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LER-1981-001, /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired |
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LICENSEE EVENT REPORT LI.NUCLEAR REGULATORY COMMISSION CO\\'JTROL BLOCK:._I_...____.... _ _.___. _ _..____,! G) 1 6
(PLEASE PRINT OR TYPE t:LL REQUIRED INFORMATION)
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LICENSEE CODE 14 1S LICENSE NUMBER 25 26 LICENSe TYPE
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68 69 EVENT DATE 74 7S REPORT DATE 80 E:VE'\\IT DESCRIPTION AND PROBABLE CONSEQUENCES@
!With the unit defueled, RT examination of loops A, B, C, main steam piping.revealed C£::J]J !linear i~di~ations at the weld near the safety va~ve riser:
RT examination was
[]JI] !being conducted as *follow-up to the finding reported in LER 80-067/0lT-Oo This event!
C2:l}] jis reportable per T.S. 6~6.2.a.(9).
The indications found represent surface pitting
[)))) 1and were code allowable.
Therefore, the health and safety of the public were not [IT:] !affected.
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SYSTEM CODE 1c 1c I@
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LEA/RO CVENT YEAR
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NUMBER 21 22
CAUSE
CAUSE COMP.
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- 11.
12 13 18 19 SEQUENTIAL OCCURRENCE REPORT VALVE SUBCOOE
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CODE TYPE I I I O I 01 11 1.,.....1 I 01 11 lLl l=1 23
- 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN t.::\\
ATTACHMENT NPR04 PRIME COMP.
REVISION NO.
LQJ 32 COMPONEI\\IT MANUFACT..JRER 80 TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM liUB.
SUPPLIER W@W@ LU@ 1.U I 01 01 01 01 L!J@). LI W 33 34 35 36 37
. 40 41 42 43 I GI 21 s 1 7 !@)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
44 47 tfhe cause,appears to be a type of corrosion pitting usually associated with stagnant 0JJJ,oxygenated water. - ~he-subject_-areas w:t;n be r.epaired_pri)JtJ;o *startup Of the unit.
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FACILITY
'3a' METHOD OF STATUS
% POWER OTHER STATUS \\;:::J DISCOVERY DISCOVERY DESCRIPTION Inservice Inspection so tITIJ l!J@ I O I O I O !@)jS/G:::Repla~ement::. j- ~I 7
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10 12 1'3 44 45 ----------------"------180 ACTIVITY CONTENT t:;;;\\
RELEASEO OF RELEASE AMO.UNT OF ACTIVITY [ill] uJ @) LJ@I.___N_A _____
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9 10 11 NA
_LOCATION OF RELEASE @
44 45 80
?ERSONNEL EXPOSURES r:;;:;.,
NUMBER
~
TYPE
DESCRIPTION
- ., ETI] -Jo* jO jO !~@.__ __
N_A _____________________
---1 7
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?ERSONNEL INJURIES (A'.;\\
NUMBER DESCRIPTION~
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NRC USE ONL y IIITJ lN.J6 _______
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J. L. Wilson (804) 357-3184 NAME::)!= OPEPARE=l-------~.:......--------
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f ;-*~ATTACHMENT 1, PAGE 1 OF 2.
SURRY POWER STATION, UNIT
! 1 e
DOCKET NO:
50-280 REPORT NO:
80-001/0lT-0 EVENT DATE:
02-25-81
/
TITLE OF EVENT:
MAIN STEAM PIPING DISCREPANCIES
- 1.
DESCRIPTION OF EVENT
With the unit defueled for steam generator replacement, RT examination of loop
'A' main steam piping revealed linear indications.
The indications are located in the vicinity of the welds that are adjacent to the safety valve riser stab-in.
The safety valve riser is located outside the containment.
The indications are in the lower third of the pipe's*circumference and at the transition of a counter bore.
RT examination was being conducted as a follow-up to the findings reported on Unit No. 1 LER 80-067/0lT~
Subsequent.RT examination of loops 'B' and 'C' main steam piping revealed similar indications at corresponding locations.
This event is being*reported pursuant. to Technical Specification 6.6.2.a.(9).
- 2.
PROBABLE CONSEQUENCES The indications found were allowable per ASME Section XI.
In addition, the indi-cations were substantially less than the critical flaw size as referenced in the FSAR, Appendix D.
Therefore, the health and safety of the public were not affected.
- 3.
CAUSE
- 4.
The cause appears to be a type of corrosion pitting usually associated with stagnant oxygenated water.
The "boat samples" were removed from A & C Main Steam piping and subjected to X-ray, macroscopic, and microscopic examination, revealing only corrosion pits and no cralking.
