Similar Documents at Surry |
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LER-1979-026, Westinghouse Told Util of Possible Failure of Certain Control Sys,Previously Assumed to Remain as is, to Fail Under Adverse Environ Conditions. FSAR Reviewed.Present Analyses Unaffected |
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LICENSEE EVENT REPORT C;~TROL BLOCK: l 10 (PLEASE PRINT OR TVP.L REQUIRED INFORMATION)
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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T I O I 1 I 7
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80 jOn August 29, 1979, Westinghouse informed Vepco that it could be possible for lo !JI !certain control systems, whi.ch were previously assumed to remain 1' 1as istt, to fail to !4 I 1when subjected to an adverse environment thus causing an impact on present safety I O Is 1,analyses.
Review of the FSAR revealed that the potential problems identified are not jo ls I routside the existing analyses, therefore the health and safety of the general public jo j 7 I !were not affected by this event.
Reportable pursuant to T.S. 6~6.2.a~9.
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CAUSE
CAUSE COMP.
SYSTEM CODE CODE SUB CODE COMPONENT CODE SUSCOOE VALVE SUSCOOE JZ IZ I@ 12.J@ l~J@ I z I z I z I z I z I z 1@ ~ L:J@
9 10 11 12 13 SEQUENTIAL t:'::-.
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. REPORT NO.
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I I O I 21 61 I......-I 21 22 23 24 26 27 TAKEN ACTION ON PLANT METHOD HOURS 22 18 OCCURRENCE CODE I 0- I 11 19 REPORT TYPE
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30 20 31 28 29 ATTACHMENT NPRD4 FORM~UB.
SUBMITTED PRIMEC::OMP.
SUPPLIER REVISION NO.
L!J 32 COMPONENT MANUFACTURER ACTION FUTURE EFFECT SHUTDOWN
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42 43 44 47 I 1 I O I jReanalysis by Westinghouse has identified potential environmental Interaction in the
! 1 j, I I steam generato.r power operated relief valve control sys*tem~ the pressurizer pressure
- , 12,.I control system, the main feedwater control system, and the rod control system,.
!l!J! ! FSAR was reviewed and results determi.ned that present analyses are unaffected.,
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. FACILITY STATUS
% POWER
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ACTIVITY CONTENT C\\
RELEASED OF RELEASE AMOUNT OF ACTIVITY IE] LlJ @) LllI NA 7
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PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 39 OTHERSTATUS @
NA METHOD OF DISCOVERY OESCRIPTI_ON DISCOVERY LJ@I NA 44 45 46 LOCATION OF RELEASE@
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11 12 LOSS OF OR DAMAGE TO FACILITY '43' TYPE
DESCRIPTION
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__.168 69 NAMF ns: PAi:P.at:1i:t:1 W. L. Stewart
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804-359-3184 80 o 0
II.
e UPDATE REPORT e SURRY POWER DOCKET NO.
REPORT NO.
EVENT DATE:
STATION, UNIT NO. 1 50-280 LER-79-026/0lX-1 08/29/79 TITLE OF REPORT:
Balance of Plant Equipment on Safety Systems
- 1.
Description of Event
On August 29, 1979, Westinghouse informed VEPCO that existing safety.analyses could be invalidated by the failure of certain control systems, which were previously assumed to remain 11as is 11, when subjected to a severe environment following a high energy line rupture.
This event is reportable pursuant to T. S. 6.6.2.a.9.
- 2.
Probable Consequences of Occurrence:
The consequences of this event were minimal.
The FSAR was reviewed to determine the impact of adverse environment on the control systems affecting present analyses and results determined that present analyses are unaffected by this event.
Unit No. 2 has the same design and is similarly unaffected
- 3.
Cause of Occurrence:
Reanalysis by Westinghouse has identified potential environmental inter-action in the steam generator power operated relief valve control system, pressurizer pressure control system, main feedwater control system, and rod contro1 system.
- 4.
Immediate Corrective Action~
- 5.
The FSAR was reviewed for a feedwater 1 ine break and a steaml ine break and it was detennined that the new potential problems identified by Westinghouse are not outside the existing analyses.
Subseq~oent Corrective Action and Action Tak.en 10 Prevent Recurrence:
Since: the initial Westinghouse notification, Westinghouse and VEPCO m~t with the staff on September 18, 1979, and discussed the scenarios.
An agreement was reached that we would address these four scenarios immedjatel'y and then continue the review of other items including unaddressed interactions.
This continuing review will be done wi_th the assistance of the appropriate vendor.
The initial review.indicates that Surry has no additional potential interaction.
between balance of plant (BOP) systems and NSSS safety grade equipment for ihe indicated systems.
There are no potential problems with the Feedwater Control or Automatic Rod Control Systems.
The specifics of each case are addressed below:
e UPDATE REPORT
- 5.
