurrence 12/8/79 Time of Occurrence 7:10 p m i!nit Identification and Desc~ri tion'of Occurrence:
Initial difficultywith maintenance of drywell to torus pressure differential. Later it was discovered that excessive drywell leakage existed.
Leakage path identified and repaired at 0830, 12/4/79, within 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> limit per technical specification 4.7.A.2.h(2).
Conditions'Prior to Occurrence:
Unit 1 at 970 MWe, end-of-cycle coastdown.
Unit 2 at 880 MWe, limited by 2A reactor feed pump maintenance, unit 3 load at approximately 200 MWe following return to service of unit from refueling outage at 1615, 12/8/79. Unit in test program.
Actioti specified in the Technical Specification S>>rvcill itic~
1(equtrements mct due to inc~et ahl>> eqt~ipment..
l)csrt ibe.
Action specified in 4.7.A.2.g requires repairs to primary containment penetration leakage be ini.tiated immediately and that unit be shutdown within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> following detection if the leakage is not corrected.
parent Cause of Occurrence:
Leak around east equipment hatch seal due to 2 or possibly 3 loose fasteners immediately terminated leakage.
Analysis of Occurrence: There was no danger to health or safety of the public, no activity
- release, no damage to plant equipment.
East equipment hatch was installed and initially failed a local leak rate test on ll/14/79.
The hatch was retorqued and passed the local leak rate test on ll/14/79. An integrated leak rate test was conducted between ll/21/79, and 11/26/79.
No leakage was observed on the east equipment hatch.
No other work was performed on southeast equipment hatch until the subject occurrence on 12/8/79.
Corrective Action
Retightening of fasteners corrected leakage.
Developing administrative controls including detailed instructions and procedures which incorporate appropriate signoffs and a. lock that will insure that the hatch is not moved without proper approval.
Fatlur>> !inta:
Tlone
+Bcvts Y>n:
Period
- - L>fctinM; Rc:;pen ihility - Administrative Supervisor s
c
f
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000296/LER-1979-001-03, /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | | | 05000296/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000259/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | | | 05000260/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000260/LER-1979-001-03, /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | | | 05000296/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000259/LER-1979-002-03, /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | | | 05000259/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000260/LER-1979-002-03, /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | | | 05000260/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000296/LER-1979-002-03, /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | | | 05000296/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000259/LER-1979-003-01, /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | | | 05000259/LER-1979-003, Forwards LER 79-003/01T-1 | Forwards LER 79-003/01T-1 | | | 05000260/LER-1979-003-01, /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | | | 05000259/LER-1979-003-03, /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | | | 05000296/LER-1979-003-03, /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | | | 05000260/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000260/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004-03, /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on | /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on Site | | | 05000296/LER-1979-004-03, /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | | | 05000260/LER-1979-004-03, /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | | | 05000296/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | | | 05000296/LER-1979-005-01, /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | | | 05000259/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000259/LER-1979-005-03, /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | | | 05000260/LER-1979-005-03, /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | | | 05000260/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000296/LER-1979-006-03, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | | | 05000296/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000259/LER-1979-006-03, /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | | | 05000259/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006-03, /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | | | 05000260/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007-03, /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | | | 05000260/LER-1979-007-03, /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | | | 05000260/LER-1979-008-01, /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | | | 05000259/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000259/LER-1979-008-03, /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | | | 05000296/LER-1979-008-03, /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | | | 05000260/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000296/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000296/LER-1979-009-03, /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | | | 05000260/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000296/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | |
|