IMMEDIATE CORRECTIVE ACTION
The indications were verified by liquid penetrant examination.
- 5.
SUBSEQUENT CORRECTIVE ACTION:
The subject areas will be repaired prior to startup of the unit. Also, the shape of the counter-bore will be changed to reduce the stress in this area.
<:_:*,.:;-~so-'6*. *- ACTIONS TAKEN TO PREVENT RECURRENCE:
As noted above, the indications were within code allowable tolerances.
Routine surveillance as required by*T.S. 4.15" is considered adequate to detect problems in the future.
(/
-..... :ATTACHNENT 1, PAGE 2 OF 2-SURRY POWER STATION, UNIT NOo 1 DOCKET NO:
50-280 REPORT NO:
80-001/0lT-0
£VENT DATE 02-25-81 TITLE OF EVENT:
MAIN STEAM PIPING DISCREPANCIES
- 7.
GENERIC IMPLICATIONS:
e A special UT examination was conducted of the corresponding areas of main steam piping on Unit 2, while the unit was at power.
- - The examination found no evidence of cracking or other significant indications that could be attributed to internal flaws.
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| 05000280/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000280/LER-1981-001-01, /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | | | 05000281/LER-1981-001-03, /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | | | 05000280/LER-1981-002-03, /03L-0:on 810122,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Shutdown & Defueled Conditions.Activity Levels Verified within Allowable Limits | /03L-0:on 810122,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Shutdown & Defueled Conditions.Activity Levels Verified within Allowable Limits | | | 05000281/LER-1981-002-03, /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced | /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced | | | 05000280/LER-1981-003-03, /03L-0:on 810129,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Decrease in Background Radiation Levels.Activity Levels Verified within Allowable Limits | /03L-0:on 810129,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Decrease in Background Radiation Levels.Activity Levels Verified within Allowable Limits | | | 05000281/LER-1981-003-03, /03L-0:on 810106,liquid Radwaste Monitors RM-GW-101,102,RM-VG-103,104,RM-SW-107 & RM-LW-108 Failed Low.Caused by Failed Fuse.Fuse Replaced | /03L-0:on 810106,liquid Radwaste Monitors RM-GW-101,102,RM-VG-103,104,RM-SW-107 & RM-LW-108 Failed Low.Caused by Failed Fuse.Fuse Replaced | | | 05000280/LER-1981-004-03, Radiation Monitoring Recorder (RR-175) Found to Be Printing Erratically.Caused by Loose Gear on Balance Motor,Allowing Drive Cable to Slip.Set Screw on Drive Gear Tightened | Radiation Monitoring Recorder (RR-175) Found to Be Printing Erratically.Caused by Loose Gear on Balance Motor,Allowing Drive Cable to Slip.Set Screw on Drive Gear Tightened | | | 05000280/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000281/LER-1981-004-03, /03L-0:on 810107,reactor Trip Breaker a Failed to Open.Caused by Sporadic Failure of Under Voltage Device Due to Missing Bushing.Under Voltage Device Replaced | /03L-0:on 810107,reactor Trip Breaker a Failed to Open.Caused by Sporadic Failure of Under Voltage Device Due to Missing Bushing.Under Voltage Device Replaced | | | 05000280/LER-1981-005-03, /03L-0:on 810301,radiation Monitor Recorder RR-175 Found Printing Erratically.Caused by Dirty Slidewire Resistor in Circuit That Controls Positioning of Printing Device.Resistor Cleaned & Recorder Returned to Svc | /03L-0:on 810301,radiation Monitor Recorder RR-175 Found Printing Erratically.Caused by Dirty Slidewire Resistor in Circuit That Controls Positioning of Printing Device.Resistor Cleaned & Recorder Returned to Svc | | | 05000281/LER-1981-005-03, /03L-0:on 810204,air Motors for Preferred Start 2 of Emergency Diesel Generator 3 Found Engaged to Flywheel. Caused by Air Leakage Through Solenoid Valve.Solenoid & Air Motors Replaced | /03L-0:on 810204,air Motors for Preferred Start 2 of Emergency Diesel Generator 3 Found Engaged to Flywheel. Caused by Air Leakage Through Solenoid Valve.Solenoid & Air Motors Replaced | | | 05000280/LER-1981-006-03, /03L-0:on 810306,alarm Setpoint for Component Cooling Water Radiation Monitor RM-CC-106 Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset to Proper Setpoint & Returned to Svc | /03L-0:on 810306,alarm Setpoint for Component Cooling Water Radiation Monitor RM-CC-106 Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset to Proper Setpoint & Returned to Svc | | | 05000281/LER-1981-006-03, /03L-0:on 810114,at