Subsequent Corrective Act-ion and Action Taken to Prevent Recurrence -cont'd
- 1.
The three steam generator power operated relief valves (SG-PORV) are postulated to fail open as a result of a main feed line break outside the containment between the penetration and the feedline check valve which would affect the SG-PORV control system *.
The SG-PORV's are located in the Main Steam Valve House which is*
immediately adjacent to the reactor containment.
This building is designed to release the energy of a High Energy Line Break to the atmosphere.
The main feed line exits the containment within this building and the distance from the main feed line penetration to the main feed line check valve is less than five feet.
The SG-PORV's are designed to fail closed on a loss of air or loss of electrical signal to the controls.
The Westinghouse recommended short term action is to instruct the control room operators that a loss of main feed may cause the SG-PORV's to fail ope_n which could cause a loss of the steam driven auxiliary feedwater pump.
Surry has two half-size motor driven auxiliary feedwater pumps in addition to the full size turbine driven auxiliary feedwater pump, and as the Surry FSAR states, one motor-driven pump alone provides sufficient feed flow.
In addition, an auxiliary feedwater cross-connect exists which enables one unit's steam generators to be fed by the other units auxiliary feedwater system.
Considering these design features, the short term action is considered sufficient.
- 2.
The main feedwater control system is postulated to fail and this reduces the mass in the steam generator to less than analyzed. -This failure of-the main feed control system is assumed to occur as~ result ofa small main feedline break (less than 0.2 sq. ft.) between the steam generator nozzle and the feedline check valve.
The main feed control system is located outside the containment in the Service Building.
The postulated break would have to occur within the containment as the first check valve is located within containment.
Only protection grade equipment associated with the main feedwater control system would be affected and not the lesser quality control grade equip-ment as postulated.
Therefore, this scenario is not applicable to Surry.
- 3.
- Toe pressurizer power operated relief valves (P-PORV) are postulated to fail open upon a feedline break between the steam generator and the containment penetration.
The P-PORV's are designed to fail closed on a loss of air, or loss of electrical signal to the controlling solenoid valves.
The postulated events require that for the short term resolution the Westinghouse recommendation is followed and that the control room operators are instructed that a High Energy Line Break within the containment might cause the P-PORV's to fail open or to fail closed.
The action will be to close the block valves in the P-PORV lines after the problem has been analyzed.
s.
b.
UPDATE REPORT -
Subsequent Corrective Action and Action Taken To Prevent Recurrence (Continued):
- 4.
The automatic rod control system was postulated to receive an erroneous signal from the excore detection system following an inside containment intermediate steamline break (0.1-0.25 sq. ft.) between 70-100 percent power.
This erroneous signal must occur within the first two minutes of the accident and will cause the rods to withdraw.
Westinghouse has provided VEPCO with a generic intermediate steamline rupture analysis which resulted in a rod withdrawal due to a cont_rol system environmental interaction prior to a reactor trip.
Westinghouse states that the results of the analysis indicated that no fuel damage occurred, which is consistent with the assumptions made in the Safety Analysis Report.
Generic Implications:
The systems were reviewed as required~ and it was determined that the present analysis was unaffected.
The generic implication of the potentia1 systems problems does not apply to th.is station.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | | | 05000281/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000281/LER-1979-004-03, /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | | | 05000280/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000281/LER-1979-005-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | | | 05000280/LER-1979-005-03, /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | | | 05000280/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000280/LER-1979-006-03, /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | | | 05000281/LER-1979-006-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | | | 05000280/LER-1979-007-03, /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | | | 05000280/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000281/LER-1979-007-03, /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | | | 05000281/LER-1979-008-03, During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | | | 05000281/LER-1979-008, Forwards Updated LER 79-008/03X-1 | Forwards Updated LER 79-008/03X-1 | | | 05000280/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000280/LER-1979-008-01, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | | | 05000280/LER-1979-009-01, /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | | | 05000280/LER-1979-009, Forwards LER 79-009/01T-0 | Forwards LER 79-009/01T-0 | | | 05000281/LER-1979-009-03, /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | | | 05000281/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000280/LER-1979-010-03, /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | | | 05000280/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010-03, /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | | | 05000280/LER-1979-011-03, /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | | | 05000280/LER-1979-011, Forwards LER 79-011/03X-1 | Forwards LER 79-011/03X-1 | | | 05000281/LER-1979-011, Forwards LER 79-011/12T-0 | Forwards LER 79-011/12T-0 | | | 05000281/LER-1979-011-12, /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | | | 05000280/LER-1979-012-03, During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | | | 05000280/LER-1979-012, Forwards Updated LER 79-012/03X-1 | Forwards Updated LER 79-012/03X-1 | | | 05000281/LER-1979-012, Forwards LER 79-012/08T-0 | Forwards LER 79-012/08T-0 | | | 05000281/LER-1979-012-08, /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | | | 05000280/LER-1979-015-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | |
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