Similar Documents at Surry |
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LER-1979-027, /01T-0:on 791003,review in Response to IE Bulletin 79-14 Indicated Three Bypass Lines & One Safety Injection Line W/Stresses in Excess of Allowable Limits.Caused by Inaccurately Installed Piping Line Supports.Mod to Be Made |
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NRC FORM 366 fZ-'!77y;.;,*
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Attachment (Page 1 of Surry Power Station, Unit Docket No: 50-280 1
Report No: 79-027/0lT-O Event Date:
10/3/79 Title of Event:
Excess Stress in RTD Bypass and Safety Injection Lines
- 1.
Description of Event
With both units at cold shutdown, the ongoing review in response to IE Bulletin No. 79-14, indicated that three (3) RTD bypass lines and (1) Safety Injection line showed stresses in excess of the allowable limits.
The event is reportable in accordance with Technical Specification 6.6.2.A.9.
- 2.
Probable Consequences/Status of Redundant Systems:
- 3.
- 4.
The review indicated that the subject as-built safety-related piping lines would yield stresses in excess of allowable in the event of a seismic event *. Since the unit was at cold shutdown, the health and safety of the general public were not affected.
Cause
A comparison was made of the field verified piping line configuration against the presently available design documents.
This comparison indicated that the subject piping line supports are not installed in accordance with the presently available design documents.
Immediate Corrective Action
Upon the discovery of the piping line support discrepancies, a detailed analysis was initiated and modifications are being made as necessary.
- 5.
Scheduled Corrective Action:
The modifications will be made prior to the* unit startup and no further action is deemed necessary.
- 6.
Action Taken to Prevent Recurrence:
The ongoing review will continue in response to I.E. Bulletin No. 79-14.
If during this review any modifications are identified, they will be evaluated under the requirements of the Technical Specifications.
- 7.
Generic Implications:
Since IE Bulletin No. 79-14 covers the seismic analysis of all safety-re-lated piping systems in the plant, there are no generic implications associated with this event.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | | | 05000281/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000281/LER-1979-004-03, /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | | | 05000280/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000281/LER-1979-005-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | | | 05000280/LER-1979-005-03, /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | | | 05000280/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000280/LER-1979-006-03, /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | | | 05000281/LER-1979-006-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | | | 05000280/LER-1979-007-03, /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | | | 05000280/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000281/LER-1979-007-03, /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | | | 05000281/LER-1979-008-03, During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | | | 05000281/LER-1979-008, Forwards Updated LER 79-008/03X-1 | Forwards Updated LER 79-008/03X-1 | | | 05000280/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000280/LER-1979-008-01, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | | | 05000280/LER-1979-009-01, /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | | | 05000280/LER-1979-009, Forwards LER 79-009/01T-0 | Forwards LER 79-009/01T-0 | | | 05000281/LER-1979-009-03, /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | | | 05000281/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000280/LER-1979-010-03, /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | | | 05000280/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010-03, /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | | | 05000280/LER-1979-011-03, /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | | | 05000280/LER-1979-011, Forwards LER 79-011/03X-1 | Forwards LER 79-011/03X-1 | | | 05000281/LER-1979-011, Forwards LER 79-011/12T-0 | Forwards LER 79-011/12T-0 | | | 05000281/LER-1979-011-12, /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | | | 05000280/LER-1979-012-03, During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | | | 05000280/LER-1979-012, Forwards Updated LER 79-012/03X-1 | Forwards Updated LER 79-012/03X-1 | | | 05000281/LER-1979-012, Forwards LER 79-012/08T-0 | Forwards LER 79-012/08T-0 | | | 05000281/LER-1979-012-08, /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | | | 05000280/LER-1979-015-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | |
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