Full Power,C Safety Injection Accumulator Found to Have Boron Concentration of 1943 Ppm, 7 Ppm Below Required Limit.Caused by Leakage Through Check Valve 1-SI-144.Valve Isolated | /03L-0:on 810114,at Full Power,C Safety Injection Accumulator Found to Have Boron Concentration of 1943 Ppm, 7 Ppm Below Required Limit.Caused by Leakage Through Check Valve 1-SI-144.Valve Isolated | | | 05000280/LER-1981-007-03, W/Unit 1 Defueled & 2 at 100% Power,Power for Several Radiation Monitors Lost.Caused by Shorting of Test Lead to Ground Causing Supply Fuse to Blow.Fuse Replaced.Monitors Returned to Svc | W/Unit 1 Defueled & 2 at 100% Power,Power for Several Radiation Monitors Lost.Caused by Shorting of Test Lead to Ground Causing Supply Fuse to Blow.Fuse Replaced.Monitors Returned to Svc | | | 05000281/LER-1981-007-03, /03L-0:on 810114,at 100% power,PT-27 (Heat Tracing) Revealed Amp Readings for Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | /03L-0:on 810114,at 100% power,PT-27 (Heat Tracing) Revealed Amp Readings for Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | | | 05000281/LER-1981-008-03, /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | | | 05000280/LER-1981-008-03, /03L-0:on 810410,process Vent Radiation Monitor Found Inoperable.Caused by Broken Pump Drive Belt Due to Misalignment.Drive Belt Replaced & Radiation Monitor Operability Verified | /03L-0:on 810410,process Vent Radiation Monitor Found Inoperable.Caused by Broken Pump Drive Belt Due to Misalignment.Drive Belt Replaced & Radiation Monitor Operability Verified | | | 05000280/LER-1981-009-01, /01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made | /01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made | | | 05000281/LER-1981-009-03, /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 11 Circuit 4C.Caused by Short in Heat Tape.Defective Heat Tracing Replaced.Design Change Initiated | /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 11 Circuit 4C.Caused by Short in Heat Tape.Defective Heat Tracing Replaced.Design Change Initiated | | | 05000280/LER-1981-010-03, /03L-0:on 810415,alarm Setpoints for RM-CC-105 & RM-CC-106 Found Greater than Tech Spec Limits on Several Occasions.Caused by Misinterpretation of Background & Insufficient Guidelines for Evaluation of Alarm Setpoint | /03L-0:on 810415,alarm Setpoints for RM-CC-105 & RM-CC-106 Found Greater than Tech Spec Limits on Several Occasions.Caused by Misinterpretation of Background & Insufficient Guidelines for Evaluation of Alarm Setpoint | | | 05000281/LER-1981-010-03, /03L-0:on 810209,svc Water pump,2-SW-P-10B, Developed Low Discharge Pressure.Caused by Eel Lodged in Impeller.Eel Removed & Pump Returned to Svc | /03L-0:on 810209,svc Water pump,2-SW-P-10B, Developed Low Discharge Pressure.Caused by Eel Lodged in Impeller.Eel Removed & Pump Returned to Svc | | | 05000281/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000280/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000281/LER-1981-011-03, /03L-0:on 810119,fire Watch Not Maintained While Fuel Oil Pumphouse Carbon Dioxide Sys Out of Svc for Design Change Mods.Caused by Personnel Leaving Post.Fire Watch re-established & Personnel Disciplined | /03L-0:on 810119,fire Watch Not Maintained While Fuel Oil Pumphouse Carbon Dioxide Sys Out of Svc for Design Change Mods.Caused by Personnel Leaving Post.Fire Watch re-established & Personnel Disciplined | | | 05000280/LER-1981-011-03, /03L-0:on 810426 & 27,process Vent Radiation Monitors Flooded Due to Introduction of Water Into Process Vent Sys.Caused by Failure of Primary Drain Tank Level Control Sys.Monitors Drained & Vacuum Pump Replaced | /03L-0:on 810426 & 27,process Vent Radiation Monitors Flooded Due to Introduction of Water Into Process Vent Sys.Caused by Failure of Primary Drain Tank Level Control Sys.Monitors Drained & Vacuum Pump Replaced | | | 05000281/LER-1981-012-03, /03L-0:on 810118,boric Acid Transfer Pump 1-CH-P-2D Failed.Caused by Bearing Failure Due to Oil Seal Failure.Pump Repaired | /03L-0:on 810118,boric Acid Transfer Pump 1-CH-P-2D Failed.Caused by Bearing Failure Due to Oil Seal Failure.Pump Repaired | | | 05000280/LER-1981-012-03, /03L-0:on 810506,seismic Instrumentation Found Not Calibr According to Tech Specs.Caused by Defective Procedures.Periodic Test Had Been Mislabeled as Calibr Procedure.Instrumentation Calibr Using Approved Procedure | /03L-0:on 810506,seismic Instrumentation Found Not Calibr According to Tech Specs.Caused by Defective Procedures.Periodic Test Had Been Mislabeled as Calibr Procedure.Instrumentation Calibr Using Approved Procedure | | | 05000281/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000281/LER-1981-013-03, /03L-0:on 810119,improperly Sealed Fire Barrier Penetration Discovered.Caused by Improper Matl Being Packed Into Penetration.Penetration Properly Sealed | /03L-0:on 810119,improperly Sealed Fire Barrier Penetration Discovered.Caused by Improper Matl Being Packed Into Penetration.Penetration Properly Sealed | | | 05000280/LER-1981-013-03, /03L-0:on 810527,radiation Monitor Recorder RR-100 Was Found Indicating Decade Lower than Corresponding Monitors.Caused by Dirty Contacts in Circuit Controlling Positioning of Printing Device.Contacts Cleaned | /03L-0:on 810527,radiation Monitor Recorder RR-100 Was Found Indicating Decade Lower than Corresponding Monitors.Caused by Dirty Contacts in Circuit Controlling Positioning of Printing Device.Contacts Cleaned | | | 05000281/LER-1981-014-03, /03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset | /03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset | | | 05000280/LER-1981-014-03, /03L-0:on 810523,auxiliary Bldg Filter Banks Were Found to Be Less Efficient than Required by Tech Spec.Caused by Formation of Void Areas Due to Settling of Charcoal in Filters.Charcoal Added | /03L-0:on 810523,auxiliary Bldg Filter Banks Were Found to Be Less Efficient than Required by Tech Spec.Caused by Formation of Void Areas Due to Settling of Charcoal in Filters.Charcoal Added | | | 05000280/LER-1981-015, Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | | | 05000280/LER-1981-015-03, /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | | | 05000281/LER-1981-015-03, /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor Pump Failed to Rotate.Caused by Failure of Pump Bearings.Pump Replaced | /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor Pump Failed to Rotate.Caused by Failure of Pump Bearings.Pump Replaced | | | 05000281/LER-1981-016-03, /03L-0:on 810119,at 100% Power,Positive Pressure Greater than 0.05 Inches Water Could Not Be Maintained in Control Room.Caused by Deteriorated Seals on Door to Control Room Complex.Defective Doors Repaired | /03L-0:on 810119,at 100% Power,Positive Pressure Greater than 0.05 Inches Water Could Not Be Maintained in Control Room.Caused by Deteriorated Seals on Door to Control Room Complex.Defective Doors Repaired | | | 05000281/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000280/LER-1981-016-03, /03L-0:on 810615,primary Sys Chloride Concentration Exceeded Tech Specs.Apparently Caused by Personnel Working on Minor Repairs to Closure Stud Hole on Reactor Vessel Flange.All Sources of Makeup Water Checked | /03L-0:on 810615,primary Sys Chloride Concentration Exceeded Tech Specs.Apparently Caused by Personnel Working on Minor Repairs to Closure Stud Hole on Reactor Vessel Flange.All Sources of Makeup Water Checked | | | 05000281/LER-1981-017-03, /03L-0:on 810210,intermediate Range Channel N36 High Level Trip Setpoint Found in Excess of Tech Spec.Caused by Setpoint Drift.Setpoint Adjusted | /03L-0:on 810210,intermediate Range Channel N36 High Level Trip Setpoint Found in Excess of Tech Spec.Caused by Setpoint Drift.Setpoint Adjusted | | | 05000280/LER-1981-017-03, /03L-0:on 810702,discovered That No Fire Watch Had Been Posted for Two Unsealed Fire Barrier Penetrations in Cable Spreading Room Area.Caused by Const Personnel Error. Fire Watch Posted & Seal Installed | /03L-0:on 810702,discovered That No Fire Watch Had Been Posted for Two Unsealed Fire Barrier Penetrations in Cable Spreading Room Area.Caused by Const Personnel Error. Fire Watch Posted & Seal Installed | | | 05000280/LER-1981-018-03, Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | | | 05000281/LER-1981-018-03, /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | | 05000280/LER-1981-019-01, /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | | | 05000281/LER-1981-019-03, /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | | | 05000281/LER-1981-020-03, /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | | | 05000280/LER-1981-020-03, Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | | | 05000281/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000280/LER-1981-021-03, /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | | | 05000280/LER-1981-021, Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | |
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